+ All Categories
Home > Documents > Case studies of air cooled vacuum steam condensers...

Case studies of air cooled vacuum steam condensers...

Date post: 27-Mar-2018
Category:
Upload: hoangdiep
View: 236 times
Download: 8 times
Share this document with a friend
30
Case studies of air cooled vacuum steam condensers performance improvements 2013 ACCUG Meeting October 14-17, 2013
Transcript
Page 1: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Case studies of air cooled vacuum steam condensers performance improvements

2013 ACCUG Meeting October 14-17, 2013

Page 2: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

CASE 1 - ACC CLEANING SYSTEM & FAN

OPTIMISATION

Page 3: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Situation ACC until 2010 • Cleaning of ACC until 2010 was max. 2 times/year • Simply cleaning in a fixed period without looking at loss of performance

Reduction in production of steam due to poor condensation

Revenue losses through loss in electricity production

Temperature up to 25oC

Percentage reduction in steam compared to maximum design temperature at 25oC

Reduction of steam compared to maximum steam flow at 25oC

Reduction in waste incinerated with steam flow at 25oC

25 to 28oC

Up to 6.23% Up to 2.65 kg/s Up to 3.24 t/h

29 to 32oC

Up to 14.54% Up to 6.18 kg/s Up to 7.67 t/h

33 to 36oC

Up to 22.86% Up to 9.70 kg/s Up to 12.02 t/h

Page 4: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

30 days temperatures over 25 °C approx. 10 h/day

300 h x ca. 5t/h loss of waste throughput

=

1500 Tons less throughput

+

5kg/s steam = approx. 5MW * 300h

=

1500 MWh less electricity throughput per year

Example of calculations for loss of revenue (minimum case)

Page 5: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Evaluation 2010

Page 6: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

• 1. Cleaning after winter • 2. Cleaning after middle pollen phase • 3. Cleaning after end of pollen phase • 4. + 5. Cleaning in summer • 6. Cleaning in Automn • 7. Cleaning before winter

Situation in 2011

Page 7: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Evaluation 2011

Page 8: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Comparison between 2010 & 2011

Page 9: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Mission • Faster cleaning • Improved efficiency of fan system

more condensation capacity

Challenges for 2012

Page 10: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

10

Optimization Winter 2011-2012 Original cleaning system • Flexible hoses with check valves • HP unit working pressure = 110 bar • Number of nozzles for cleaning head = 12 • Incorrect position of nozzles versus bundle and nozzle orientation • No option to rinse plenum chamber (after cleaning) and bottom rows bundle

Page 11: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

11

Optimization Winter 2011-2012 Improved cleaning system • Removed check valves and installed ball valves • New high capacity HP unit working pressure incl. Soft-start = 120 bar • Number of nozzles for cleaning head = 24 • Correct position of nozzles versus bundle and nozzle orientation • Tube union Tee for HP gun (rinsing off dirt inside plenum and lower rows of bundle)

Page 12: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

12

Optimization Winter 2011-2012

Page 13: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

13

Optimization Winter 2011-2012

Page 14: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

14

Improvement made by modification cleaning machine

• Before it took 7 hours to clean 1 side (2 fans) and with new optimized system is took only 3 hours for 1 side • Only 1 passage for cleaning head now versus 2 passages before

due to higher pressure and better positioning & orientation of the nozzles

• Cleaning head approx. 2 times wider then original cleaning head

• Better cleaning result per cleaning • 4 cleaning sessions per year (versus 7 in 2011) due to

improved cleaning results

Page 15: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

15

Optimization Winter 2011-2012 Original fan system • Margin over on motors • Fairly low pressure capacity of existing fans as soon as ΔP increases due to wind

or external fouling, fans was starting to cavitate/stall

New Situation fan system • Increase by 15% in fan RPM by increasing frequency of VSD’s from 50 Hz to 57.5 Hz. • Decrease in pitch angle from 19.1o to 14.0o • Improved airflow of minimum 8-10% versus original situation • Improved pressure capacity of fan to cope with wind and especially external fouling

Page 16: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

16

Evaluation 2012

15

20

25

30

35

40

45

50

55

-15 -10 -5 0 5 10 15 20 25 30 35 40

Fris

chda

mpf

men

ge in

kg/

s

Außentemperatur °C

LUKO-Auswertung MHKW 2012

2012

Page 17: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

17

Comparison between 2011 & 2012

15

20

25

30

35

40

45

50

55

-15 -10 -5 0 5 10 15 20 25 30 35

Fris

chda

mpf

men

ge

Außentemperatur

LUKO-Auswertung MHKW 2011 zu 2012

20122011

Page 18: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

18

Evaluation 2010 / 2011 / 2012

15

20

25

30

35

40

45

50

55

-15 -10 -5 0 5 10 15 20 25 30 35

Fris

chda

mpf

men

ge

Außentemperatur

LUKO-Auswertung MHKW 2010 zu 2011 und 2012

201120122010

Page 19: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

19

Evaluation 2010 / 2011 / 2012 (Back pressure)

Abdampfdruck Trend - Gleitender Durchschnitt

0

0,02

0,04

0,06

0,08

0,1

0,12

0,14

0,16

0,18

0,2

201020112012

Page 20: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

20

Consequence of improvement

Page 21: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

CASE 2 – INSTALLATION OF VARIABLE SPEED DRIVES

Existing situation No variable speed drives No room for VSD in sub-station (MCC) Pitch angle : 19o

Fan tip speed : 30.9 m/s Motor power : 162 amps Temperature range : -20oC + 30oC Average measured data Airflow: 534 m3/s Static pressure: 55 Pa Amperage : 136 Amps

Traditional Solutions New fan with more blades or wider blades AND / OR New higher rating motor AND / OR Increased heat transfer surface

Page 22: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

ELFLOW BV solution

• Increased tip speed of fan by 20% (50 to 60 Hz)

• Decreased pitch angle from 19o to 16o

• Fully loaded motor to 158 Amps

Page 23: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

ELFLOW BV SOLUTION ADVANTAGES New IP20 VSD with IP66 casing inside each cell instead of in sub station Savings • No new sub-station • No new fans, motors or bundles • No costly DU/DT filter (close to motor) • No costly Sinus filter (close to motor) • No extra cooling as fan is cooling VSD • No cabling from sub-station to motor (if VSD is installed in sub station)

Page 24: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

ELFLOW BV SOLUTION ADVANTAGES Advantages No need anymore for extra capacity on motor Fans will turn slower

in winter as cooling is not an issue at -20oC!!!!!!! This power can be utilized to increase airflow during summer operation

Lower noise level during night/cooler period (when it is cooler and when noise limitations are stricter)

Decreased total power consumption required by ACC during a year as regulation is optimized by VSD

Strongly reduced load on fan blades, gearboxes and motor when running at lower RPM

No wind-milling (fans will only run slower) Reduced maintenance costs of gearbox and fans (no start-stop) Ability to increase fan RPM by approx. 20% (50 to 60 Hz or 60 to 70 Hz)

and therefore efficiency and pressure capacity Increased pressure capacity of fan by approx. 40% Increased static efficiency of fans by 6% Increased airflow of fans by 14% versus original situation

Page 25: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers
Page 26: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

CASE 3 – ADIABATIC COOLING FOR ACC IMPROVEMENT

Page 27: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Adiabatic cooling

50 mbar

45 mbar

35 mbar

25 mbar

Typical ACC performance curve (Alstom turbine) illustrating improvement in vacuum with increments of 5*C in air temperature (at same steam flow rate)

20 mbar

Page 28: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Price of electricity varies with air temp.

Page 29: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Reduce ambiant air temperature Proper chilling system depends on …..

Droplet size

Distance between fog and finned tube

bundle/mechanics

25 °C

Face velocity

Climate conditions

Page 30: Case studies of air cooled vacuum steam condensers ...acc-usersgroup.org/.../10/...of-air-cooled-vacuum-steam-condensers.pdf · Case studies of air cooled vacuum steam condensers

Possible Reduction in ambiant air temperatures using COOLINGMIST™ system

0

5

10

15

20

25

30

12:5

9:58

13:0

3:28

13:0

6:58

13:1

0:28

13:1

3:58

13:1

7:28

13:2

0:58

13:2

4:28

13:2

7:58

13:3

1:28

13:3

4:58

13:3

8:28

13:4

1:58

13:4

5:28

13:4

8:58

13:5

2:28

13:5

5:58

13:5

9:28

Temp MGR015

Temp MGR016

Temp MGR017

Temp MGR018

Temp MGR019

0

20

40

60

80

100

120

12:5

9:58

13:0

3:28

13:0

6:58

13:1

0:28

13:1

3:58

13:1

7:28

13:2

0:58

13:2

4:28

13:2

7:58

13:3

1:28

13:3

4:58

13:3

8:28

13:4

1:58

13:4

5:28

13:4

8:58

13:5

2:28

13:5

5:58

13:5

9:28

RH MGR019

RH MGR018

RH MGR017

RH MGR016

RH MGR015


Recommended