MANAGEMENT PROGRAM FOR SPENT MODIFIED IN SITU RETORTS
J. E. Boysen and J. R. Coveil
Western Research Institute
University ofWyoming Research Corp.
P. O. Box 3395, University Station
Laramie, WY 82071
By
R. G. Vawter
Occidental Oil Shale Inc.
P. O. Box 880408
Steamboat Springs, CO 80488
K. G. Kofford and J. E. Marshall
EMRx CorporationP. O. Box 1550
Palisade, CO 81526
ABSTRACT
Following the completion of retorting, modified in situ (MIS)
retorts are cooled and treated to produce an environmentally
benign structure, which can ultimately be reclaimed in compliance
with state and federal environmental regulations. Post-retorting
experiments have been conducted for a number of years at the
Occidental Oil Shale Inc. Logan Wash site near De Beque,
Colorado to collect environmental data from in situ retorts
completed nearly a decade ago. The data collected, along with
studies conducted by theWestern Research Institute, EMRX
Corporation, and others have shaped a program for circulating
water through spent MIS retorts in a manner that reduces
materials which could impact groundwater to acceptable levels and
uses process and indigenous waters efficiently.
INTRODUCTION
Occidental Oil Shale Inc. (OOSI) successfully demonstrated its
modified in situ (MIS) oil shale retorting technology by conducting
large-scale field tests at its Logan Wash facility near De Beque,
Colorado. OOSI operated the Logan Wash MIS retorting facility
from 1972 until 1982 (Stevens and Zahradnik 1983). The MIS
technology developed by OOSI was proven technically feasible and
commercial projections suggest that the technology can be
profitable in the future.
One of the environmental concerns associated with in situ
processing is the impact of the process on local groundwater.
Chemical compounds potentially soluble in groundwater are
created during MIS retorting. The hot spent retorts must be
cooled and then cleaned of these water-soluble chemical
compounds to mitigate the process's impact on local groundwater.
Spent retorts were cooled and cleaned at Logan Wash by
circulating water through the retorts to remove soluble materials.
Water produced from the MIS retorts (process water) was used in
the cooling and initial stages of the cleaning. Baseline quality
groundwater collected in the mine sumps (mine water) was used in
the later stages of the cleaning. The groundwater quality from
most spent retorts at Logan Wash is restored to near baseline.
These experiments, conducted by OOSI and its contractor EMR^,
demonstrated that impact on groundwater quality from MIS
retorting can be mitigated. However, a commercial-scale
operation requires careful water management to ensure that
sufficient water is available to clean all spent retorts created.
OOSI is developing plans for demonstrating commercial-scale
oil production from a federal prototype oil shale lease (Tract C-b)
in northwestern Colorado. OOSI contracted with the Western
Research Institute (WRI) to conduct laboratory research and
analytical studies for optimum commercial-scale water
management. OOSI also contracted with EMR^ to continue field
tests of potential water management schemes at Logan Wash.
The goal of the two efforts is a cost-effective procedure for
cleaning commercial spent retorts that optimizes use of the supply
of water.
This paper discusses the MIS oil shale retorting technology
development by OOSI, the post-retorting conditions of spent MIS
retorts, the previous research conducted by OOSI and EMRv to
mitigate potential groundwater impact, the current research by
EMRx anc* WRI to develop cost-effective procedures for cleaning
commercial spent retorts, and OOSI's future plans for
commercializing MIS oil shale retorting.
Development of the MIS Oil Shale Retorting Technology
The OOSI MIS process requires that a retort be constructed
underground using explosives to fracture the oil shale and create
the permeability necessary for retorting. In order to effectively
fracture the oil shale and create permeability, a portion of the oil
133
shale in the retort is mined to provide the void volume needed for
the remaining oil shale to expand into when it is fractured with
explosives. To create a rubble bed, explosives are set and ignited
in boreholes drilled from the mined areas into unfractured oil
shale.
The top of the oil shale rubble bed is heated to Ignition
temperature using hot inert gas. When the oil shale is hot enough
for ignition, air is injected into the rubble bed to begin combustion
and retorting of the oil shale. The hot gases, produced by
combusting the residual carbon that remains after retorting, flow
downward through the rubble bed and pyrolyze the kerogen in the
oil shale ahead of the advancing combustion front. Oil from
kerogen pyrolysis and gases from both kerogen pyrolysis and oH
shale combustion are produced at the bottom of the rubble bed
(McCarthy et al. 1976; McCarthy and Cha 1976).
Eight MIS retorts were constructed and operated by OOSI at
Logan Wash (Figure 1). The first six were designed to determine
the effects of the geometry of the mined void area, explosive
fracturing tecliniques, and ignition and operating procedures on
retorting efficiency. Retorts 7 and 8, the last two MIS retorts
operated by OOSI, were commercial-scale and operated
simultaneously to simulate commercial operation (Figure 2). These
retorts were designed to demonstrate the technical feasibility of
MIS technology at a commercial scale.
Results obtained from processing Retorts 7 and 8 prove that
commercial-scale oil shale retorting using the OOSI MIS process is
technically feasible. The processing of oil shale using these retorts
confirmed that a high oil yield can be achieved in retorts with low
void volumes. Further, the results confirmed that the
straightforward retort construction and operation used in Retorts 7
and 8 can potentially achieve economic oil recovery(Stevens and
Zahradnik 1983).
Conditions that Cause MIS Groundwater Impact
A better understanding of the MIS groundwater impact
process is needed to minimize the amount of water required to
clean commercial spent retorts. The conditions existing in a MIS
retort after retorting is nearly completed areillustrated in Figure 3.
The rubble bed in the retort consists of three distinct zones: raw
unretorted oil shale, retorted oil shale, and combusted oil shale.
The residual carbon remaining after retorting wascombusted in
the top part of the bed. Unretorted oil shale underwent limited or
no thermal alteration in the bottom of the bed, and it is possible
that heavy fractions of the oil produced from retorted shale
condensed there. Between these zones, retorted oil shale
underwent thermal pyrolysis, which produced oil and gas from the
shale.
After retorting, temperature in the retort remains high. The
temperature in many parts of the combusted shale zone exceed
1500F (816C). The temperatures in the retorted and
unretorted zones are progressively cooler but can be as hot as
1000 and 500F (538 and 260C), respectively. The sides and
bottom of the rubble bed are surrounded by oil shale that was not
explosively fractured (pillars). Also, an air space or void exists at
the top of the retort (Figure 3).
Two sources for potential groundwater impact exist because
of the retort conditions when processing ceases. One source of
impact is water-soluble material remaining in the spent retort.
Another less obvious potential source is water-soluble material
OCCIDENTAL OIL SHALE
RETORT S
7MS'
UPPER INTERMEDIATE LEVEL
LOWER INTERMEDIATE LEVEL
PRODUCT LEVEL
RETORT 5
RETORT 4
78S9'
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Figure 1 . Summary of the MIS Retorts at the Logan Wash Site
134
Figure 2. Isometric View of Retorts 7 and 8
generated by the continuing kerogen pyrolysis in the pillars and
unretorted shale. This post operation pyrolysis occurs as a result
of energy or residual heat stored in the hot spent shale. A spent
MIS retort, similar to Retorts 7 or 8, contains more than 100
billion Btu of residual heat. This energy needs to be removed from
the MIS retort to minimize post retorting pyrolysis and also to
prevent heat conduction into the surrounding pillars, thereby
preventing a reduction of their mechanical strength. In addition,
the amount of energy in the form of residual heat from a
commercial operation is considerable and, if used, can significantly
improve the overall MIS thermal efficiency (Hester and Jacobson
1983).
Effective procedures to clean spent retorts must cool the
retort to preserve mine integrity, use residual heat in the spent
retort to react much of the soluble material into insoluble forms,
and provide a means by which to remove remaining water-soluble
contaminants from the retort. Experiments were conducted at
Logan Wash by OOSI and EMR^ to develop procedures to clean
spent retorts. The following section discusses the results of these
experiments.
Environmental Research Conducted using Retorts 7 and 8
The water management procedures needed for MIS
operation liave been investigated by OOSI and EMR^ since 1982
using Retorts 7 and 8. In November of 1982, a short time after
the completion of processing Retorts 7 and 8, OOSI initiated
water-quenching studies on these full size retorts. Water
quenching was initiated to accelerate the cool down of these spent
retorts. In addition, recovery of residual heat from spent retorts in
135
Raw Oil Shale/Condensed Oil
Product Level Bulkhead
Figure 3. MIS Post-Retorting Conditions
the form of combustible gases generated through steam-carbon
reactions was investigated. The water quenching research also
removed many of the potentially soluble materials from the retorts.
A quench-water flow rate of 50 gal/min into each of the two
retorts was desired but sufficient quantities of water were not
available at the Logan Wash site to maintain this flow rate in both
retorts. Consequently, quenching research concentrated on Retort
8 where the desired quench-water flowrate was maintained for
several months. Thus, Retort 8 is more thoroughly evaluated
because it has undergone more thorough quenching than Retort 7
which was quenched with less water or Retort 6 which was not
quenched.
Details regarding the results of the initial quenching of these
spent retorts in 1982 and 1983 are reported by Hester and
Jacobson (1983). These initial experiments, using process water,
confirmed that water quenching is a viable procedure by which to
cool spent retorts. Reactions of the quench water with hot
material in the spent retort produced combustible gases and clean
condensate. From 1983 through 1988, periodic water injection
into the retorts continued to examine cooling of the retortsand
material removal from the retorts.
In December 1988, OOSI and EMRX tested another
potential retort cleaning procedure called staged deluge. The
staged deluge removes soluble compounds from spent retorts by
circulating water through the rubble bed. A grid of 26 water
injection points was constructed at the top of the rubble bed by
drilling from the upper mine level (instrument air level). Roughly
170,000 gal of water were injected sequentially into each of the
injection points at a high rate of approximately 1,000 gal/min.
The water collected in the lower portion of the retort was
reinjected into the retorts. During the staged deluge, roughly
500,000 gal of water (approximately three injections) was injected
into each of the 26 injection points.
The concentrations of retort-induced constituents in the
process waters from Retort 8 decrease with time. Figure 4 shows
the concentrations of dissolved organic carbon (DOC) in the
process water as a function of time (retort completion given as July
1982). Vertical dashed lines in the figure represent periods of
quenching or staged deluge. From this figure alone, the impact of
quenching on DOC concentrations is not obvious.
DOC concentrations may also have been reduced as a result
of the staged deluge. Figure 5 shows the DOC concentrations in
process water from Retort 8 for the period January 1, 1985,
through September 21, 1989. Again, vertical dashed lines in the
figure represent the periods of quenching or staged deluge. The
dashed line on day 2334 is the start of the staged deluge. There
are periodic fluctuations in the DOC concentrations. The reasons
for these fluctuations are again not obvious, and the fluctuations
make evaluation of these data difficult. It is also difficult to
determine from this figure if the staged deluge caused the
reduction in DOC concentrations or if the reduction was a
continuation of the short-term natural cleansing trend.
However, comparisons of DOC concentrations in process
water from Retort 8 with process water from other retorts that
were not quenched (Retort 6) or were partially quenched (Retort 7)
show that both quenching and staged deluge do reduce DOC
concentrations to a certain extent. After approximately 87
months (2,610 days), the DOC concentration in process water
from Retort 6 was 175 mg/L (Figure 6). This value compares to
80 mg/L measured in process water from Retort 8 at the
corresponding time after retort completion. Likewise for process
water from Retort 7, the DOC concentration on February 27,1989 was 210 mg/L compared to 95 mg/L for Retort 8 on the
same day. Retort 7 was quenched with roughly 20% of the
amount of process water used in Retort 8.
136
Total dissolved solids (TDS) concentrations in the process
water from Retort 8 show a steady increase since the monitoring
of these concentrations began (Figure 7). During periods of
quenching, TDS concentrations temporarily increased. There is a
linear increase in TDS concentration with time. The major TDS
constituent in the process water is sulfate.
The environmental remediation research conducted by OOSI
using spent Retorts 7 and 8 lead to the following observations.
First, the quenching of spent retorts with water is effective in
reducing the temperatures in the spent retorts and, thereby,
reducing kerogen pyrolysis that occurs after retorting. The current
temperatures monitored in Retort 6, which was not quenched, are
greater than those monitored in Retorts 7 and 8 which were
shutdown much later and were quenched. In addition, the water
quenching removed much of the residual carbon from these retorts
and transported it to the surface in the form of combustible gas.
The gas can be used to supply energy that is required for the plant
operations (Hester and Jacobson 1983). Second, the
concentrations of potential organic contaminants in process water
flowing from the retorts decreases naturally with time but this
decrease can be accelerated by quenching with water. The current
DOC concentration in the process water flowing from Retort 8 is
lower than the current DOC concentrations in the process water
flowing from either Retort 7 or Retort 6 (EMRX 1989).
In August 1989, EMRX modified the staged deluge process
by using clean water for the deluge instead of recycling water from
spent retorts. More soluble constituents were removed from the
spent retort using clean deluge water than were removed using
recycled deluge water. This behavior is typical of mass transfer-
controlled processes.
In a mass transfer-controlled restoration process, the
concentration gradient between the injected waters and the area
being cleaned regulates the rate of constituent removal. In the
initial stages of restoration, the concentrations of soluble materials
in a spent retort are high, and these constituents dissolve readily in
clean water. However, as the retort is cleaned, the concentration
gradient decreases, and the rate of chemical constituent
solubilization into injected waters declines. When this occurs,
removal of the soluble materials from the retort can be increased
by injecting cleaner water to increase the concentration gradient.
The procedure of injecting clean water to decrease the amount of
time required for the final stages of groundwater restoration is
used successfully to restore groundwater from uranium solution
mining wellfields.
Examination of the data presented in Figure 4 shows that the
decline in the concentration of DOC in the process water from
Retort 8 slowed in 1989. This indicated that it was time to inject
cleaner water into the retort to accelerate the further removal of
soluble constituents. Deluges conducted in August 1989
confirmed that using clean water accelerated DOC removal.
However, the major problem with continuing to deluge Retort 8
with clean water is the limited availability of water at Logan Wash.
In January 1990, EMRX continued the staged deluge of
Retort 8 using the relatively clean water flowing into the mine
drifts at Logan Wash. The results of the first two deluges in Retort
8 using mine water were similar to the August 1989 clean water
deluges. Process water produced from these deluges was disposed
of in an evaporation pond near the Logan Wash site rather than
reinjecting it into the retorts. The results thus far show increased
removal of soluble compounds from Retort 8 using mine water in
place of process water for deluging. By using the indigenous
water at the site, the need to acquire clean water for the retort
cleaning was reduced.
In summary, the water quenching and staged deluge of Retort
8 successfully reduced the amount of time required for cleaning
spent MIS retorts. However, the time required for cleaning spent
retorts still needs to be minimized.
Current Research Activities
Currently, OOSI plans to continue pursuing
commercialization of the MIS oil shale retorting technology. The
procedure and schedules required for cleaning spent MIS retorts
need to be developed more quantitatively for commercialization.
EMRX and theWestern Research Institute (WRI) are presently
contracted to quantify the water management procedures for
cleaning the spent retorts. EMRX will continue to investigate the
cleaning of Retorts 7 and 8 at Logan Wash using the staged
deluge procedure, and WRI will conduct laboratory research to
investigate the potential benefits of other procedures that can be
applied with the quenching and deluge procedures to reduce the
time and resources required for cleaning spent retorts.
EMRX continues to deluge Retort 8 using mine water and
then discharges the produced water to the evaporation pond. At
Logan Wash however, the amount of mine water is limited, so
methods to increase the frequency and effectiveness of deluges
without using additional water will be investigated. One method to
achieve more deluges per month without requiring additional clean
137
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Quenching
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Days Si nee
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Figure 4. DOC Concentrations in Retort 8 Waters from 1983 to 1989
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Days Sine* Retort Completion
Figure 5. DOC Concentrations in Retort 8 Waters from 1985 to 1989
138
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Months Since July 1979
Figure 6. DOC Concentrations in Retort 6 Waters from 1979 to 1989
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Figure 7. TDS Concentrations in Retort 8 Waters from 1985 to 1989
139
water is to treat the deluge water to remove potential
contaminants and then reinject the treated water for another
deluge.
WRI is constructing a laboratory-scale simulator for the MIS
retort cleaning process. The objective of the simulations is to
determine a post-retort ing operating procedure for optimal water
management during the cleaning of the spent retorts. WRI will use
the experimental set-up illustrated in Figure 8 for the laboratory-
scale simulations.
Water Influx Tubas
with Thermocouples
InsirJt \ i;:^vJ fc^fl Vffl\>s'"A',':Crushed Oil Shale
Thermocouple and
ouch
ProductWater Collector
Bottom
'Water Injection
Tube
Sealed Top
Product Water
Collector Tubes
Sealed Bottom
Figure 8. MIS Groundwater Contamination Simulation
Experimental Set-up
Post-retorting conditions in spent MIS retorts will be
simulated inside an 8-inch-diameter stainless steel pipe by creating
a rectangular area (5 by 5 inch) into which a rubble bed of oil shale
can be charged. The rubble bed will be heated to ignition
temperature with inert gas and combusted with air. This
procedure is similar to the retorting procedure used at Logan
Wash. Retorting will be stopped before the rubble bed is
completely retorted. Stopping at this point will create conditions
similar to those shown in Figure 3.
After conditions in spent retorts are simulated, procedures to
accelerate retort clean-up without using largevolumes of water will
be investigated. Sample pouches will be located in the bed. These
pouches will be constructed of stainless steel screen, and a
thermocouple will be inserted in each pouch to provide a
temperature history of the experiment on the sample.These
samples will be used to determine the amount of water-soluble
constituents in the spent shale and the rehydration characteristics
of the spent shale. The simulator will have ports for water
injection to simulate water influx, quenching, and deluge. The
outlets at the bottom of the simulation retort will be similar in
design to Retorts 7 and 8 at Logan Wash. The total organic
concentration of injected and produced waters will be determined
to evaluate the success of different spent retort cleaning
procedures.
In addition, a larger simulation of the best post-retorting
operating procedure will be conducted using WRI's 10-ton retort.
The procedure for the 10-ton retort will be similar to that used in
the laboratory.
The results from EMRX field testing at Logan Wash and
results from WRI simulations will be used to develop a
comprehensive plan for cleaning commercial spent MIS retorts.
Future Plans
The OOSI long-term plan is to commercialize MIS retorting.
Negotiations are in progress to solicit U.S. Department of Energy
participation in construction and operation of a 1200 bbl/day
proof-of-concept oil shale facility at Tract C-b (the project). The
project will be designed to improve commercial economics by
maximizing total resource use. The oil shale mined to construct
MIS retorts will be burned in a circulating fluidized-bed combustor
(CFBC) to generate electric power. The CFBC will be co-fired
with MIS off gas, oil shale and coal to provide electrical power and
steam for the project and also for export power to local
consumers. The co-firing with oil shale, because of its alkaline
mineral content, will control sulfur emissions from the power-
generating plant. In addition, the CFBC can use the combustible
gas generated from quenching of spent retorts to improve the
overall plant efficiency.
The project construction will require three years, and plans
are to operate the facility for seven years. MIS retort construction
and operation procedures will be similar those of Retorts 7 and 8
at Logan Wash. Plans are to simultaneously operate two MIS
retorts. In addition, the spent retort cleaning procedure resulting
from the work of EMRj^ and WRI will be tested. Experience
gained from the continuous operation over the seven-year period
will be used to design and construct a 23,000 bbl/day commercial
plant on Tract C-b (Bechtel 1989).
140
The demonstration of an integrated commercial-scale MIS oil
shale retorting facility will provide the United States with a
commercially proven and environmentally acceptable technology
to reduce dependence on foreign oil supplies beyond the year
2000. It is imperative that such technologies be developed by the
time world oil reserves significantly decline.
SUMMARY
In summary, the efforts of OOSI from 1972 to 1982 to
develop a commercial technology for producing oil from oil shale
resources in the western United States resulted in the MIS oil shale
retorting process. This process was proven technically feasible on
a large scale and is also simple and straightforward. After 1982,
OOSI and its contractor EMRj^ continued to pursue development
of the MIS technology by conducting research both to optimize the
process's resource recovery and to minimize the process's
environmental impact. The results suggest that resource recovery
and overall economics can be improved by using the oil shale
mined during the construction of the MIS retorts as a fuel for
electric power generation. Also, the residual heat contained in a
spent MIS retort can be used to generate clean combustible gas for
use as fuel. In addition, cleaning of several of the spent MIS
retorts was achieved. However, a reduction in the time and effort
required for completely cleaning spent MIS retorts will improve the
commercial economics of the process.
OOSI plans to continue efforts to commercialize the MIS
technology by constructing a 1200 bbl/day proof-of-concept
engineering scale demonstration plant. In support of this
objective, EMR^ and WRI are working together to develop
cleaning procedures for spent MIS retorts that are cost effective,
easy to implement and minimize environmental impact.
REFERENCES
Bechtel, Inc., 1989, Western States Oil Shale Recovery
Program, Bechtel Job Number 20227-000.
EMRX Corporation, 1989, Retort Staged Deluge
Progress Report, Through October 15, 1989.
Unpublished report submitted to Occidental Oil
Shale, Inc.
Hester, N.E., and C. Jacobson, 1983, The Utilization
of Residual Heat in Spent MIS Retorts for
Wastewater Treatment and Process
Improvements. Proceedings of the 16th Oil Shale
Symposium, Golden, CO. pp 487-497.
McCarthy, HE., C.Y. Cha, W.J. Bartel, and RS.
Borton, 1976, Development of the Modified In
Situ Oil Shale Process. AIChE Symposium Series,
v72, No. 155, pp 14.
McCarthy, H.E., and C.Y. Cha, 1976, Modified In Situ
Oil Shale Process Development and Update.
Proceeding of the 9th Oil Shale Symposium,
Golden, CO. pp 85-100.
Stevens, A.L., and R.L. Zahradnik, 1983, Results from
the Simultaneous Processing of Modified In Situ
Retorts 7 & 8. Proceeding of the 16th Oil Shale
Symposium, Golden, CO. pp 267-280.
141