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4_004 Potassium Carbonate Carryover

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Potassium Carbonate Carry Over
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19 th AFA Int’l Fertilizer Technical Conference & Exhibition 18- 20 April 2006 Four Seasons Hotel Doha- Qatar Case Study : Potassium carbonate carryover in carbon dioxide gas going to urea plant Mr. Bashar Al-Aradi Yield Consumption Engineer- GPIC Bahrain
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Page 1: 4_004 Potassium Carbonate Carryover

19th AFA Int’l Fertilizer Technical Conference & Exhibition

18- 20 April 2006 Four Seasons Hotel

Doha- Qatar

Case Study : Potassium carbonate carryover in carbon dioxide gas going to urea plant

Mr. Bashar Al-Aradi Yield Consumption Engineer- GPIC

Bahrain

Page 2: 4_004 Potassium Carbonate Carryover

Gulf Petrochemical Industries Company(GPIC)

Kingdom of Bahrain

Overcoming Potassium Carbonate carryover Problem from Benfield Section

(Case Study)

19th AFA International Annual Technical Conference

Prepared By:

1. Mr. Khalid Al-Bin Ali/ Senior Process Engineer 2. Mr. Bashar Al-Aradi/ Yield & Consumption Engineer

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GPIC 1 of 23

CONTENT PAGE ABSTRACT 2

1.0 Introduction 4

2.0 CO2 Removal System Performance in different periods

2.1 Prior 1989 Debottlenecking 5

2.2 Post 1989 Debottlenecking 6

2.3 Post commissioning of Urea Plant 7

3.0 Where was the problem then? 8

4.0 Proposals to minimize potassium carbonate carryover:

4.1 Installation of high efficiency demister in the knock-out 10 drum (D-8101) and washing CO2 gas with demin water. 4.2 Installation of a steam heater at the suction of the CO2 11 Compressor (K-8101) and hot gas recycle through K-8101. 4.3 Installation of three typical Thormann trays. 12

4.4 Installation of Direct Cooling Contact. 13

4.5 Installation of a new modified Thormann Tray in CO2 15 Desorber (C-0502). 5.0 Conclusion. 17

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ABSTRACT

In the Ammonia process, Carbon Dioxide (CO2) gas is generated as a by-

product and removed by absorption in a Potassium Carbonate solution in

the Benfield Absorption Column. The Potassium Carbonate solution is

regenerated in the Benfield Desorber where the CO2 gas is removed and

vented.

Prior to the commissioning of the GPIC Urea plant in 1998, part of CO2 gas

from the Ammonia process was used in the Methanol plant to increase

production. After commissioning Urea plant, all the CO2 gas is consumed in

the production of Urea.

At the end of 1998, increased Potassium Carbonate carryover in the CO2

gas to the Urea plant was experienced. This resulted in the deposition of

solid Potassium Carbonate on the internals of the Urea plant CO2

compressor, especially on the impellers. These deposits caused an increase

in vibration in the compressor resulting in the Urea plant being shut down

to wash the compressor internals with water. The deposits were observed

to be severe in the low pressure (LP) casing (first and second stages) with

fewer deposits found in the third and fourth stages of the high-pressure

(HP) casing.

This paper highlights the causes of the problem and discusses a number of

suggested remedial solutions considered to minimize the carryover problem

as summarized below:

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1. Replacement of the first separator demister in the CO2 Compressor.

2. Washing CO2 gas with demin water.

3. Installation of steam heaters on the compressor suction.

4. Hot gas recycle in the CO2 compressor.

5. Installation of three Thormann trays.

6. Installation of Direct Contact Cooling System.

7. Installation of new modified washing tray (Thormann tray) in the

Benfield Desorber.

Some of the proposals were implemented, some were rejected. The

reasons for implementation and rejection will be discussed in this paper.

Subsequent to the implementation of some of the above proposals, a

significant reduction with respect to Potassium Carbonate carryover was

noticed with minimum deposits in the CO2 compressor. The proposal that

contributed most substantially to solve the carryover problem was the

installation of the new modified Thormann tray in the Benfield Desorber.

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1.0 Introduction

Gulf Petrochemical Industries Company (GPIC) was formed in 1979 as an

equal partnership between the government of Bahrain, the government of

Saudi Arabia representative by (SABIC) and the government of Kuwait

representative by (PIC) with the objective of utilizing Bahrain’s natural gas

resources for the production of petrochemicals.

GPIC’s first project was a grassroots petrochemical complex at Sitra Island

on the North East coast of Bahrain. A site of 60 hectares was successfully

reclaimed from the sea to construct the Ammonia and Methanol plants,

along with related Utilities and offsite facilities. The original plant capacity

was 1000 MPTD of each product. In 1989 the Ammonia and Methanol

plants were debottlenecked to increase production to 1200 MTPD of each

product.

Part of the debottlenecking of the Methanol plant involved the diversion of

CO2 gas generated in the Ammonia process. The CO2 pressure was boosted

by a reciprocating compressor (K-1403) prior to entering the Methanol

synthesis loop.

In January 1998, GPIC commissioned a 1700 MTPD granular Urea plant

downstream of the Ammonia plant. All the CO2 gas vented from the

Ammonia process was channeled to Urea plant and none was available for

the production of Methanol.

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2.0 CO2 Removal System Performance in different periods

2.1 Prior 1989 Debottlenecking

Prior to 1989 debottleneck project, small quantity of CO2 gas from

Ammonia process, Benfield section, was channeled to the Methanol plant

(See figure #1). The pressure of the CO2 gas stream was boosted by a

reciprocating CO2 compressor (K-1403). The addition of CO2 gas boosted

Methanol production without any trouble and resulted in very steady

operation of the Methanol synthesis loop. However, a decision was taken

by GPIC management to increase the capacity of Ammonia Plant as well as

for Methanol Plant. After the debottleneck project, all units in both

Ammonia and Methanol Plants handled 20% higher load to achieve the

targeted output 1200 MTPD for each product.

In an assessment study prior to the debottlenecking project, the feasibility

of high load was investigated. Equipments were provided in parallel where

necessary, to cater for the 20% increases in flow rate demanded by the

debottlenecked conditions.

During this investigation the Benfield units were studied to check the

adequacy of both the CO2 Absorber (C-0501) and CO2 Desorber (C-0502)

to handle the additional flow rates.

The study revealed that both units would operate close to transition or

borderline conditions due to increase in gas velocities inside the columns. It

was also noted that minor Potassium Carbonate carryover with the CO2 gas

Page 8: 4_004 Potassium Carbonate Carryover

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may occur under these conditions. The magnitude of this carryover, in view

of the borderline operating conditions, was not determined.

Moreover, there was no concern for the potential adverse effects on the

positive displacement compressor (K-1403) as it was well known that this

type of machine is less sensitive to minor deposits of solids, compared to

high-speed centrifugal compressors.

2.2 Post 1989 Debottlenecking

Subsequent to the debottlenecking the target production of 1200 MTPD of

both Ammonia and Methanol was achieved and all units, including the

Benfield section and the CO2 reciprocating compressor, ran steadily and

reliably.

It was noticed during routine maintenance of the CO2 compressor (K-1403)

that some Potassium Carbonate had deposited in the compressor inlet

chambers and around the pistons. It was assumed that this was the result

of operating at borderline conditions in the Benfield section. As this did not

cause any limitation in the operation of the compressor (K-1403), it was

disregarded.

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2.3 Post commissioning of Urea Plant

Urea Plant commissioned in January 1998. The incoming CO2 gas from

Ammonia Plant is cooled in a CO2 Cooler exchanger (E-8101) and any

condensate is removed in the knock-out drum (D-8101). The CO2 gas is

then compressed in a four-stage centrifugal compressor (K-8101). After

that, the CO2 gas goes to the Urea reactor where it is reacted with

Ammonia to form Urea Carbamate.

After Urea plant commissioning, the requirement for CO2 gas rose to a level

which demanded nearly all the CO2 gas stripped from the Potassium

Carbonate solution in the Benfield section. This led to a decision to divert

all the stripped CO2 gas from the Benfield Desorber directly to the Urea

plant. Thus no CO2 gas was fed to the Methanol plant any longer and the

CO2 compressor (K1403) was taken out of service (See figure 2).

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3.0 Where was the problem then?

After several months of operation following the initial start-up, the CO2

compressor (K-8101) started showing abnormal vibrations and high

displacement levels. The plant was taken off line and the compressor

inspected internally.

Very heavy deposits of Potassium Carbonate were found in the first and

second stages of the compressor, with smaller deposits in the third and

fourth stages. It was obvious that for high-speed centrifugal compressors

the carryover and deposition of solid material on impellers is critically

detrimental, leading to vibration levels that could affect the safety and

integrity of the machine. It also resulted in serious production loss as the

only remedy was to take the plant off line and clean the compressor.

This issue became crucial to the reliable and economic operation of the

Urea plant. A task force was formed to explore various options and to

evaluate the feasibility of implementing the solutions proposed prior to the

complex turnaround in September 2000.

The following remedial solutions were considered to minimize the carryover

problem:

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1. Replacement of the first separator demister in the CO2

Compressor.

2. Washing CO2 gas with demin water.

3. Installation of steam heaters on the compressor suction.

4. Hot gas recycles in the CO2 compressor.

5. Installation of three typical Thormann trays.

6. Installation of Direct Contact Cooling System.

7. Installation of new modified washing tray (Thormann tray) in the

Benfield Desorber.

Some of the above proposals were implemented, some were rejected. The

reasons for implementation and rejection are discussed below.

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4.0 Proposals to minimize potassium carbonate carryover

4.1 Replacement of the first separator demister with high

efficiency demister in the knock-out drum (D-8101) and Washing

CO2 gas with demin water

The proposal was to wash out the entrained potassium carbonate by

installing a demineralized water sparger upstream the CO2 Cooler

exchanger (E-8101) and then separate the condensate in CO2 Knock out

drum (D-8101) using high efficiency demister(See figure#3).

4.1.1 Expected Benefits:

The expected benefits were:

1. Dissolving potassium carbonate in demin water.

2. Improving the separation efficiency in CO2 Knock out drum.

The existing demister type (York 421) had been designed to remove 99.9%

of particles up to 10 micron in size, while the new demister type (York 709)

was designed to remove 96.4% of particles up to 5 micron in size and

62.6% of particles up to 3 micron in size.

4.1.2 Post-Implementation Results

The new demister was installed in June 2000 while the demineralised water

sparger was commissioned during July 2000. The combined effect was a

marginal improvement. The Urea plant could be run for approximately 3

months continuously, compared to 2 months prior to the modification.

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4.2 Installation of a steam heater at the suction of the CO2

compressor (K-8101) and hot gas recycle through K-81O1

It was proposed to install steam heaters in the first and second stage

suction lines of the CO2 compressor (K-8101) to heat the CO2 gas stream,

which is 100% saturated with water, through the compressor (See figure#

4).

4.2.1 Expected Benefits

By using steam as indirect heating medium for the above exchanger, the

temperature of CO2 gas would be raised by 1 or 2 °C above saturation

temperature, hence maintaining superheated conditions and preventing

condensation inside the compressor.

This proposal was discarded as the risk of steam entering the CO2 gas

stream in the case of any severe leakage took place. As an alternative to

steam heating, it was proposed to recycle hot CO2 gas from the second

stage discharge to the first and second stage suction lines, effectively

achieving the same temperature increase of 1 to 2 °C (See figure# 5).

4.2.2 Post-Implementation Results

This proposal was implemented during 2000 Turnaround. Subsequent to

plant start-up, the temperature increase of about 2°C in the suction of both

the first and second stages was achieved, which contributed to the

reduction of Potassium Carbonate deposition to some extent.

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4.3 Installation of three typical Thormann trays:

It was proposed to install three bubble cap trays in series at the top section

of CO2 desorber.

4.3.1 Expected Benefits:

By increasing the number of bubble cap trays from one to three, the

contact between the two phases will increase i.e. CO2 gas washing contact

will increase and hence the potassium carbonate will decrease due to

sufficient washing.

4.3.2 Analysis:

The proposal was rejected based on the following facts:

1. The vertical space in the desorber is not sufficient.

2. Involve a major modification such as cutting and welding of the

column, which would require long period of shutdown.

3. The additional height will increase the load on the structure whose

design should be reviewed and modified.

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4.4 Installation of Direct Cooling Contact:

Its purpose is to scrub K2CO3 with process condensate and fresh make-up demin water in a packed tower to get clean CO2 gas. It will also cool the gas from 85 oC to 40 oC (See figure# 6). The CO2 gas exit of the scrubbing column will follow the normal path going to CO2 compressor of Urea Plant via existing CO2 cooler (E-8101) and separator (D-8101). The condensate from the bottom of the tower is cooled in an indirect cooler exchanging heat with sea water and fed back to scrubber as a scrubbing media. About 20 m3/hr of condensate will be sent to the stripping unit of Utility section for further polishing and recycling. The stripping unit in Utilities Section is adequate to handle the additional 20m3/hr of condensate. However, the liquid inlet distributors to the stripping column will have to be replaced as they will reach their capacity limits. One of the major concerns of this project would be the provision of about 1000 m3/hr of sea cooling water which can not be met during summer months with 5 sea water pumps running. If the 6th sea water pump is also operated then it would mean no stand-by pump will be available which is not acceptable. Hence to meet this additional sea water requirement, a 7th spare pump will have to be installed.

4.4.1 Expected benefits:

1. Eliminate K2CO3 carryover to CO2 Compressor and hence prevent

Urea Shutdowns.

2. Cooling the CO2 gas to around 40oC as against design temperature

of 50oC.

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4.4.2 Analysis:

Based on the above facts, the payback period was worked out assuming the worst operating scenario of frequent Urea Plant shutdowns and low load operation due to excessive carryover of K2CO3 in CO2 gas. During year 2000, total of 25,402 MT of Urea product was lost due to K2CO3 carryover problem, at the rate of 1700 MTPD Urea production. This is equivalent to 15 days production loss. Based on the above 15 days production loss per year, and the high budgetary cost of the project, the payback for the project worked out to be 5.7 years. The proposal was not attractive from economic point of view; therefore, it was frozen until considering the last proposal of installing new modified Thormann tray in CO2 desorber and evaluating its results.

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4.5 Installation of a new modified Thormann Tray in CO2 Desorber

(C-0502)

This proposal addressed the root cause of the problem by considering an

improved design of the Thormann bubble cap tray utilized for washing the

CO2 gas stream leaving the Benfield Desorber (C-0502).

4.5.1 Expected Benefits

The elimination, or at least minimization, of the Potassium Carbonate

carryover from the Benfield Desorber (C-0502) by the reduction of the

velocity of the desorbed CO2 gas through the bubble caps of the Thormann

tray.

The following comparison table shows the difference between the old

bubble cap and the new one:

Description Original Tray New Modified Tray

Active area (m2) 10.07 12.04

Number of bubble caps 155 250

Downcomer shape Envelope Pipe

Jet Flood Percentage 101.25 85

Material of Construction SS 304 SS 410

Pressure drop (mmHg) 5.86 3.57

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4.5.2 Post-Implementation Results

This modification was implemented during Turnaround 2000 and since then

a noticeable reduction in the carryover of Potassium Carbonate has been

observed. No forced shutdown due to deposits of Potassium Carbonate in

the CO2 compressor has been experienced since that time. It is worth

mentioning in addition, that when the Benfield Desorber (C-0502) was

opened to replace the old Thormann tray, the tray was found slightly loose

with some sections displaced. This could very well have been the result of

operating the column at borderline conditions before. It also justifies the

replacement of this tray with a similar one of higher capacity. This

replacement has finally cured the Potassium Carbonate carryover problem.

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5.0 Conclusion

Of the various proposals to overcome the problem of Potassium Carbonate

carry-over from the Ammonia plant’s Benfield Desorber (C-0502) which

was affecting the operational stability of the CO2 compressor in the Urea

plant, the replacement of the Thormann Tray with one of improved design

and higher capacity proved successful in solving the root cause of the

problem. In addition, all the other modifications resulting from the other

proposals benefited the situation marginally.

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Figure #1: Benfield flow diagram before de-bottlenecking project

Air Coolers

F-0503Separator

C-0502Desorber

F-0506Separator

E-0507CO2 Cooler

F-0505Separator

K-1403CO2 compressor for

Methanol Plant

Lean Solution outlet

CO2 Rich Solution inlet

CO2 Gas

Demister

Thormann Tray

E-0504Deionat

Preheater

Page 21: 4_004 Potassium Carbonate Carryover

GPIC 19 of 23

Figure #2: Benfield flow diagram after commissioning of Urea Plant

Air Coolers

F-0503Separator C-0502

Desorber

F-0506Separator

E-0507CO2 Cooler

F-0505Separator

K-1403CO2 compressor for

Methanol Plant

Lean Solution outlet

CO2 Rich Solution inlet

CO2 Gas

Demister

Thormann Tray

E-0504Deionat

Preheater

K-8101CO2 compressor in Urea

PlantD-8101

Knock Out Drum

E-8101CO2 Cooler

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Figure #3: Proposal of installing a modified demister and a water sparger.

D-8101Knock Out Drum

E-0507CO2 Cooler

K-8101CO2 compressor in Urea

Plant

E-8101CO2 Cooler

Installation of water sparger

Replacing the Demister with Improved type

Page 23: 4_004 Potassium Carbonate Carryover

GPIC 21 of 23

Figure #4: Proposal to install Steam Heaters

1st2nd

3rd4th

K- 8101

CO2 GAS IN

CO2 GAS IN

Proposed Steam

Heaters

Page 24: 4_004 Potassium Carbonate Carryover

GPIC 22 of 23

Figure #5: Proposal to recycle hot CO2 gas

1st2nd

3rd4th

K- 8101

CO2 GAS IN

CO2 GAS IN

Proposed routing

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Figure #6: Proposal of Direct Cooling Contact

Demin Water

CO2 Gas Inlet

CO2 Gas outlet

Sea Water


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