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Industrial Application of Two Stage Industrial Application of Two Stage
Dry Pulverized Coal GasificationDry Pulverized Coal GasificationDry Pulverized Coal Gasification Dry Pulverized Coal Gasification
TechnologyTechnologyTechnologyTechnology
HuanengHuaneng Clean Energy Research InstituteClean Energy Research InstituteHuanengHuaneng Clean Energy Research InstituteClean Energy Research Institute
Nov 2012Nov. 2012
ChiChi HH GGChina China HuanengHuaneng GroupGroup
The Largest Independent Power Company In China, No.2 in the
world.
Clean Energy Research Institute(HNCERI)Clean Energy Research Institute(HNCERI)Clean Energy Research Institute(HNCERI)Clean Energy Research Institute(HNCERI)Research on clean coal power generation
and renewable generation technologyand renewable generation technology.
Thermal Power Research Institute(TPRI)Thermal Power Research Institute(TPRI)A principal and leading research institute
in the field of thermal power engineering.Dr. Xu Shisen
President of HNCERI
Scientist of Gasification
15 years efforts on coal gasification technology15 years efforts on coal gasification technology
•• The first stage—Theoretical Research and Simulation (1993~1997);
• Th d t B h S l E i t• The second stage—Bench Scale Experiments
(1997~2001);
• Th hi d Pil S l E i• The third stage—Pilot Scale Experiments
(2001~2005);
•• The fourth stage—Industrialization
(2006~);
Coal gasification and IGCCCoal gasification and IGCC
Pilot Scale:Pilot Scale: 36t/d(10MWth) ,2005
B h S l 0 7t/d 1998Bench Scale: 0.7t/d,1998Commercial Scale:1000t/d~2000t/d,2012
Gasifier Type:• Entrained flow• D f d• Dry feed• Pure oxygen• Water wall • Pressure: ~4.0MPa• Two Stages Reaction• Cold syngas efficiency: >81%Cold syngas efficiency: >81%• CO+H2>90%• Carbon conversion>99%•• Syngas cooler and quencher
Configuration of HCERI Two-stage Entrained Flow Gasifier
Syngas Cooler ProcessSyngas Cooler Process(SGC) Syngas Quencher Process
(SGQ)
CHNG GreenGen ProjectCHNG GreenGen Project
GreenGen Ltd CoGreenGen Ltd., Co.
The First IGCC Power Plant in China China Huaneng Group, Holding Company,
financial contribution 52%
China Datang Group 6%
China Huadian Corporation 6% China Huadian Corporation 6%
China Guodian Corporation 6%
China Power Investment Corporation 6% China Power Investment Corporation 6%
Shenhua Group 6%
St t D l t & I t t C 6% State Development & Investment Co. 6%
China Coal Group 6%
Peabody Energy USA 6%
CHNG Green Gen ProjectCHNG Green Gen Project
CHNG Green Gen Project
Design Points
CHNG Green Gen Project
Design Points
• SGC Process
• Gasifier Capacity: 2000t/d;
• Pressure: 3.0 MPa;;
• Entrained gas: N2
• Effective syngas flow(CO+H2+CH4): 137 600Nm3/h;• Effective syngas flow(CO+H2+CH4): 137,600Nm /h;
• Cold gas efficiency:83%;
• Eff ti t(CO+H +CH ) 91%• Effective component(CO+H2+CH4): 91%;
• Net Power: 250MW;
CHNG Green Gen Project
Commissioning and Operation
CHNG Green Gen Project
• Apr.16th; 17h; Active Shutdown
• May 9th; 70h; Pulverized Coal Fill Filter LeakageMay 9th; 70h; Pulverized Coal Fill Filter Leakage
• May 27th; 31h; Misoperation
• Jun 9th; 27h; Syngas Pipe Leakage• Jun.9th; 27h; Syngas Pipe Leakage
• Jun.25th; 96h; Misoperation
J l 10th 16h Ai S t U it F lt• Jul.10th; 16h; Air Separator Unit Faults
• Jul.16th; 77h; Muffle Burn Out
• Agu.8th; 22h; Whole Plant Cooling Water Pipe Burst
• Agu.29th; 175h; Active Shutdown
CHNG Green Gen Project
C O
CHNG Green Gen Project
Commissioning and Operation
• Gasification Unit Commissioning Work Finished• Gasification Unit Commissioning Work Finished
• Technological Process Proved
• Two Stage Gasification Experiment Finished• Two Stage Gasification Experiment Finished
• Different Kinds of Coal Tested
• Chinese Equipment and Instrument
• Technology Improvement
GreengenGreengen GasifierGasifierStart TransportationStart Transportation
2929thth S 2010S 2010on 29on 29thth Sep. 2010Sep. 2010
CHNG Green Gen Project
Performance Index (Shenhua bituminous)
CHNG Green Gen Project
Performance Index (Shenhua bituminous)
• Cold Gas Efficiency: 84.1%
• Oxygen consumptions: 303 Nm3/1000Nm3 CO+H2
• Coal consumptions: 580 kg/1000Nm3 CO+H2
• Syngas compositions: CO2<2%
• Steam produced: 150t/h
Key PointKey Point
Effects of The Second Stage Gasification
• The Second stage Coal Input Rate 5~6%• The Second stage Coal Input Rate 5 6%
• Total Carbine Reaction Rate >99%
• Cold Gas Efficiency Improved: 0 5 1%• Cold Gas Efficiency Improved: 0.5~1%
• Coal consumptions deceased: 4~8 kg/1000Nm3 Effective syngas
(CO H2)(CO+H2)
• Oxygen consumptions deceased : 10~20 kg/1000Nm3 Effective
(CO H2)syngas (CO+H2)
• Syngas temperature deceased:100~200 ℃
CHNG Green Gen Project
Next Work
CHNG Green Gen Project
Next Work
• Gas Turbine Commissioning
• Whole Plant 72+24h Operation Acceptance Test
• Operation Optimization
Shili M th l P j tShilin Methanol Project
Shili M th l P j tShilin Methanol Project
Shili M th l P j t
Design Points
Shilin Methanol Project
Design Points
• SGQ ProcessG ifi C it 1000t/d• Gasifier Capacity: 1000t/d;
• Pressure: 4.0 MPa;
• Entrained gas: CO2Entrained gas: CO2
• Effective syngas flow(CO+H2): 71500Nm3/h;
• Cold gas efficiency:82%;
• Effective component(CO+H2) of dry syngas: 91%
• Methanol production: 300,000 t/a;
Shili M th l P j tCommissioning and Operation
Shilin Methanol Project
• Agu.9th; 1h; Misoperation
• Agu.27th; 22h; Pump FaultAgu.27th; 22h; Pump Fault
• Agu.29th; 43h; Instrument Wrong Signal
• Sep 15th; 15h; Misoperation• Sep.15th; 15h; Misoperation
• Sep.20th; 124h; Misoperation
S 28th 624h Still O ti• Sep.28th; 624h; Still Operating
Wh ?Why run so easy?
• Experience in Greengen Project
• System Simple
Shili M th l P j t
Performance Index(Shenhua bituminous)
Shilin Methanol Project
Performance Index(Shenhua bituminous)
• Cold Gas Efficiency: 83%
• Carbine Reaction Rate >99%
• Oxygen consumptions: 313 Nm3/1000Nm3 CO+H2
• Coal consumptions: 551 kg/1000Nm3 CO+H2
• Steam produced: 50t/h
GasifierGasifier Arrives Arrives ShilinShilin Site Site on 20on 20thth Jul. 2010Jul. 2010
Shili M th l P j t
Next Work
Shilin Methanol Project
Next Work
• Operation Optimization
• Gasify lignite
SGC & SGQSGC & SGQ
The Advantage of SGCThe Advantage of SGC
• Total Heat Recovery, Produce More Steam
• Lower Operation Cost
• Lower Water Consumption
The Advantage of SGQ
• Simple System
L I t t• Lower Investment
• Higher Operation Reliability
C l iConclusions
• Realized Long Period Operation in Both Industrialized Units.
• Two Stage Gasification Technology Improved Gasification
Efficiency ,Deceased Coal and Oxygen Consumption.
• One Step Forward comparing with One Stage Gasification.
• SGC Process Low Operation Cost• SGC Process Low Operation Cost
• SGQ Process Low Investment
• Chinese Design, Equipment , Installation in Both Project.
I F tIn Future
• Large scale Gasifier.
• Gasifier adaptability to Coal .
• Technology Improvement
Thank you for your attention !y y
Questions?
Contact: Guangyu Li
Director of GreenGen Department
Huaneng Clean Energy Research InstituteHuaneng Clean Energy Research Institute
Email:liguangyu@hnceri.com
Phone: +8613572296264