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MANAGEMENT PROGRAM FOR SPENT MODIFIED IN SITU RETORTS J. E. Boysen and J. R. Coveil Western Research Institute University of Wyoming Research Corp. P. O. Box 3395, University Station Laramie, WY 82071 By R. G. Vawter Occidental Oil Shale Inc. P. O. Box 880408 Steamboat Springs, CO 80488 K. G. Kofford and J. E. Marshall EMRx Corporation P. O. Box 1550 Palisade, CO 81526 ABSTRACT Following the completion of retorting, modified in situ (MIS) retorts are cooled and treated to produce an environmentally benign structure, which can ultimately be reclaimed in compliance with state and federal environmental regulations. Post-retorting experiments have been conducted for a number of years at the Occidental Oil Shale Inc. Logan Wash site near De Beque, Colorado to collect environmental data from in situ retorts completed nearly a decade ago. The data collected, along with studies conducted by the Western Research Institute, EMRX Corporation, and others have shaped a program for circulating water through spent MIS retorts in a manner that reduces materials which could impact groundwater to acceptable levels and uses process and indigenous waters efficiently. INTRODUCTION Occidental Oil Shale Inc. (OOSI) successfully demonstrated its modified in situ (MIS) oil shale retorting technology by conducting large-scale field tests at its Logan Wash facility near De Beque, Colorado. OOSI operated the Logan Wash MIS retorting facility from 1972 until 1982 (Stevens and Zahradnik 1983). The MIS technology developed by OOSI was proven technically feasible and commercial projections suggest that the technology can be profitable in the future. One of the environmental concerns associated with in situ processing is the impact of the process on local groundwater. Chemical compounds potentially soluble in groundwater are created during MIS retorting. The hot spent retorts must be cooled and then cleaned of these water-soluble chemical compounds to mitigate the process's impact on local groundwater. Spent retorts were cooled and cleaned at Logan Wash by circulating water through the retorts to remove soluble materials. Water produced from the MIS retorts (process water) was used in the cooling and initial stages of the cleaning. Baseline quality groundwater collected in the mine sumps (mine water) was used in the later stages of the cleaning. The groundwater quality from most spent retorts at Logan Wash is restored to near baseline. These experiments, conducted by OOSI and its contractor EMR^, demonstrated that impact on groundwater quality from MIS retorting can be mitigated. However, a commercial-scale operation requires careful water management to ensure that sufficient water is available to clean all spent retorts created. OOSI is developing plans for demonstrating commercial-scale oil production from a federal prototype oil shale lease (Tract C-b) in northwestern Colorado. OOSI contracted with the Western Research Institute (WRI) to conduct laboratory research and analytical studies for optimum commercial-scale water management. OOSI also contracted with EMR^ to continue field tests of potential water management schemes at Logan Wash. The goal of the two efforts is a cost-effective procedure for cleaning commercial spent retorts that optimizes use of the supply of water. This paper discusses the MIS oil shale retorting technology development by OOSI, the post-retorting conditions of spent MIS retorts, the previous research conducted by OOSI and EMRv to mitigate potential groundwater impact, the current research by EMRx anc* WRI to develop cost-effective procedures for cleaning commercial spent retorts, and OOSI's future plans for commercializing MIS oil shale retorting. Development of the MIS Oil Shale Retorting Technology The OOSI MIS process requires that a retort be constructed underground using explosives to fracture the oil shale and create the permeability necessary for retorting. In order to effectively fracture the oil shale and create permeability, a portion of the oil 133
Transcript
Page 1: facility EMRx · 2012. 2. 6. · MANAGEMENTPROGRAMFORSPENTMODIFIEDINSITURETORTS J.E.BoysenandJ.R.Coveil WesternResearchInstitute UniversityofWyomingResearchCorp. P.O.Box3395,UniversityStation

MANAGEMENT PROGRAM FOR SPENT MODIFIED IN SITU RETORTS

J. E. Boysen and J. R. Coveil

Western Research Institute

University ofWyoming Research Corp.

P. O. Box 3395, University Station

Laramie, WY 82071

By

R. G. Vawter

Occidental Oil Shale Inc.

P. O. Box 880408

Steamboat Springs, CO 80488

K. G. Kofford and J. E. Marshall

EMRx CorporationP. O. Box 1550

Palisade, CO 81526

ABSTRACT

Following the completion of retorting, modified in situ (MIS)

retorts are cooled and treated to produce an environmentally

benign structure, which can ultimately be reclaimed in compliance

with state and federal environmental regulations. Post-retorting

experiments have been conducted for a number of years at the

Occidental Oil Shale Inc. Logan Wash site near De Beque,

Colorado to collect environmental data from in situ retorts

completed nearly a decade ago. The data collected, along with

studies conducted by theWestern Research Institute, EMRX

Corporation, and others have shaped a program for circulating

water through spent MIS retorts in a manner that reduces

materials which could impact groundwater to acceptable levels and

uses process and indigenous waters efficiently.

INTRODUCTION

Occidental Oil Shale Inc. (OOSI) successfully demonstrated its

modified in situ (MIS) oil shale retorting technology by conducting

large-scale field tests at its Logan Wash facility near De Beque,

Colorado. OOSI operated the Logan Wash MIS retorting facility

from 1972 until 1982 (Stevens and Zahradnik 1983). The MIS

technology developed by OOSI was proven technically feasible and

commercial projections suggest that the technology can be

profitable in the future.

One of the environmental concerns associated with in situ

processing is the impact of the process on local groundwater.

Chemical compounds potentially soluble in groundwater are

created during MIS retorting. The hot spent retorts must be

cooled and then cleaned of these water-soluble chemical

compounds to mitigate the process's impact on local groundwater.

Spent retorts were cooled and cleaned at Logan Wash by

circulating water through the retorts to remove soluble materials.

Water produced from the MIS retorts (process water) was used in

the cooling and initial stages of the cleaning. Baseline quality

groundwater collected in the mine sumps (mine water) was used in

the later stages of the cleaning. The groundwater quality from

most spent retorts at Logan Wash is restored to near baseline.

These experiments, conducted by OOSI and its contractor EMR^,

demonstrated that impact on groundwater quality from MIS

retorting can be mitigated. However, a commercial-scale

operation requires careful water management to ensure that

sufficient water is available to clean all spent retorts created.

OOSI is developing plans for demonstrating commercial-scale

oil production from a federal prototype oil shale lease (Tract C-b)

in northwestern Colorado. OOSI contracted with the Western

Research Institute (WRI) to conduct laboratory research and

analytical studies for optimum commercial-scale water

management. OOSI also contracted with EMR^ to continue field

tests of potential water management schemes at Logan Wash.

The goal of the two efforts is a cost-effective procedure for

cleaning commercial spent retorts that optimizes use of the supply

of water.

This paper discusses the MIS oil shale retorting technology

development by OOSI, the post-retorting conditions of spent MIS

retorts, the previous research conducted by OOSI and EMRv to

mitigate potential groundwater impact, the current research by

EMRx anc* WRI to develop cost-effective procedures for cleaning

commercial spent retorts, and OOSI's future plans for

commercializing MIS oil shale retorting.

Development of the MIS Oil Shale Retorting Technology

The OOSI MIS process requires that a retort be constructed

underground using explosives to fracture the oil shale and create

the permeability necessary for retorting. In order to effectively

fracture the oil shale and create permeability, a portion of the oil

133

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shale in the retort is mined to provide the void volume needed for

the remaining oil shale to expand into when it is fractured with

explosives. To create a rubble bed, explosives are set and ignited

in boreholes drilled from the mined areas into unfractured oil

shale.

The top of the oil shale rubble bed is heated to Ignition

temperature using hot inert gas. When the oil shale is hot enough

for ignition, air is injected into the rubble bed to begin combustion

and retorting of the oil shale. The hot gases, produced by

combusting the residual carbon that remains after retorting, flow

downward through the rubble bed and pyrolyze the kerogen in the

oil shale ahead of the advancing combustion front. Oil from

kerogen pyrolysis and gases from both kerogen pyrolysis and oH

shale combustion are produced at the bottom of the rubble bed

(McCarthy et al. 1976; McCarthy and Cha 1976).

Eight MIS retorts were constructed and operated by OOSI at

Logan Wash (Figure 1). The first six were designed to determine

the effects of the geometry of the mined void area, explosive

fracturing tecliniques, and ignition and operating procedures on

retorting efficiency. Retorts 7 and 8, the last two MIS retorts

operated by OOSI, were commercial-scale and operated

simultaneously to simulate commercial operation (Figure 2). These

retorts were designed to demonstrate the technical feasibility of

MIS technology at a commercial scale.

Results obtained from processing Retorts 7 and 8 prove that

commercial-scale oil shale retorting using the OOSI MIS process is

technically feasible. The processing of oil shale using these retorts

confirmed that a high oil yield can be achieved in retorts with low

void volumes. Further, the results confirmed that the

straightforward retort construction and operation used in Retorts 7

and 8 can potentially achieve economic oil recovery(Stevens and

Zahradnik 1983).

Conditions that Cause MIS Groundwater Impact

A better understanding of the MIS groundwater impact

process is needed to minimize the amount of water required to

clean commercial spent retorts. The conditions existing in a MIS

retort after retorting is nearly completed areillustrated in Figure 3.

The rubble bed in the retort consists of three distinct zones: raw

unretorted oil shale, retorted oil shale, and combusted oil shale.

The residual carbon remaining after retorting wascombusted in

the top part of the bed. Unretorted oil shale underwent limited or

no thermal alteration in the bottom of the bed, and it is possible

that heavy fractions of the oil produced from retorted shale

condensed there. Between these zones, retorted oil shale

underwent thermal pyrolysis, which produced oil and gas from the

shale.

After retorting, temperature in the retort remains high. The

temperature in many parts of the combusted shale zone exceed

1500F (816C). The temperatures in the retorted and

unretorted zones are progressively cooler but can be as hot as

1000 and 500F (538 and 260C), respectively. The sides and

bottom of the rubble bed are surrounded by oil shale that was not

explosively fractured (pillars). Also, an air space or void exists at

the top of the retort (Figure 3).

Two sources for potential groundwater impact exist because

of the retort conditions when processing ceases. One source of

impact is water-soluble material remaining in the spent retort.

Another less obvious potential source is water-soluble material

OCCIDENTAL OIL SHALE

RETORT S

7MS'

UPPER INTERMEDIATE LEVEL

LOWER INTERMEDIATE LEVEL

PRODUCT LEVEL

RETORT 5

RETORT 4

78S9'

TUB-

UPPER ROOMAM LEVEL

SUXPRXAR

5

<US=

cc

5

o

<

m

5

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a

RETORT IE

777a

j*j :

7J00

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7120

7*00

77BD

77M

-7740

77

7700

-7M0

-7HO

7H0

-TWO

-7M0

-7SW

-7M0

Figure 1 . Summary of the MIS Retorts at the Logan Wash Site

134

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Figure 2. Isometric View of Retorts 7 and 8

generated by the continuing kerogen pyrolysis in the pillars and

unretorted shale. This post operation pyrolysis occurs as a result

of energy or residual heat stored in the hot spent shale. A spent

MIS retort, similar to Retorts 7 or 8, contains more than 100

billion Btu of residual heat. This energy needs to be removed from

the MIS retort to minimize post retorting pyrolysis and also to

prevent heat conduction into the surrounding pillars, thereby

preventing a reduction of their mechanical strength. In addition,

the amount of energy in the form of residual heat from a

commercial operation is considerable and, if used, can significantly

improve the overall MIS thermal efficiency (Hester and Jacobson

1983).

Effective procedures to clean spent retorts must cool the

retort to preserve mine integrity, use residual heat in the spent

retort to react much of the soluble material into insoluble forms,

and provide a means by which to remove remaining water-soluble

contaminants from the retort. Experiments were conducted at

Logan Wash by OOSI and EMR^ to develop procedures to clean

spent retorts. The following section discusses the results of these

experiments.

Environmental Research Conducted using Retorts 7 and 8

The water management procedures needed for MIS

operation liave been investigated by OOSI and EMR^ since 1982

using Retorts 7 and 8. In November of 1982, a short time after

the completion of processing Retorts 7 and 8, OOSI initiated

water-quenching studies on these full size retorts. Water

quenching was initiated to accelerate the cool down of these spent

retorts. In addition, recovery of residual heat from spent retorts in

135

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Raw Oil Shale/Condensed Oil

Product Level Bulkhead

Figure 3. MIS Post-Retorting Conditions

the form of combustible gases generated through steam-carbon

reactions was investigated. The water quenching research also

removed many of the potentially soluble materials from the retorts.

A quench-water flow rate of 50 gal/min into each of the two

retorts was desired but sufficient quantities of water were not

available at the Logan Wash site to maintain this flow rate in both

retorts. Consequently, quenching research concentrated on Retort

8 where the desired quench-water flowrate was maintained for

several months. Thus, Retort 8 is more thoroughly evaluated

because it has undergone more thorough quenching than Retort 7

which was quenched with less water or Retort 6 which was not

quenched.

Details regarding the results of the initial quenching of these

spent retorts in 1982 and 1983 are reported by Hester and

Jacobson (1983). These initial experiments, using process water,

confirmed that water quenching is a viable procedure by which to

cool spent retorts. Reactions of the quench water with hot

material in the spent retort produced combustible gases and clean

condensate. From 1983 through 1988, periodic water injection

into the retorts continued to examine cooling of the retortsand

material removal from the retorts.

In December 1988, OOSI and EMRX tested another

potential retort cleaning procedure called staged deluge. The

staged deluge removes soluble compounds from spent retorts by

circulating water through the rubble bed. A grid of 26 water

injection points was constructed at the top of the rubble bed by

drilling from the upper mine level (instrument air level). Roughly

170,000 gal of water were injected sequentially into each of the

injection points at a high rate of approximately 1,000 gal/min.

The water collected in the lower portion of the retort was

reinjected into the retorts. During the staged deluge, roughly

500,000 gal of water (approximately three injections) was injected

into each of the 26 injection points.

The concentrations of retort-induced constituents in the

process waters from Retort 8 decrease with time. Figure 4 shows

the concentrations of dissolved organic carbon (DOC) in the

process water as a function of time (retort completion given as July

1982). Vertical dashed lines in the figure represent periods of

quenching or staged deluge. From this figure alone, the impact of

quenching on DOC concentrations is not obvious.

DOC concentrations may also have been reduced as a result

of the staged deluge. Figure 5 shows the DOC concentrations in

process water from Retort 8 for the period January 1, 1985,

through September 21, 1989. Again, vertical dashed lines in the

figure represent the periods of quenching or staged deluge. The

dashed line on day 2334 is the start of the staged deluge. There

are periodic fluctuations in the DOC concentrations. The reasons

for these fluctuations are again not obvious, and the fluctuations

make evaluation of these data difficult. It is also difficult to

determine from this figure if the staged deluge caused the

reduction in DOC concentrations or if the reduction was a

continuation of the short-term natural cleansing trend.

However, comparisons of DOC concentrations in process

water from Retort 8 with process water from other retorts that

were not quenched (Retort 6) or were partially quenched (Retort 7)

show that both quenching and staged deluge do reduce DOC

concentrations to a certain extent. After approximately 87

months (2,610 days), the DOC concentration in process water

from Retort 6 was 175 mg/L (Figure 6). This value compares to

80 mg/L measured in process water from Retort 8 at the

corresponding time after retort completion. Likewise for process

water from Retort 7, the DOC concentration on February 27,1989 was 210 mg/L compared to 95 mg/L for Retort 8 on the

same day. Retort 7 was quenched with roughly 20% of the

amount of process water used in Retort 8.

136

Page 5: facility EMRx · 2012. 2. 6. · MANAGEMENTPROGRAMFORSPENTMODIFIEDINSITURETORTS J.E.BoysenandJ.R.Coveil WesternResearchInstitute UniversityofWyomingResearchCorp. P.O.Box3395,UniversityStation

Total dissolved solids (TDS) concentrations in the process

water from Retort 8 show a steady increase since the monitoring

of these concentrations began (Figure 7). During periods of

quenching, TDS concentrations temporarily increased. There is a

linear increase in TDS concentration with time. The major TDS

constituent in the process water is sulfate.

The environmental remediation research conducted by OOSI

using spent Retorts 7 and 8 lead to the following observations.

First, the quenching of spent retorts with water is effective in

reducing the temperatures in the spent retorts and, thereby,

reducing kerogen pyrolysis that occurs after retorting. The current

temperatures monitored in Retort 6, which was not quenched, are

greater than those monitored in Retorts 7 and 8 which were

shutdown much later and were quenched. In addition, the water

quenching removed much of the residual carbon from these retorts

and transported it to the surface in the form of combustible gas.

The gas can be used to supply energy that is required for the plant

operations (Hester and Jacobson 1983). Second, the

concentrations of potential organic contaminants in process water

flowing from the retorts decreases naturally with time but this

decrease can be accelerated by quenching with water. The current

DOC concentration in the process water flowing from Retort 8 is

lower than the current DOC concentrations in the process water

flowing from either Retort 7 or Retort 6 (EMRX 1989).

In August 1989, EMRX modified the staged deluge process

by using clean water for the deluge instead of recycling water from

spent retorts. More soluble constituents were removed from the

spent retort using clean deluge water than were removed using

recycled deluge water. This behavior is typical of mass transfer-

controlled processes.

In a mass transfer-controlled restoration process, the

concentration gradient between the injected waters and the area

being cleaned regulates the rate of constituent removal. In the

initial stages of restoration, the concentrations of soluble materials

in a spent retort are high, and these constituents dissolve readily in

clean water. However, as the retort is cleaned, the concentration

gradient decreases, and the rate of chemical constituent

solubilization into injected waters declines. When this occurs,

removal of the soluble materials from the retort can be increased

by injecting cleaner water to increase the concentration gradient.

The procedure of injecting clean water to decrease the amount of

time required for the final stages of groundwater restoration is

used successfully to restore groundwater from uranium solution

mining wellfields.

Examination of the data presented in Figure 4 shows that the

decline in the concentration of DOC in the process water from

Retort 8 slowed in 1989. This indicated that it was time to inject

cleaner water into the retort to accelerate the further removal of

soluble constituents. Deluges conducted in August 1989

confirmed that using clean water accelerated DOC removal.

However, the major problem with continuing to deluge Retort 8

with clean water is the limited availability of water at Logan Wash.

In January 1990, EMRX continued the staged deluge of

Retort 8 using the relatively clean water flowing into the mine

drifts at Logan Wash. The results of the first two deluges in Retort

8 using mine water were similar to the August 1989 clean water

deluges. Process water produced from these deluges was disposed

of in an evaporation pond near the Logan Wash site rather than

reinjecting it into the retorts. The results thus far show increased

removal of soluble compounds from Retort 8 using mine water in

place of process water for deluging. By using the indigenous

water at the site, the need to acquire clean water for the retort

cleaning was reduced.

In summary, the water quenching and staged deluge of Retort

8 successfully reduced the amount of time required for cleaning

spent MIS retorts. However, the time required for cleaning spent

retorts still needs to be minimized.

Current Research Activities

Currently, OOSI plans to continue pursuing

commercialization of the MIS oil shale retorting technology. The

procedure and schedules required for cleaning spent MIS retorts

need to be developed more quantitatively for commercialization.

EMRX and theWestern Research Institute (WRI) are presently

contracted to quantify the water management procedures for

cleaning the spent retorts. EMRX will continue to investigate the

cleaning of Retorts 7 and 8 at Logan Wash using the staged

deluge procedure, and WRI will conduct laboratory research to

investigate the potential benefits of other procedures that can be

applied with the quenching and deluge procedures to reduce the

time and resources required for cleaning spent retorts.

EMRX continues to deluge Retort 8 using mine water and

then discharges the produced water to the evaporation pond. At

Logan Wash however, the amount of mine water is limited, so

methods to increase the frequency and effectiveness of deluges

without using additional water will be investigated. One method to

achieve more deluges per month without requiring additional clean

137

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Quenching

Staged Deluge

i 1 1 i i i i 1

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600 800

Days Si nee

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Figure 4. DOC Concentrations in Retort 8 Waters from 1983 to 1989

0-

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700 800 900 1000 1100 1200 1300 1400 1500 1600 1700 1800 1900 2000 2100 2200 2300 2400 2500 2600 2700 280Q

Days Sine* Retort Completion

Figure 5. DOC Concentrations in Retort 8 Waters from 1985 to 1989

138

Page 7: facility EMRx · 2012. 2. 6. · MANAGEMENTPROGRAMFORSPENTMODIFIEDINSITURETORTS J.E.BoysenandJ.R.Coveil WesternResearchInstitute UniversityofWyomingResearchCorp. P.O.Box3395,UniversityStation

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Months Since July 1979

Figure 6. DOC Concentrations in Retort 6 Waters from 1979 to 1989

14500

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0 1 1 1 1 1 1 1 1 1 1 1 1 1 \ 1 1 1 \ 1 1 1800 900 1000 1100 1200 1300 1400 1500 1600 1700 1800 1900 2000 2100 2200 2300 2400 2500 2600 2700 2800

Days Since Retort Completion

Figure 7. TDS Concentrations in Retort 8 Waters from 1985 to 1989

139

Page 8: facility EMRx · 2012. 2. 6. · MANAGEMENTPROGRAMFORSPENTMODIFIEDINSITURETORTS J.E.BoysenandJ.R.Coveil WesternResearchInstitute UniversityofWyomingResearchCorp. P.O.Box3395,UniversityStation

water is to treat the deluge water to remove potential

contaminants and then reinject the treated water for another

deluge.

WRI is constructing a laboratory-scale simulator for the MIS

retort cleaning process. The objective of the simulations is to

determine a post-retort ing operating procedure for optimal water

management during the cleaning of the spent retorts. WRI will use

the experimental set-up illustrated in Figure 8 for the laboratory-

scale simulations.

Water Influx Tubas

with Thermocouples

InsirJt \ i;:^vJ fc^fl Vffl\>s'"A',':Crushed Oil Shale

Thermocouple and

ouch

ProductWater Collector

Bottom

'Water Injection

Tube

Sealed Top

Product Water

Collector Tubes

Sealed Bottom

Figure 8. MIS Groundwater Contamination Simulation

Experimental Set-up

Post-retorting conditions in spent MIS retorts will be

simulated inside an 8-inch-diameter stainless steel pipe by creating

a rectangular area (5 by 5 inch) into which a rubble bed of oil shale

can be charged. The rubble bed will be heated to ignition

temperature with inert gas and combusted with air. This

procedure is similar to the retorting procedure used at Logan

Wash. Retorting will be stopped before the rubble bed is

completely retorted. Stopping at this point will create conditions

similar to those shown in Figure 3.

After conditions in spent retorts are simulated, procedures to

accelerate retort clean-up without using largevolumes of water will

be investigated. Sample pouches will be located in the bed. These

pouches will be constructed of stainless steel screen, and a

thermocouple will be inserted in each pouch to provide a

temperature history of the experiment on the sample.These

samples will be used to determine the amount of water-soluble

constituents in the spent shale and the rehydration characteristics

of the spent shale. The simulator will have ports for water

injection to simulate water influx, quenching, and deluge. The

outlets at the bottom of the simulation retort will be similar in

design to Retorts 7 and 8 at Logan Wash. The total organic

concentration of injected and produced waters will be determined

to evaluate the success of different spent retort cleaning

procedures.

In addition, a larger simulation of the best post-retorting

operating procedure will be conducted using WRI's 10-ton retort.

The procedure for the 10-ton retort will be similar to that used in

the laboratory.

The results from EMRX field testing at Logan Wash and

results from WRI simulations will be used to develop a

comprehensive plan for cleaning commercial spent MIS retorts.

Future Plans

The OOSI long-term plan is to commercialize MIS retorting.

Negotiations are in progress to solicit U.S. Department of Energy

participation in construction and operation of a 1200 bbl/day

proof-of-concept oil shale facility at Tract C-b (the project). The

project will be designed to improve commercial economics by

maximizing total resource use. The oil shale mined to construct

MIS retorts will be burned in a circulating fluidized-bed combustor

(CFBC) to generate electric power. The CFBC will be co-fired

with MIS off gas, oil shale and coal to provide electrical power and

steam for the project and also for export power to local

consumers. The co-firing with oil shale, because of its alkaline

mineral content, will control sulfur emissions from the power-

generating plant. In addition, the CFBC can use the combustible

gas generated from quenching of spent retorts to improve the

overall plant efficiency.

The project construction will require three years, and plans

are to operate the facility for seven years. MIS retort construction

and operation procedures will be similar those of Retorts 7 and 8

at Logan Wash. Plans are to simultaneously operate two MIS

retorts. In addition, the spent retort cleaning procedure resulting

from the work of EMRj^ and WRI will be tested. Experience

gained from the continuous operation over the seven-year period

will be used to design and construct a 23,000 bbl/day commercial

plant on Tract C-b (Bechtel 1989).

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The demonstration of an integrated commercial-scale MIS oil

shale retorting facility will provide the United States with a

commercially proven and environmentally acceptable technology

to reduce dependence on foreign oil supplies beyond the year

2000. It is imperative that such technologies be developed by the

time world oil reserves significantly decline.

SUMMARY

In summary, the efforts of OOSI from 1972 to 1982 to

develop a commercial technology for producing oil from oil shale

resources in the western United States resulted in the MIS oil shale

retorting process. This process was proven technically feasible on

a large scale and is also simple and straightforward. After 1982,

OOSI and its contractor EMRj^ continued to pursue development

of the MIS technology by conducting research both to optimize the

process's resource recovery and to minimize the process's

environmental impact. The results suggest that resource recovery

and overall economics can be improved by using the oil shale

mined during the construction of the MIS retorts as a fuel for

electric power generation. Also, the residual heat contained in a

spent MIS retort can be used to generate clean combustible gas for

use as fuel. In addition, cleaning of several of the spent MIS

retorts was achieved. However, a reduction in the time and effort

required for completely cleaning spent MIS retorts will improve the

commercial economics of the process.

OOSI plans to continue efforts to commercialize the MIS

technology by constructing a 1200 bbl/day proof-of-concept

engineering scale demonstration plant. In support of this

objective, EMR^ and WRI are working together to develop

cleaning procedures for spent MIS retorts that are cost effective,

easy to implement and minimize environmental impact.

REFERENCES

Bechtel, Inc., 1989, Western States Oil Shale Recovery

Program, Bechtel Job Number 20227-000.

EMRX Corporation, 1989, Retort Staged Deluge

Progress Report, Through October 15, 1989.

Unpublished report submitted to Occidental Oil

Shale, Inc.

Hester, N.E., and C. Jacobson, 1983, The Utilization

of Residual Heat in Spent MIS Retorts for

Wastewater Treatment and Process

Improvements. Proceedings of the 16th Oil Shale

Symposium, Golden, CO. pp 487-497.

McCarthy, HE., C.Y. Cha, W.J. Bartel, and RS.

Borton, 1976, Development of the Modified In

Situ Oil Shale Process. AIChE Symposium Series,

v72, No. 155, pp 14.

McCarthy, H.E., and C.Y. Cha, 1976, Modified In Situ

Oil Shale Process Development and Update.

Proceeding of the 9th Oil Shale Symposium,

Golden, CO. pp 85-100.

Stevens, A.L., and R.L. Zahradnik, 1983, Results from

the Simultaneous Processing of Modified In Situ

Retorts 7 & 8. Proceeding of the 16th Oil Shale

Symposium, Golden, CO. pp 267-280.

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