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  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    1/19

    CE Engineerings and Chemicals Pvt

    Ltd

    SIA ACTIVITY

    Dec13

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    2/19

    SIA Monthly Review PPT

    Signed Hoshin KanriCo-operation Team Supplier Improvement Activity Plan in ACE Engineering

    Quality Goal VECV Team Supplier Team

    # To reduce ppm level to 150 PPM by

    2014 end

    Facilitator Mr Tomochi Katsumata MD & CEO Mr. Pradeep Jain

    Leader Mr Vinayak Shanbagh Head-Manuf. Mr. Manoj Ohja

    #

    Zero defect at customer end

    Co-ordinator Mr Yogesh Jagtap Head-Design Mr. Ramkaran Meena

    Materials Mr Jeetendra Joshi RQC Mr. Mayur Ajmera#

    Continual improvement in process

    through Poka-Yoke & Kaizens

    QA Ms. Neha Jain In process Quality Mr. Mayur Ajmera

    PDD Mr. Amarjeet singh PDI Mr. Mayur Ajmera

    Supplier up-gradation Mr. Vinay Singh Tool Room Mr. Rajesh Dixit

    Main

    Issu

    e

    Controlled KPI -Ace Engg.

    Activity

    Watched KPI - Ace Engg. Responsible &

    Supporting DepartmentObje

    ctive

    Name

    KPI

    Item

    s

    2009

    (Base)

    201

    2

    Tgt. Tgt.

    Respons

    ibleKPI Items

    Base

    (2012

    Q4)

    Target 2013

    Respo

    nsible2013 2014 Q1 Q2 Q3 Q4 ProdDesig

    n

    Tool

    room

    QCpurch

    ase

    Delivery

    Qual

    ity

    PPM

    wise

    PPM

    Impr

    ove

    ment

    Delivery

    PPM

    impr

    ove

    ment

    11575 350 200 150 CFT

    Start

    QRQCIn-house monthly PDI PPM 3747 3000 2500 200 1500

    CalibrationIn-house monthly Process

    PPM4000 3800 3500 3200 3000

    MSA In-coming monthly PPM 1950 1800 1700 1600 1500

    5SNo of DOL parts

    (Total 68 parts)61 62 63 65 66

    ProcessAudit

    PDI Execution (% of PDI

    followed invoices/Totalinvoices raised)

    100 100 100 100 100

    Poka Yoke Process audit (No of parts ) 8 3 3 3 3

    Layout inspection (No. of

    parts)10221 29 19 18

    IMTE and Gauge Calibration - - - 8

    Tooling validation (Dies, Jigs

    & Fixture validation &

    Maintenance)

    10 0 5 5 5

    Poka Yoke 12 3 5 6 6 QS Sign off _ _ 40 28

    System audit score 81% 95%

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    3/19

    SIA Monthly Review PPT

    ACE ENGINEERINGS & CHEMICALS PVT.LTD.

    Monthly Internal Hoshin Kanri Review MOM with top management

    S.

    No

    .

    Date Location Issue Analysis Action Target Dt. Complet

    ion Dt

    Resp. GY

    R

    stat

    us

    1 5/12/13 VECV

    Cover plate

    assy

    rejection

    Due to improper adhesiveness of

    insert on pp part cover plate assy.

    Insert comes out; the adhesive

    used acra-bond shows poor

    compatibility with the partmaterial.

    Adhesive My-T Bond grade

    103 is used & tested as per

    pull out test.

    7/12/13 7/12/13

    2 12/12/13 VECV

    GSC IA303087- C.C

    Dimension is

    out by 9-10-

    mm due to

    which fitment

    issue

    occurred.

    Rejected mould were used byproduction dept, only 2 mould were

    OK and rest were rejected due to

    which ok & not ok parts were found at

    VECV as well as FG Stock. Drilling

    done by seeing marking which is very

    light due to which c.c varies is also the

    source of variation.

    Each part checked at

    FG,filing,painting,moulding,re

    worked with providion of

    drilling fixture. New mould to

    be provided with pin provision

    for further production.

    17/12/13 17/12/13Mr.Laxman

    Surage

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    4/19

    SIA Monthly Review PPT

    ACE ENGINEERINGS & CHEMICALS PVT.LTD.

    Monthly Internal Hoshin Kanri Review MOM with top management

    S.

    No

    .

    Date Location Issue Analysis Action Target

    Dt.

    Complet

    ion Dt

    Resp. GYR

    status

    3 22/12/13 vecvGear shift cvr

    IA209914 gap

    issue.

    It is seen that the gap of 15-25 mm

    found after fitment of the part on

    line. When checked dimensionally

    height found 409-415 mm against 412

    mm. Although part as per drawing has

    also resulted in gap from chamfer

    side.

    Sample (3) provided to VECV as

    per fitment basis. Waiting for

    feedback for changes from

    VECV.

    5/1/14 TBP vecv

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    5/19

    SIA Monthly Review PPT

    Control KPI

    KPI Summary

    Months Jan-13 Feb-13March-

    13Apr-13 May-13 Jun-13 Jul-13 Aug-13 Sep-13 Oct-13 Nov-13 Dec-13

    KPI R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G

    Controlle

    d0 0 1 1 0 0 0 0 1 0 0 1 1 0 0 0 0 1 1 0 0 0 0 1 0 0 1 0 0 1 1 0 0 0 0 1

    Controlled KPI :-

    S. No.Main

    Issue

    Objective

    NameKPI Items Status

    Targets VS ActualRemark

    s13-

    Jan

    13-

    Feb

    13-

    Mar

    13-

    Apr

    13-

    May

    13-

    Jun13-Jul

    13-

    Aug

    13-

    Sep

    13-

    Oct

    13-

    Nov

    13-

    Dec

    1.

    Delivery

    Quality

    PPM

    wise

    PPM

    Improveme

    nt

    Delivery PPM

    improvement

    TARGET 325 325 325 300 300 300 250 250 250 200 200 200

    ACTUAL 49 939 96 39 606 0 756 200 90 79 682 133

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    6/19

    SIA Monthly Review PPT

    Control KPI 1 Pareto & Root Cause analysis with implementation detail

    1 1 1

    7

    9

    10

    0

    2

    4

    6

    8

    10

    12

    Handle Loose Metal Insert

    removing

    Hinge Inclined DAMAGE BOLT LOOSE PAINT PROBLEM

    DEFECT REPEATATION

    QUANTITY

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    7/19

    Customer End Rejection Monitoring from JAN '13-DEC 13

    Sno.Item

    CodeItem Name Nature of Defects

    JAN'13

    FEB'13

    MAR'13

    APR13

    MAY'13

    JUN'13

    JUL'13

    AUG'13

    SEP'13

    OCT'13

    NOV'13

    Dec;13

    Root Cause Action PlanTarget

    Date

    Statu

    s

    (RY

    G)

    1 IA22025

    9

    PANEL SHIELD

    SIDE UPPER RH

    DAMAGE 1 NA NA NAG

    2 IA22453

    5

    ASSY. ENGINE

    COVER

    BOLT LOOSE 9 Pin dia was less in

    mold.

    Mold scraped which was

    found wrong

    02-Mar-

    13 G

    100% of visual inspection

    will be done of the bolt

    before dispatch & yellow

    sticker is pasted on the hinge

    if bolt found wrong

    01-Mar-

    13

    G

    HANDLE 1 I1)mproper tightening

    of the screw

    1)Sop prepared for

    tightening the screwControl; plan has also been

    revised.

    2) Checking of handle by

    pulling it is also implemented

    at the time of PDI

    01-Nov-

    13

    G

    3 IA225381

    PAD SPRAYSUPPRESSION

    CD DIMENSIONNOT OK

    3 Drilling fixture verified& found not ok

    New drilling fixture madewith hardened bush.

    Checking of gauges is done in

    every 4 month.

    15-Feb-12

    G

    7 Drilling process is not

    adequate .

    Punching will be used for the

    control of dimension

    8/06/13

    G

    4

    IA22360

    9

    BATTERY COVER

    DAMAGE(AIR

    BUBBLE AROUND

    BUSH

    1Air bubble at the time

    of molding

    Painting process has been

    revised , checking being done

    at primer stage.

    25

    may13

    g

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    8/19

    Customer End Rejection Monitoring from JAN '13-DEC 13

    Sno

    .

    Item

    CodeItem Name Nature of Defects

    JAN'13

    FEB'13

    MAR'13

    APR13

    MAY'13

    JUN'13

    JUL'13

    AUG'13

    SEP'13

    OCT'13

    NOV'13

    Dec;13

    Root Cause Action PlanTarget

    Date

    Statu

    s

    (RY

    G)

    5IA30745

    2

    AIR CLEANER

    COVER ASSY

    DAMAGE 2 G

    DAMAGE AT

    GROMMET2

    Crack found at the position of

    grommet

    Grommet will beassemble in parts at

    supplier end

    G

    2

    Previously grommet was fixed

    by hand , due to

    transportation there are

    chances of releasing grommet

    from parts.

    At the time of fixing the

    grommet , the adhesive

    is also pasted to give

    good bonding.

    10/08/20

    13

    G

    6IA23018

    7

    COWL GRILL

    CENTER (HCV

    FACE COWL)

    DAMAGE 1 Handling damage at VECV -- NIL G

    C.C OUT

    1

    Different parts were checked

    dimensionally with logo

    fitment and found ok at

    VECV by our quality person.

    It is to be discussed with

    the VECV concern

    erson that part

    rovided is ok but the

    mating part could not

    meet the dimension.

    Sep13 G

    C.C OUT 1

    It is analyzed that C.C 280 is

    observed 277-278mm.While

    mounting the logo taking hole

    as reference the last pin (215

    C.C in part)is coming out of

    the part when logo is fitted.

    Logo pin also has variation of1 mm in C.C dimension.

    Part, tool & mating part

    dimensions measured for

    rectifying the tool. Tool

    sent to tool maker for

    modification in c.d of pin

    location.0/10/201

    3

    G

    The 2 mm variation in part &

    1 mm variation in logo

    resulted in problem

    Parts provided by filing

    the slots as an immediate

    action.

    7IA22999

    0COWL GARNISH

    LOGO FITMENT

    ISSUE

    3

    Observed that horse logo

    resent at VECV is not fitted

    and logo at our end has no

    fitment issue.

    New mould pin already

    implimented and logo

    available at VECV is

    rought at our end,parts

    now send with checking

    logo mounting on theart at PDI.

    19-Jul G

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    9/19

    Customer End Rejection Monitoring from JAN '13-DEC 13

    Sno. Item Code Item Name Nature of Defects

    JAN'13

    FEB'13

    MAR'13

    APR13

    MAY'13

    JUN'13

    JUL'13

    AUG'13

    SEP'13

    OCT'13

    NOV'13

    Dec;13

    Root CauseAction

    Plan

    Target

    Date

    Status

    (RYG

    )

    8 IA22385 DASHBOARD PAINT PROBLEM 10

    21 out of 24

    Dashboards were

    found with polythene

    impression on it,.

    Also there is

    problem with the

    paint application

    which impart thick

    layers on the part

    which gives

    polythene impression

    even after proper

    curing time.

    Holes in the

    polythene is done

    after proper curing

    time, also electric

    heaters provide

    better curing of part

    as compared with

    the earlier used gas

    furnace oven.

    17/07/201

    3G

    9 IA222215PANEL SHIELD

    T/M LOWERDAMAGE 1

    Handling damage at

    VECV.... NIL G

    10 IC322032 Cover Plate Assy. Metal insert removing 5

    the adhesive which

    we are using is notcompatible to adhere

    the metal insert with

    ABS .

    We are planning to

    change our processof joining of metal

    insert with ABS8/12/13

    G

    11 IA302841

    ENGINE HOOD

    ASSY

    Hinge Inclined 1

    CD Dimasion of the

    hole was found

    shifted due to which ,

    The hinge found

    tilted with respect to

    cd dimension

    Checking gauge

    provided at PDI to

    check the hole CD.

    Immediat

    e G

    TOTAL 1 14 2 1 8 0 13 4 1 1 5 1

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    10/19SIA Monthly Review PPT

    WATCH KPI TRENDS.No. WATCHED KPI

    MEASUREJAN FEB MAR APR MAY JUN JUL AUG SEP OCT NOV DEC

    -MENT

    1In-house monthly PDI

    PPM

    TOTAL Qty 64687 52930 66373 76000 80401 75486 74546 59406 37720 54275 27955 61144

    REJECTED 242 200 250 253 323 195 390 286 205 208 98 169

    ACTUAL 3741 3778 3767 3470 4020 2580 5231 4814 5434 3680 3520 2760

    TARGET 3800 3800 3800 2500 2500 2500 2000 2000 2000 1500 1500 1500

    2-AIn-house monthly

    Process PPM (Molding)

    ACTUAL

    Activity started from may

    -* 2680 3338 8678 2800 2000

    TARGET 3500 3500 3200 3200 5000 3000 3000 3000

    2-BIn-house monthly

    Process PPM (Filing)

    ACTUAL

    Activity started from september8931 4950 4800 4850

    TARGET TBF 5000 5000 5000 5000

    2-C

    In-house monthly

    Process PPM(Painting)

    ACTUAL

    Activity started from september

    11139 8051 9580 6850

    TARGET TBF 7000 7000 7000 7000

    3In-coming monthly

    PPM

    ACTUAL 3400 0 0 0 0 0 0 0 0 0 0 0

    TARGET 4000 4000 4000 3500 3500 3500 3000 3000 3000 2500 2500 2500

    4

    No of DOL partsACTUAL

    61 61 58 60 62

    (Total 68 parts)TARGET

    62 62 62 63 63 63 65 65 65 66 66 66

    5

    PDI Execution (% ofPDI followed

    invoices/Total invoices

    raised)

    No OF PDI 60 55 50 55 51 50 51 60 60 55 55 55

    ACTUAL 100 100 100 100 100 100 100 100 100 100 100 100

    TARGET 100 100 100 100 100 100 100 100 100 100 100 100

    6Process audit (No of

    parts )

    ACTUALActivity started from may

    5 5 3

    TARGET 5 5 3

    7

    Dock audit (No of

    parts)

    ACTUAL

    Activity will start from june

    30 10 10 10 10 10 10

    TARGET 30 10 10 10 10 10 10

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    11/19SIA Monthly Review PPT

    S.No. WATCHED KPIMEASURE

    -MENTJAN FEB MAR APR MAY JUN JUL AUG SEP OCT NOV DEC

    8

    Raw material

    inspection plan

    ACTUAL

    Activity started from

    APRIL..

    2 2 2

    (Third party)TARGET

    2 2 2

    9Layout inspection

    (No. of parts)

    ACTUAL 7 7 5 5 10 8 6 9 6 9 8 4

    TARGET

    7 7 5 5 10 8 6 9 6 9 8 4

    10IMTE and Gauge

    Calibration

    ACTUAL .. 11

    TARGET

    .. .. .. .. .. .. .. 8

    11

    Tooling validation

    (Dies, Jigs & Fixture

    validation &

    Maintenance)

    ACTUAL

    Activity started from may..

    3 2 5 3 3 3 3 3

    TARGET 3 2 5 3 3 3 3 3

    12 Poka YokeACTUAL 1 1 1 1 0 2 0 1 0 2 2 1

    TARGET 1 1 1 1 2 2 2 2 2 2 2 2

    13 QS Sign offACTUAL

    Activity will start from june..0

    TARGET 40 26

    14 System audit scoreACTUAL 85%

    TARGET95%

    KPI Summary

    Months Jan-13 Feb-13 March-13 Apr-13 May-13 Jun-13 Jul-13 Aug-13 Sep-13 Oct-13 Nov-13 Dec-13

    KPI R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G R Y G

    Watched 0 0 1 1 0 0 0 0 1 0 0 1 1 0 0 0 0 1 1 0 0 0 0 1 6 0 7

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    12/19SIA Monthly Review PPT

    Open Red KPI Status

    S.

    No.KPI Month

    Red

    ParameterReason Root Cause Action

    Target

    DateResp. Status

    1

    controlled

    g

    2

    W

    atched

    Inhouse

    RejectionHole Not Clear

    During painting

    metafill deposition

    mistakenly on the

    part lead to hole

    block.

    Painting supervisor

    instructed to check part

    visually before sending

    to PDI. & Clear hole

    before proceeding

    ImmediateMayur

    AjmeraG

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    13/19SIA Monthly Review PPT

    Road-map status to achieve KPI

    KPI Action to achieve the KPI TARGET RESPONSIBILITY

    In-house monthly PDI PPM In process improvement & in process

    checking June'13 Mr.Mayur Ajmera

    In-coming monthly PPMSupplier up gradation through

    supplier audit July'13 Mr.R.Patidar

    No of DOL parts

    100% gauging implementation, And

    special focus on repeated issue July'13

    Mr.Mayur

    Ajmera,Mr.Laxman

    Surage and

    Mr.Mayaram Sharma

    Defect analysis in QRQC Jan'13 Mr. Jasvin S Bhatia

    Information of defect to the down

    level through involvement of

    workers in QRQC Jan'13

    Top Management

    Process auditStrengthening the QC department June'13 Top Management

    Raw material inspection plan Third party involvement for

    inspection July'13 Mr.Mayur Ajmera

    Tooling validation (Dies, Jigs &

    Fixture validation & Maintenance)Validation of drilling fixtures with in

    4 months April'13 Mr. Rajan S Patta

    Poka Yoke Daily QRQC & Involvement of CFT

    team Jan13 Mr. Mayur Ajmera

    System audit score

    Internal Audit June'13 &July'13 QC & MR

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    14/19SIA Monthly Review PPT

    Layout StatusS.

    No.Month

    Comp.

    Planed

    Comp.

    Complet

    ed

    N. C.

    obser

    ved

    N. C.

    Closed

    Cumulati

    ve Open

    N.C.

    Reason for open NC

    Target

    date for

    Open N

    C

    Resp. Remarks

    1 Jan-13 7 7 0

    2 Feb-13 7 7 1 1 0

    3 Mar-13 5 5 0

    4 Apr-13 5 5 1 1 0

    5 May-13 10 10 2 1 1 Drawing req. from VECV.15 JULY

    2013vecv

    Horizontal slots

    converted to vertical as

    per req in air cleaner

    cover assy.

    6 Jun-13 8 8 1 0 1As per fitment part is ok, but still it is to

    verify whether dim variation.

    15 JULY

    2013

    Quality

    dept.

    7 Jul-13 6 6 0 0

    8 Aug-13 9 9 1 1 0

    9 Sep-13 6 6 1 1 0

    10 Oct-13 9 9 1 0 0

    Due to fouling of RH part in mudguard 12

    mm trimming of the part has to be done

    according to the fitment purpose, But the

    LH (IA222296) IS SUPPLIED

    ACCORDING TO THE WIDTH GIVEN IN

    DRAWING .

    15/10/1

    3

    VECV Mr.

    Vinay

    Gupta

    The drawing has to be

    revised according to the

    reduced width

    11 Nov-13 9 9 0

    12 Dec-13 4 4 0

    7 7

    5 5

    10

    8

    6

    9

    6

    9 9

    1

    65

    4

    87

    6

    8

    5

    89

    0

    2

    4

    6

    8

    10

    12

    No. of Parts completed 100% Green Parts

    0

    1

    0

    1

    2

    1

    0

    1 1 1

    00 0 0

    1 1

    0 0

    1 1

    0 00

    1

    00

    1 1

    0 0 0 0

    0

    0.5

    1

    1.5

    2

    2.5

    Total N.C. N.C. Closed Cumm. Pending N.C.

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    15/19SIA Monthly Review PPT

    In-house PPM Trend

    PARETO FOR TOP CONTRIBUTOR

    0

    1000

    2000

    3000

    4000

    5000

    6000

    INHOUSE PPM TREND

    PPM

    34

    26 2421

    5

    05

    10152025

    303540

    REJECTED

    QUANTITY

    TOP CONTRIBUTOR OF DEC'13

    In-house Rejection Status

    S. No. Part No.

    Non-

    conformance

    Detail

    Repeated or

    NotRoot Cause ACTION Target date Resp. Status

    1 ID206599Hole Not

    Clear

    R

    ep

    a

    t

    e

    d

    During

    painting

    metafill

    deposition

    mistakenly

    on the part

    lead to hole

    block.

    Painting

    supervisor

    instructed to

    check part

    visually

    before

    sending to

    PDI. & Clear

    hole before

    proceeding

    ImmediateMayur

    Ajmera

    g

    2 IA303087Hole Not

    Clear

    3 IA218893 Hole Not Clear

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    16/19SIA Monthly Review PPT

    Improvement plan & status

    IMPROVEMENT PLAN 2013

    Sl. No Particulars PLAN DETAILS Target Responsibility

    1

    Quali

    tyrelatedimpro

    vements

    Raw Material Inspection

    Third party APRIL '13

    Mr. Mayur Ajmera

    2

    Measurement of Raw

    Material at shop floor MAY'13Mr. Abhinav

    3

    Avoid repeated customer

    complaint JUNE'13Mr.Mayur Ajmera

    4Dock audit to be conduct

    JUNE'13Mr. Jasvin S Bhatia

    5

    Arrange of all gauges near

    the working area. JULY'13

    Mr.Jasvin S Bhatia

    6

    100% Guaging

    Implementation of all the

    parts JULY'14

    Mr.Mayur Ajmera; Mr. Laxman Surage

    7

    Aim for 0 ppm at

    customer end JULY'13Mr. Mayur Ajmera

    8

    100% will be checked in

    layout report. JULY'13Mr.Jasvin S Bhatia

    9To achieve quality System

    Audit Score 95% AUG'13Mr. Mayur Ajmera

    10

    Punching Die

    Implementation For all

    types of mud flap AUG'13

    Mr. Nikhil Jain

    11

    Machine for Dry

    Sandering Is to Be Started

    For Better Results SEP'13

    Mr. Mayur Ajmera

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    17/19SIA Monthly Review PPT

    POKA YOKE IMPLEMENTATION DEC13

    CHECKING GAUGE FOR CD DIMENSION ENGINE HOOD ASSY IA302841

    Checking of Hole By qualifying with PIN

    CD dimension

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    18/19SIA Monthly Review PPT

    General Awareness About 5S

    Training conducted at our plant regarding general awareness

    about 5 S, under the guidance of Mr. Sanjay Agrawal Sir.

  • 8/10/2019 Copy of Hoshin KanrDec2013 (1)

    19/19SIA M thl R i PPT

    Thanks


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