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Copyright 2000 SIEP B.V. Shell Canada E&P Conversion of Sulfinol-D to MDEA at the Shell Canada Burnt Timber Facility Jamie Grant Operations Engineer April 27, 2007 GPAC O&M Conference
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Copyright 2000

SIEP B.V.

Shell Canada E&P

Conversion of Sulfinol-D to MDEA

at the Shell Canada Burnt Timber

Facility

Jamie Grant

Operations Engineer

April 27, 2007

GPAC O&M Conference

Copyright 2001

SIEP B.V.

Shell Canada E&P

Introduction

� Shell Canada’s Burnt Timber Facility is located 120 km northwest of Calgary, Alberta

� Plant 1 – constructed in 1970

� Capacity of 1830 e3m3/d (65 MMSCFD)

� Plant 2 – constructed in 1976

� Capacity of 2000 e3m3/d (71 MMSCFD)

Copyright 2001 SIEP B.V.

Shell C

ana

da E

&P

Copyright 2001

SIEP B.V.

Shell Canada E&P

Current Plant Configuration

PLANT 1

GAS TREATING

PLANT 2

GAS TREATING

PLANT 2

DEHYDRATION

PLANT 1

SRU

INCINERATION

PLANT 1

DEHYDRATION

COMMON FACILITIES

SW STRIPPER AND CONDENSATE STABILIZATION

PLANT 1

INLET SEPARATION

PLANT 2

INLET SEPARATION

PLANT 2

SRU

RAW GAS FROM FIELD

Copyright 2001

SIEP B.V.

Shell Canada E&P

29

Original Gas Treating Configuration

Copyright 2001

SIEP B.V.

Shell Canada E&P

Reasons for Change

� Hydrocarbon Content in Acid Gas

� Consumption of air

� Produced large amounts of CS2

� Un-combusted BTX caused deactivation of 1st

converter bed

� This resulted in 1st bed catalyst being changed every 6 to 9 months.

� Excessive operating costs

� Lost Production

Copyright 2001

SIEP B.V.

Shell Canada E&P

Reasons for Change

� High CO2 Content in Acid Gas

� Increases pressure drop therefore reducing blower capacity and plant capacity

� Production of COS reducing sulphur recovery

� Reduces reaction furnace flame temperature

Copyright 2001

SIEP B.V.

Shell Canada E&P

Component

(mole %)

Year

2005 2020

H2S 10.1 8.1

CO2 8.0 10.2

N2 0.6 0.5

C1 75.8 80.4

C2 2.1 0.8

C3 0.4 0.2

i-C4 0.1 0.0

n-C4 0.1 0.0

i-C5 0.1 0.0

n-C5 0.1 0.0

C6 0.3 0.1

C7+ 3.3 1.2

Reasons for Change

� Change in feed gas composition

� Burnt Timber Field: H2S = 10.2% CO2 = 6.4%

� Panther Field: H2S = 7% CO2 = 11.5%

Copyright 2001

SIEP B.V.

Shell Canada E&P

Reasons for Change

� Changing Feed Composition would result in:

� Poor Acid Gas H2S:CO2 ratio

� Higher acid gas HC content due to higher amine circulation ratios

� End Result = Lower Plant capacity and lower sulphur recovery

Copyright 2001

SIEP B.V.

Shell Canada E&P

Benefits of Conversion to MDEA

� Slip CO2 to sales improving acid gas H2S:CO2 ratio.

� Decrease HC co-absorption in the amine.

� Decrease air requirements in SRU and increase capacity.

� Increase heating value to sales gas.

� Reduce flash gas volume.

� Circulation rate not impacted by H2S:CO2 ratio.

� Lower reboiler duty

Copyright 2001

SIEP B.V.

Shell Canada E&P

Risks of Conversion to MDEA

� Reduced removal of trace sulphurs

� Depending on raw gas trace sulphur content, may not be able to meet specification.

� Aqueous MDEA has a higher foaming tendency than Sulfinol which may lead to capacity constraints

� Decision was made to change amine to MDEA.

� Millenia Resource Consulting of Calgary was contracted to do the detailed Engineering design.

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

MDEA Conversion Modifications

Absorber Design

� Slip up to 4% CO2 and less than 8 ppmv H2S

� 2% CO2 required when Plant 1 is shutdown

CO2 Concentration Profile - Year 2020

1

3

5

7

9

11

13

15

17

19

21

2.0 3.0 4.0 5.0 6.0 7.0 8.0 9.0 10.0 11.0

CO2 Concentration (%)

Tra

y N

um

be

r

14 trays

16 trays

18 trays

22 trays

MDEA = 40C and

0.0028 mol/mol

loading.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Absorber Design

H2S vs Number of trays

0

2

4

6

8

10

12

12 14 16 18 20 22 24

Number of trays

H2

S i

n T

rea

ted

Ga

s

(pp

mv

)

Year 2005

Year 2020

MDEA = 40C and

0.0028 mol/mol

loading.

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

16

14

12

Absorber Design

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

Flash Drum Design

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

Lean Rich Exchangers

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

Regenerator

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

Carbon Filter

Copyright 2001

SIEP B.V.

Shell Canada E&P

22

18

16

14

Inlet Filter Coalescer & Preheater

Copyright 2001

SIEP B.V.

Shell Canada E&P

Construction

� Construction was one of the most challenging aspects of the project

� Equipment located on three skids

� Gas/Gas Exchanger and Coalescer Skid

� L/R Exchanger Skid

� Flash Tank Skid

� Issues with the skids – late and unfinished.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Construction

� Major work during shutdown was in the Absorber

� Installation of three feed nozzles

� Installation/modification of tray rings

� Strip lining the bottom 10 m

� Lining the nozzles with stainless steel

� Absorber had to have a hydrogen bake out, continuous weld preheat, and stress relieving.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� First task was to clean the system

� Absorber and regenerator were vacuumed.

� Start-up suction strainers installed.

� Vessels and piping were air freed and gross leak tested using N2.

� Final leak check at operating pressure with fuel gas.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� Cleaning the system cont’d

� System was charged with steam condensate.

� Circulation was established with L/R exchangers by-passed.

� Steam condensate temperature was raised to 60 deg C.

� A degreasing solution was added (1% soda ash, 1% tri-sodium phosphate and 0.2% surfactant).

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� Cleaning the system cont’d

� The system was completely drained and then refilled with fresh steam condensate.

� Circulation was then established for 3 hours or 3 full circulations.

� The system was drained then charged with 50:50 MDEA/Water mixture.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� Start-up

� Gas was introduced with no unexpected issues.

� When L/R exchangers were placed in series, the Booster Pumps experienced cavitation.

� The pumps were damaged and 3 day outage was necessary due to delivery of replacement parts.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� Start-up….Next Problem

� Plugged Absorber Level Control Valve.

� Valve was plugged with welding slag, bolts, and other debris.

� This occurred three more times with the same result.

� Installed a bypass LCV with different style trim.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Commissioning, Start-up and Operation

� Start-up

� Hang-ups were experienced in the regenerator due to excessive steaming

� Placing L/R exchangers in series on the rich side solved this issue.

� The L/R exchangers did experience some plugging.

� They were cleaned several times online.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Optimization and Current Operation

H2S and CO2 in Treated Gas versus Tray Location

0.00

0.50

1.00

1.50

2.00

2.50

3.00

3.50

4.00

4.50

Tray 22 Tray 14

Tray Location

H2

S (

pp

mv)

an

d C

O2

(%

) in

Tre

ate

d G

as

Sales CO2

Sales H2S

Copyright 2001

SIEP B.V.

Shell Canada E&P

Key Process Performance Results

� Inlet Raw Gas

� Design = 1850 e3m3/d

� Performance Test = max. 2050 e3m3/d

� Reboiler Steam demand

� 25% less steam per volume of raw gas

� Flash Gases

� Reduced from 30 to 2-4 e3m3/d

Copyright 2001

SIEP B.V.

Shell Canada E&P

Key Process Performance Results

� Sulphur Plant Operation

<1% (CH4 eq.)2.5% (CH4 eq.)Acid Gas HC Content

50 & 16 ppmv130 & 200 ppmvCOS & CS2 from Stack

0.23%1.25%CS2 to 1st Converter

100 ppmv600 ppmvTRS (Total Reduced S)

96.9%95%Sulphur Recovery

400 – 500 ppmv> 2300 ppmvBTX in Acid Gas

Up to 70% H2S58%Acid Gas H2S

MDEASulfinolParameter

Copyright 2001

SIEP B.V.

Shell Canada E&P

Key Process Performance Results

� Trace Sulphur Removal

80%85%112 mg S/m3Sulfinol

26%

28%

COS

Total Sulphur in Sales = 59 mg S/m3 (spec = 115)

47%112 mg S/m3MDEA

37%117 mg S/m3Design (MDEA)

RSH

% RemovalInlet Gas

Copyright 2001

SIEP B.V.

Shell Canada E&P

Key Process Performance Results

� Trace Sulphur Removal

� Subsequent tests showed only 8% and 15% removal of COS and RSH with the inlet containing 199 mg S/m3.

� Combined Sales contained = 141 mg S/m3

� Inlet Trace Sulphur was high due to sulphur washes on a sulphur producing well.

Copyright 2001

SIEP B.V.

Shell Canada E&P

Summary

� Conversion to MDEA was a success at Burnt Timber.

� System operates well with little foaming.

� Inlet coalescer and carbon bed.

� MDEA was the correct solution to the problem at Brunt Timber.


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