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Page 1: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India

Chapter 6.0: Cause Effect Analysis & Chapter 6.0: Cause Effect Analysis & Generating GP options Generating GP options

66..00 CCAAUUSSEE EEFFFFEECCTT AANNAALLYYSSIISS && GGPP OOPPTTIIOONNSS The cause effect analysis was carried out of all the identified waste streams/problem areas. Following are the waste streams/problem areas for which cause effect analysis was carried out:

Waste Stream-1 : Oil loss in DOC Waste Stream-2 : Oil loss in Refinery Waste Stream-3 : Hexane loss in Solvent Extraction Plant Waste Stream-4 : Waste water generation & its treatment Waste Stream-5 : Energy loss Waste Stream-6 : Inadequate steam generation leading to high oil &

hexane loss Waste Stream-7 : Inadequate Air Pollution Control Devices (APCD) Waste Stream-8 : Improper material handling & house keeping practices

The objectives of cause effect analysis were to generate Green Productivity options for reduction/elimination of waste streams and evolve solutions for problem areas for generating Green Productivity options. For this purpose appropriate tools and techniques such as Fishbone Diagram (Ishikawa Diagram), Eco-mapping, brainstorming etc. were used. The detail of the cause effect analysis is presented below for all the waste streams & problem areas. 66..11 OOIILL LLOOSSSS IINN DDOOCC ((HHIIGGHH RREESSIIDDUUAALL OOIILL CCOONNTTEENNTT IINN DDOOCC)) 6.1.1 (A) General observations & present practices Out of the 19.75% oil content in the seed, an average of 18.57% oil is extracted and the remaining is lost and goes along with DOC, i.e. an extraction efficiency of about 94%. The loss of oil is due to combined effect of several causes at various process stages, each one having some effect on oil extraction efficiency. The residual oil content in DOC varies from 0.7% to 1.5%. The average residual oil content in RPL is 1.18% as compared to 0.5% in Japan. In India, there is no established benchmark for oil loss in DOC.

National Productivity Council, New Delhi (India) Page:6. 1

Page 2: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India

This oil loss of 1.18% (out of 19.75% oil content in seed) amounts to about 990 tones of oil loss per year. A 10% reduction in this oil loss would save about 99 T/year amounting to about Rs.21.8 lakh/year. Calculation: Seed Processed = 300 TPD = 1,00,000 T/yr Average oil content in seed = 19.75% Average oil extracted from seed = 18.57% Crude oil production = 18,000 T/yr Cost of crude oil = Rs.22, 000/T DOC Production = 83,000 T/yr Cost of DOC = Rs. 7,000/T Cost of waste stream: Oil loss in DOC = 1.18% (goes with DOC) 10% reduction in oil loss in DOC = 99 T oil/yr [10%x1.18%X1, 00, 000 T/yr seedx84%] Saving potential 99 t @ Rs 22/kg) = Rs. 21.8 lakh/year (B) Concerned process steps: PREPARATORY: Cracker Cooker Flaker SEP: Extractor DTDC (C) Environmental pollution problem:

This does not contribute direct environmental pollution problem. But the productivity of the organization goes down in the form of loss of product. 6.1.2 Cause effect analysis The various tools for the identification of the causes of oil loss in DOC have been applied. In line with identification of causes & their effect, a fish bone diagram-(Isikawa Diagram) was prepared showing causes of total oil loss with respect to man, machine, material, methods and environment and is presented in Figure-6.1.

National Productivity Council, New Delhi (India) Page:6. 2

Page 3: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India

Figure-6.1: Fishbone Diagr

Inadequate Temp

No proper working Instruction

Considering average thickness instead of standard deviation

Faulty quality control of flake thickness

Thick flaking

Faulty bleaching Process

Combined degumming & Neutralisation

Poor maintenance of pumps & glands

Improper Cleaning of seed

Imof

Im

No proper record keepin

Method Excess additionNo proper working

Instruction

Poor splitting Inadequate oil separation

Less residence time

High oil presence in wastewater

Inadequate ETP

Non Compliance

Environment Less Vacuum

Inadequate steam supply i

Absence of flow m

Machine

ImpropPoor Maintena

Improper craHigh residual oil in DOC

cking Presence of ston

Worn Out rollerInadequate Capacity

Less heating surface area for indirect steam

Improper addition of Wearing off of oil seal

Improper Flaker Insufficient Residence time

Worn out rollers Leakage from oil handling pumps

Caustic

Improper Cooker

National Productivity Council, New Delh

am d

prope Caus

propeg

Faulty f

Am

of wa

n SEP

eter

Le

er Exnce

e s

i (Indi

epicting Soy Oil loss

Unskilled labour

Power interruption

High residual oil Improper seed preparation

in DOC

Poor quality of bleaching earth

Excess use of bleaching earth r addition

tic

Distribution loss

Improper steam supplyInadequate Boiler capacity

Damaged seed

Green seed

High moisture content

Material

Poor quality of seeExcess foreign matter

d r seed preparation Inadequate Cracking & Flaking

Inadequate cooking

low meter

bsence of flow meter & instant easurement of FFA

ter

Inadequate spray of hexane ss drainage time for miscella

Excess water additionFaulty water flow meter

Mind set

Inadequate training

Improper house keeping Man

tractor

Oil Loss

a) Page:6. 3

Page 4: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Causes for oil loss in DOC: Various causes identified for the oil loss in DOC are summarized below:

1. Less efficient Cracking: wide variation in seed size and there is no grading of seed, worn out Roller, stone in seed

2. Inadequate Cooking: small size of cooker, less heating surface 3. Less efficient Flaking: worn out Roller, inadequate Cracking & Cooking 4. Less efficient Extraction: low drainage time, improper hexane spray,

inadequate Cracking, Cooking & Flaking The details of the causes are discussed subsequently: 6.1.2.1 Cause: Less Efficient Cracking Best practices: The best practice of cracking recommends that the cleaned seed should be cracked by shear action to 4 - 6 pieces. There should not be any whole grain seed. This enables the seed for proper cooking & flaking. Inefficient cooking & flaking results in high oil content in DOC. Field study data:

Cracking: Cleaned Seed

Escaped seedEscaped seed

Cracked seed along withWhole seed

Percentage size distribution of cracked seed

Whole Seed29%

Half Seed34%

< Half Seed37%

Whole Seed Half Seed < Half Seed

Figure-6.2 Seed cracking & size distribution of cracked seeds

National Productivity Council, New Delhi (India) Page:6. 4

Page 5: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India The cleaned seed is passed through cracker to break the seed into four to six pieces. A representative sample was collected at the inlet of the flaker and sieved to separate whole seeds, half seeds and less than half seeds to find out the cracking efficiency of the cracker. The seed cracking & size distribution of cracked seed is given at Figure-6.2. The percentages of whole and half seed are very high. The reasons for inefficient cracking was attributed to the following:

• There is large variation in seed sizes • The rollers were found to be damaged by way of pitting of surfaces as well

as blunting of cutting edges. This is due to presence of stone in the seed and excess use of the existing rollers.

Conduction of trials: The trials were conducted to establish the relation between whole bean content in crushed bean & thickness of flake and between thickness of flake and extraction yield. The trial results are given below: Trial: Relationship between whole bean content in crushed bean and

thickness of flake Higher content of thick flakes brought about higher remaining oil content and the large amount of whole bean in crushed soybean led to higher content of thick flakes. This relationship was determined quantitatively as shown in Table 6.1

Table-6.1 : Relationship between whole bean content and flake thickness

Seed Cracker

No.1 No.2

Clearance of crushing roller

Ordinary Narrow Ordinary Narrow

Whole bean after Cracker 8.1% 3.3% 5.4% 3.2%

Flakes Clearance Ordinary Ordinary Ordinary Ordinary

Thickness of flake Average

0.39mm 0.36mm 0.38mm 0.35mm

>0.35mm 80% 68% 82% 60%

>0.40mm 54% 30% 50% 25%

>0.45mm 9% 0% 4% 0%

National Productivity Council, New Delhi (India) Page:6. 5

Page 6: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Trial: Relationship between thickness of flake and extraction yield Soybean flakes were separated into two portions i.e.(<0.35mm and >0.35mm thickness) by hand and extracted with hexane for 90 min. in laboratory.

Table 6.2: Relationship between flake thickness and oil yield

Thickness of flakes

Oil yield Difference

<0.35mm 19.42% >0.35mm 19.25%

0.17%

The results shown in Table 6.1 & 6.2 indicate that it is very important for low oil content in DOC to decrease the whole soybean contained in crushed bean and to keep the uniform thickness of flakes (0.33-0.37). Observations: Based on the above analysis, it was identified that the existing cracking efficiency was lower. The identified reasons are summarized below:

(i) Wide variation in seed size and no grading of seed (ii) Worn out roller (iii) Presence of stone in the seeds

Effects: Inefficient cracking leads to higher percentage of off-sized cracked seed (powder or hole seed content) adversely affecting further process steps such as cooking and flaking and ultimately oil extraction. GP option evolved: To minimize the adverse effect due to less efficient cracking, following GP options were evolved:

1. Installation of Seed grader with conveyance system for the grading of seed before cracking.

2. Replacement of worn-out roller of the cracker. 3. Putting in operation the existing de-stoner equipment.

National Productivity Council, New Delhi (India) Page:6. 6

Page 7: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India 6.1.2.2 Cause – Inadequate Cooking Best practices: As reported by management, the best practices of cooking recommend following controlled parameters for adequate cooking of seeds. Temperature during cooking - 800C Residence time in the Cooker - 45 to 60 minutes Moisture in the cooked seed - max. 10% Field study data: Cooking of cracked seeds before flaking is required to plasticise the kernel particles. Plasticity is essential to produce optimum thick flakes. It has been observed that the residence time available in the cooker was only 15-20 minutes, which is less than the desired value of 45-60 minutes. The heating surface area of the cooker was found to be inadequate. The temperature of the cooker is maintained through direct steam as well as indirect steam. There is no temperature gauge installed to control the temperature inside the cooker. The inadequate cooking in the cooker leads to poor flaking and extraction of oil and finally contribute in increasing the oil content in DOC The details of the study to identify the causes of inadequate cooking is given below:

1. Presently a sample is drawn into a polyethylene bag in which thermometer is inserted to measure temperature which is done generally two hourly.

2. As there is no temperature gauge installed, a continuous controlled

temperature cannot be ensured at all time. A thermo-couple installed on the cooker frequently comes under maintenance due to dust deposition, which leads to erroneous reading, and therefore it has been taken out.

As regards to maintaining requisite moisture percentage direct steam is supplied into the cooker, which (in addition to increasing moisture percentage) contributes in cooking purpose. The indirect steam also contributes in cooking. At times when moisture percentage in seeds is higher, addition of direct steam would increase further moisture beyond desirable limit. To avoid the same, the direct steam supply needs to be reduced. But this leads to inadequate cooking of the material because indirect heating alone is not sufficient to raise the temperature to the desired extent. In such cases, the residence time needs to be increased or feed rate needs to be reduced.

National Productivity Council, New Delhi (India) Page:6. 7

Page 8: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Observation: Keeping specially the situation in higher moisture seed, limiting direct steam, as the present heat transfer area of indirect steam pipe is inadequate and to improve the cooking, the heat transfer area of indirect steam pipe has to be increased. Effects: Inadequate cooking has adverse effect in terms of improper flaking due to inadequate plasticity, which ultimately affects in terms of oil loss. GP option evolved: To minimize the adverse effect due to inadequate cooking, following GP options were evolved:

1. Increase the heating surface area in the cooker by adding more steam pipes (limpets)

2. Install a new cooker of requisite size. 6.1.2.3 Cause: Less efficient flaking Best practices: The best practices of flaking recommend that the thickness of flakes vary between 0.33mm to 0.37mm. Flake thickness more than 0.37mm leads to high oil content in DOC. Thinner flakes (less than 0.33mm thickness) generate more sediments and inhibits during extraction which is carried out by spraying hexane over the flakes in the extractor. Field study data: The flakers in the preparatory section have been examined and found that uneven roller gap in one of the flakers results in the thicker flakes. The rest of the flakers required proper maintenance. The roller gap has to make uniform for uniform flake thickness. Thicker flake leads to high oil content in DOC. The diagram given below shows the details:

Flaking: Cracked & Conditioned Seed

Flakes

National Productivity Council, New Delhi (India) Page:6. 8

Page 9: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India

The conditioned cracked seed passes through the flaker to produce flakes. The optimum thickness of the flakes is 0.33mm- 0.37mm. To find out the uniformity of flakes produced by flaker, the samples were collected and measured for the flakes thickness distribution. The measured variation in flake thickness and percentage distribution of flakes thickness is given at Figure 6.3.

% in total17%13%

Flake thickness range

58%

0.25-0.320.33-0.370.38-0.43>0.43 12%

Percentage Distribution of Flake thickness

0.25-0.32 mm17%> 0.43 mm

12%

0.33-0.37 mm13%

0.38-0.43 mm58%

0.25-0.32 0.33-0.37 0.38-0.43 > 0.43

0. 39

0. 29

0. 4

0. 25

0. 45

0. 4

0. 36

0. 41

0. 38

0. 31

0. 36

0. 30. 29

0. 340. 35

0. 410. 4

0. 30. 28

0. 31

0. 59

0. 44

0. 36

0. 45

0. 4 0. 4 0. 4

0. 3

0. 4 0. 4 0. 40. 380. 38

0. 44

0. 410. 4

0. 35

0. 4 0. 4 0. 40. 38

0. 420. 4

0. 5

0. 37

0. 40. 39

0. 31

0. 390. 410. 4

0. 35

0. 3

0. 47

0. 4 0. 41

0. 38

0. 420. 42

0. 380. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 3830. 383

1 4 7 10 13 16 19 22 25 28 31 34 37 40 43 46 49 52 55 58

sa m p le n o .

Thic

knes

s of

the

flake

Ser i es 1 Ser i es 3 Ser i es 4 Ser i es 2

0

0 .1

0 .2

0 .3

0 .4

0 .5

0 .6

0 .7

Figure-6.3: Measured variation in thickness of flakes & percentage distribution The average of the flakes have been found to be 0.38 mm-0.43mm thick. The percentage of thick flakes (>0.38mm) is as high as 70% which is undesirable for proper extraction in extractor, resulting high residual oil content in DOC. The capillary paths must be short so that the distance over which diffusion occurs is as short as possible. These thick flakes are causing high residual oil (1.2%) in DOC against the achievable 0.7-0.9% residual oil.

National Productivity Council, New Delhi (India) Page:6. 9

Page 10: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India The unit had already made some attempts to bring down this residual oil level to <1.2% but it yielded poor quality of oil with impurities like phosphetides. This has occurred due to the excessive extraction of oil from the flakes, which are having optimum thickness of (0.33-0.37mm). The residual oil of 1.2% is the average content in DOC. Among the DOC, residual oil varies from 0.5% to >2.5% depending upon the thickness of the flakes. It was observed that flakes produced from the centre of the flaker are comparatively thicker than flakes produced from the ends. This is due to excessive wear occurring at the centre compared to the ends because of more material passing through the centre. Moreover every day 7.83 tons of foreign matter (1.82% of raw material) passes through the flaker. The foreign material mostly silica related only, is abrasive. Excessive wear at the centre

FLAKER ROLLS

FLAKER ROLLS

Figure-6.4: Uneven gap between rollers affecting efficiency of Flaker Observations: Based on the above analysis and study, it was identified that the flaking is inefficient. The identified reasons are summarized below:

i) Worn-out flaker roller ii) Inadequate cracking and cooking

Effects: It is clear that there is direct relationship between flake thickness & residual oil content in DOC. As the thickness of the flake increases, oil content in DOC increases. GP option evolved: To minimize the adverse effect due to high thickness of flakes, following GP options were evolved:

a) Repair worn-out roller of the flaker b) Replace irreparable roller of the flaker.

National Productivity Council, New Delhi (India) Page:6. 10

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Report on GPDP Project in an Edible Oil Industry in India 6.1.2.4 Cause: Less efficient extraction Best practices: The best practices of extraction recommend that the spray of hexane should be done uniformly over larger surface area of flakes/collets. The residence time in the extractor should be between 1.5 hrs to 2.5 hrs. There should adequate drainage time to drain out Miscella from wet DOC. Field study data: It has been observed that the existing hexane spray system does not provide uniform quantity of hexane spray over the flakes/collets. There are no baffles to divert the flow of hexane at different angles to reach over maximum surface area of flakes/collets. It needs modification. Also, only two baskets are kept for draining the Miscella from wet DOC. It has been observed that the hexane concentration in wet DOC is more due to less drainage time. This helps in carrying oil along with DOC and result in high oil content in DOC. In addition, high concentration of hexane in wet DOC leads to high load on desolventisation process in DTDC. Observations: Based on the above study, it was identified that the extraction efficiency was poor due to following reasons:

i) Low drainage time in the extractor ii) Inefficient hexane spray system

Effects: Poor extraction leads to high residual oil content in DOC. GP option evolved: To increase the extraction efficiency, following GP options were evolved:

a) Increase the hexane drainage time in Extractor b) Improve the hexane spray system

National Productivity Council, New Delhi (India) Page:6. 11

Page 12: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India

66..22 OOIILL LLOOSSSS IINN RREEFFIINNEERRYY 6.2.1 (A) General observations & present practices The unit is processing 30,000 Ton crude oil in a year. The average refinery losses are 7%. The oil loss results in low yield of refined oil, high pollution load to the ETP and generation of low cost by-product like soap stock. There is room for improvement and even by reduction of 0.35% in present losses may lead to saving of Rs. 23.1 lakh per annum. The details are discussed as below: Average Crude Oil processed = 100 TPD = 30,000 T/yr Average Refined Oil production = 93 TPD = 27,900 T/yr Cost of waste stream: Oil loss in Refinery = 7% of the crude oil processed 0.35% reduction in oil loss in Refinery = 105 T oil/yr [0.35% X30,000 T/yr oil] Saving potential 105 T @ Rs 22/kg) = Rs. 23.1 lakh/year (B) Concerned process steps:

SHORT-MIX PLANT DEGUMMING & NEUTRALISATION BLEACHER BLEACHING DE-ODORISER DE-ODORISATION

(C) Environmental pollution problem: This is the major area of environmental pollution. The wastewater from the short-mix plant, spent bleaching earth from bleacher and odiferous compond come out from the de-odoriser are the major water, solid and air pollution. 6.2.2 Cause effect analysis The various tools for the identification of the causes of oil loss in Refinery have been applied. In line with identification of causes & their effect, a fish bone diagram was prepared showing causes of total oil loss with respect to man, machine, material, methods & environment and has already been explained in Figure-6.1.

National Productivity Council, New Delhi (India) Page:6. 12

Page 13: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Causes for oil loss in refinery: The various causes identified for the oil loss in Refinery are summarized as under:

1. Excess water addition in hydration & neutralization: faulty Flow Meter 2. Absence of one washing separator 3. Possibilities of excess caustic addition in neutralization: no Flow Meter,

manual dosing, excess Saponification 4. Use of low grade bleaching earth: high oil carry over (in spent bleaching

earth.), possibilities of color reversal 5. Improper bleaching earth addition: addition of powder in place of slurry 6. Oil leakage from pump: worn out seal

The details of the causes are discussed subsequently. 6.2.2.1 Cause: Excess water addition in hydration & Neutralisation Best practices: The best practice of water addition for degumming is quantity of water (in %) should be in equal proportion to the percentage of gum present in the crude oil. Similarly, the water is required for the Caustic Preparation depends on the concentration required to neutralize the Free Fatty Acid. In addition, water is used for flushing of separator. Observations & field study data: The hot water is mixed with the oil for hydrolysis of gum and subsequently separation in the separator. The quantity of water should be equal to the quantity of gum present in the crude oil. However, due to faulty water meter/ flow meter, the water addition was found to be at higher rate. The monitoring results are tabulated below: Location of water

flow meters Water flow rate as

per flow meters (lit. per hour)

Measured water flow rate

(lit. per hour)

Water saving after calibration

(lit. per day) Before Hydration Tank-1

122 130 192

Before Hydration Tank-2

88 267 3,580

For flushing water at separator-2

155 360 4,920

For flushing water at separator-4

170 410 5,760

TOTAL 14,452

National Productivity Council, New Delhi (India) Page:6. 13

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Report on GPDP Project in an Edible Oil Industry in India Estimated total water saving = 14.0 m3/day (approx.) = 4,200 m3/annum The reaction of water with oil & fats i.e. hydrolysis of oil & fats is given below:

NaOH & Water Tri-glyceride Di-glyceride +FFA

Heat

Hydrolysis of Fats & oil EFFECTS: Excess water addition hydrolyses the oil and forms emulsion and reduces concentration of soap stock, leading to excess refinery oil loss and generation of excess wastewater. GP option evolved: To minimize the adverse effect due to excess water addition, following GP options were evolved:

a) The existing water flow meter should be rectified/ calibrated to give accurate reading

6.2.2.2 Cause: Absence of one washing separator Best practices: As per the recommendation of ALFA Level (Supplier of Short-Mix Plant), the degumming, neutralization & washing Operations should be carried out in three different separators. There are two sets of separators. Therefore, for 100TPD production, the total number of separators should be 6. But in RPL, there are only 5 separators. The present practice is degumming & Neutralisation operations are carried out in one separator and two separators are use at a time for degumming & Neutralisation. But for washing only one separator is used. Therefore, there is high load on the washing separators and it affects the quality of neutral oil and results in refinery loss. Observations & field study data: The analysis results of TFM concentration in wastewater indicate that there is problem in washing of neutral oil through single separator instead of recommended two separators. To explore possibilities of reducing oil loss, trials were conducted.

National Productivity Council, New Delhi (India) Page:6. 14

Page 15: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Trials: The wash water quality and characteristics at different flow rates /processing of oil through the existing washing separator have been monitored & analysed. The results are discussed below: Case (I): Oil Flow rate : 5000 litres/hr Wash water quantity: 1205 l/h Characteristics of wash water: pH - 11.1 COD - 58,500 mg/l TFM - 1.36% FFA - 52.12% Case (II): Oil Flow rate : 2500 litres/hr i.e. at 50% Wash water quantity: 1200 l/h Characteristics of wash water: pH - 10.4 COD - 14,700 mg/l TFM - 0.32% FFA - 24.01% Case (I): Water required for processing of oil at 5000 litres/hr = 1205 litres/hr Total TFM loss = 16.39 litres/hr Case (II): Water required for processing of oil at 2500 litres/hr = 2400 litres/hr Total TFM loss = 7.68 litres/hr Therefore, total difference in TFM loss due to single washing separator is 113% i.e. 174 litres/day. Effects: • Wastewater difficult to treat because of the presence of hydrated soluble gums. • More oil loss in refinery. GP option evolved: To minimize the adverse effect due to lack of one washing separator, following GP options were evolved:

a) Use of 2 Washing Separators in place of one. b) Separate degumming and Neutralisation.

National Productivity Council, New Delhi (India) Page:6. 15

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Report on GPDP Project in an Edible Oil Industry in India 6.2.2.3 Cause: Possibilities of excess caustic addition in

Neutralisation Best practices: To neutralize the Free Fatty Acid (FFA) present in the crude oil, caustic lye at 16 to 20 degree Boumen is added. The quantity of caustic solution addition depends on the quantity of FFA present in the crude oil. About 20% excess caustic is added for effective neutralization of FFA and reduction of color. Observations & field study data: There is no flow meter installed to know the quantity of caustic being added. It is judged by checking pH, which indicates that the solution has come to the alkaline range only. But how much excess caustic has been added, is still unknown to the operator. Effects: The excess alkali saphonify the neutral oil and leads to more refining loss. It generates lower cost soap-stock, which consume more Sulphuric acid for acid oil production and generates more acidic wastewater. Thus resulting more pollution. This also results in the wastage of raw material, adding to the cost of production. GP option evolved: To minimize the adverse effect due to excess caustic addition, following GP option was evolved: a) Installation of automatic caustic dosing system 6.2.2.4 Cause: Use of low grade bleaching earth BEST PRACTICES: The bleaching earth is used to reduce the colour to the desired level. There should not be problem of colour reversal and retain lesser oil in the spent bleaching earth. OBSERVATIONS & FIELD STUDY DATA: The unit is using Indian earth during season (i.e. from October to March). As per the management opinion, during this time, the color of the oil is not permanent & it is easily come down to desired level through Indian earth.

National Productivity Council, New Delhi (India) Page:6. 16

Page 17: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Whereas, during off season (i.e. from April to September), the unit is using Tonsil to reduced the permanent colour up to desired level. The unit is facing color reversal problem from the market. Therefore, the APO-Oil Expert suggested using Tonsil in place of local Indian Bleaching Earth for better stability of oil. Characteristics & cost of different bleaching earth: a) Indian Earth:

• Bleaching efficiency = 65- 70% • Cost = Rs. 18,000/- per ton. • Oil content in spent bleaching earth = 22 to 25% • Consumption of bleaching earth = 6 kg/T of oil

b) Tonsil: Bleaching efficiency = 75%

• Cost = Rs. 30,000/- per ton. • Oil content in spent bleaching earth = 19 to 20% • Consumption of bleaching earth = 6 kg/T of oil

Effects: The local bleaching earth does not give stability to the colour of refined oil. Further, the efficiency of colour removal is not effective. GP option evolved: To minimize the adverse effect due to the use of local (Indian) bleaching earth, following GP options were evolved: a) Use of Tonsil in place of Local (Indian) bleaching earth. 6.2.2.5 Cause: Improper bleaching earth addition Best practices: The bleaching earth should be added in slurry form instead of powder. The slurry should be prepared with the neutral oil to be bleached separately and mixed into the bleacher.

National Productivity Council, New Delhi (India) Page:6. 17

Page 18: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India Observations & field study data: The bleaching earth is dosed through hopper into the bleacher. The dosing is adjusted based on the flow rate & color of oil, quality of bleaching earth. The bleaching earth freely falls on the surface of the oil in the bleacher. Effects: The fine powder of bleaching earth is being sucked during charging into the bleacher over the oil surface due to vacuum in the system. This is a loss of bleaching earth. The mixing of powdered bleaching earth is not uniform results in ineffective bleaching of neutral oil. GP option evolved: To minimize the adverse effect due to wrong method of bleaching earth addition, following GP options were evolved:

a) Addition of bleaching earth slurry in place of powder. b) Lowering the pipe and dip in the oil.

6.2.2.6 Cause: Oil leakage from pump Best practices: The oil is transferred at various stages by means of pumps. The seal of the pumps should be properly maintained so that there should not be any spillage/leakage from the pump gland. Observations & field study data: It has been found that the gland seal of transfer pump transferring crude oil, neutral oil, bleached oil and refined oil were faulty. It was not replaced/maintained for the long time resulting in the leakage of oil through gland seal. Effects: The oil leakage results in a low yield of refined oil. It creates major pollution load in the wastewater once it mixed into the waste streams. Further, it is the loss of resources. GP option evolved: To minimize the adverse effect due to oil leakage from pump, following GP options were evolved: a) Preventive maintenance of gland seal & timely replacement

National Productivity Council, New Delhi (India) Page:6. 18

Page 19: Fish Bone Diagram

Report on GPDP Project in an Edible Oil Industry in India 66..33 HHEEXXAANNEE LLOOSSSS IINN SSEEPP

♦ ♦ ♦ ♦ ♦

6.3.1 (A) General observations & present practices The hexane is used as a solvent for the extraction of oil. On an average, specific hexane loss/ consumption is in the range of 4.93 (3.64- 5.4) litres per ton of seed processed compared to 1.0 to 1.5 litres per ton in Japan. The hexane loss is due to following points:

Carry over along with crude oil Uncondensed vapor going through final vent of recuperation unit Carry over with meal drying air in Meal Dryer Carry over with DOC Hexane loss from Leakage

Carryover along with Crude oil: Stripping is the final step in separating the hexane from Miscella and is carried at 1200C and 380 mm Hg vacuum. The desired vacuum is 450mmHg. Live steam is also sparged. It was estimated that hexane loss through crude oil accounts for 2-3% of total losses. Uncondensed vapor going through final vent of recuperation unit: Wet DOC entering into the DTDC contains approximately 30-40% solvent. Since wet DOC has less draining time available in extractor, the solvent content in DOC is high. Only two hoppers are provided to collect the solvent draining from wet DOC by gravity. Sufficient draining time curtails desolventisation load on DTDC. Uncondensed vapour loss through final vent accounts for 10-12% of total loss. This is due to the inefficiency of condensers. In addition to this, air ingress takes place from the DOC outlet due to lack of rotary valve at DOC outlet. This leads to lower condensation temperature at which solvent does not condense.

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Cooler

Dryer

Desolventiser

Toaster

Wet DOC Solvent Vapor

Air inletAir outlet

Scerewconveyor fortranferof DOC

Air ingress

Figure- 6.5: DTDC stages Recuperation system is provided to absorb the uncondensed vapour before going to the final vent. The system contains mineral oil in closed system, which absorbs uncondensed vapour and release upon heating the recovery system. Due to fluctuation in the steam supply and insufficient heating surface available for solvent release from absorbing oil in recovery system, hexane concentration increases in the mineral oil and, therefore, mineral oil does not absorb uncondensed vapour efficiently. Carryover with meal drying air in Meal Dryer: There is 70%-80% of total hexane loss in meal drying section. This is due to the incomplete desolventisation of DOC in desolventisation section. In most of the plants, which have reduced their hexane loss to 1-1.5 lit/ton, a counter current DTDC with four desolventisation trays and four toasting trays, has been provided. Steam is given from the bottom of the section and it travels towards the upper section where the DOC falls from top to bottom. Heat is transferred efficiently from the steam to meal. In lower trays, steam loses temperature by supplying its specific heat to the final traces of solvent contained by meal and in the upper tray steam condenses to give its latent heat to the meal to vaporise the solvent. In this unit DTDC contains only two desolventisation trays and two toasting trays. Steam is supplied at the bottom of the two toasting sections through a 50mm perforated coil placed at the circumference of the tray, and passes to the upper trays through the meal outlets. Since the DTDC is inadequately designed desolventisation remains incomplete and the residual hexane is being carried over to the dryer section where it is being exposed to large quantity of air/ hot air. The residual hexane carried by the air is impossible to recover.

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Meal outlet

Sparge Ste

Meal Outlet

Figure-6.6: Internal arrangement of DTDC

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Sparge steam coil

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Report on GPDP Project in an Edible Oil Industry in India Carryover with DOC: Hexane carried over with DOC is estimated to be 5-7% of the total hexane loss. The DOC contains average residual oil content of 1.18%, which also contains some hexane. This adds to the problem of incomplete desolventisation. Improving the process conditions in desolventisation section can bring down the entrapped solvent percentage in DOC. Hexane loss (emission) from Leakage The poor maintenance of the extractor gear box and DTDC shaft leads to leakage of hexane from the system. Though the concentration is negligible but smell of hexane from the gearbox of extractor and DTDC shaft has been observed. Field data Reported hexane loss = 4.93 lit/T of seed During season (Oct-March)= 3.64 lit/T (continuous operation, less interruption.) Off season (April-Sep.) = 5.40 lit/T (non continuous operation, more interruption) Best figure for hexane loss = 1.0 to 1.5 lit/t of seed (Japan) Cost of waste stream: 10% reduction = 0.49% (4.93 lit/T 4.43 lit/T) = 49300 lit/yr Saving potential = 9.4 lakh per year (0.49 lit//Tx1 lakh T/yr @ Rs. 19 per lit.) (B) Concerned process steps: PREPARATORY : Cracker Cooker Flaker SEP : Extractor DTDC (C) Environmental pollution problem: The fugitive hexane emission generates air pollution. Also, excess concentration of hexane in the air may lead to fire hazard.

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6.1.3 Cause effect analysis The various tools for the identification of the causes of oil loss in DOC have been applied. In line with identification of causes & their effects, a fish bone diagram was prepared showing causes of hexane loss with respect to man, machine, material, methods and environment and is presented in Figure-6.7. Causes for hexane loss: 1. Inadequate vacuum in DTDC & distillation: inadequate steam, inadequate cooling

& condenser 2. Inadequate de-solventisation in DTDC: inadequate steam, inadequate heating

surface area 3. Inadequate drainage in extractor: inadequate drainage time, higher hexane

concentration in wet DOC 4. Inadequate recuperation: inadequate absorption/release of hexane 5. Inadequate crude oil stripping: inadequate steam & vacuum, inadequate

condenser size. The details of the causes are discussed subsequently: 6.3.2.1 Main Cause: Inadequate vacuum in DTDC & distillation Best practices: The vacuum in DTDC & distillation is required for efficient separation of hexane from the DOC & crude oil respectively. The desired vacuum should be 5 to 10mm/wc. The constant and uniform steam supply is required for better performance of SEP. Field study data: Presently, vacuum in system is 380 mmHg at stripper condenser against desired vacuum of 450 mmHg. There is fluctuation of steam due to power interruption and poor performance of Boiler. Previous year, the unit faced 189 times power failure up to 78 hrs and steam interruptions of 249 times up to 421 hrs. The steam used in the DTDC and distillation is 50-54 MT and 28 MT/day respectively. The cooling water temperature was monitored to be 25-27 deg C, whereas in Japan the temperature used is 6 deg C through refrigeration plant. The difference of temperature at the inlet & outlet of cooling tower is 5 deg C. Cooling water temperature affects the condensation of the hexane vapor.

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Figure-6.7: Fishbone diagram depicting hexane loss

Inadequate steam supply in SEP

Hexane Loss

Man Work instruction not duly followed

Negligence of plant periodic maintenance

Leakage through Extractor Sealing

Shortage of skilled manpower Mind set

Improper Extractor

Inadequate Vacuum

Less drainage time for miscella

Inadequate DTDC

Inadequate Design

Less heating surface area Insufficient contact between DOC and steam

for indirect steam Less absorption of hexane by Mineral oil

Improper CoInadequate recuperation system

ndensation

Air ingressment Inadequate recuperation system

Fluctuation in steam pressure Insufficient Boiler capacity

High moisture in collets

Fouling of condenser Absence of rotary valveat out let

High bed thickness

Improper flaking

High solvent seed ratio

Faulty quality control of flake thickness

Considering average thickness instead of standard deviation

Presence of foreign matter,which is being considered as seed

Improper Cleaning

Common condensation of vapour

Improper seed preparation

Material Damaged / green seed

High residual oil in DOC Hexane retention by residual oil

High moisture in seed

Inadequate cooking

Inadequate Cracking & Flaking

Power interruption

Insufficient plasticity

Improper flake thickness Worn out flaker rollers

Method

Inadequate recovery facility

Poor recovery ofHexane

Large quantity of hydro carbons discharged into atmosphere.

Environment

Machine

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Observation: Based on the above analysis, it was identified that the existing vacuum in the system is inadequate. The identified reasons are summarised below: (i) Inadequate supply of steam (quantity & pressure) (ii) Poor vapour condensation due to high temperature of cooling water Effects: Inadequate vacuum leads to poor separation of hexane in the DTDC and distillation unit increasing the specific consumption of hexane. The quality of crude oil & DOC may further degrade due to presence of high concentration of hexane. GP option evolved: To minimize the adverse effect due to inadequate vacuum in the system, following GP options were evolved:

1. Ensure adequate steam (quantity & pressure) 2. Provide cold/chilled water for effective condenser cooling

6.3.2.2 Main Cause: Inadequate desolventisation in DTDC Best practices: The wet DOC passes through desolventisation unit of DTDC where steam is used to increase the temperature of DOC to 90 -110 deg C. It also helps in blending of wet DOC to loosen the DOC for hexane escape. The bed thickness in the desolventisation column is normally kept at 400mm and steam pressure at 2.0 Kg/cm2 Field study data: The steam supply from Boilers is not meeting the demand. Presently, the steam supplied to the DTDC is 50-54 MT/day against desired value of 55-60 MT/day. The heating surface area in the DT is not sufficient to transfer heat through existing limpets. Further, the bed thickness was also found to be more, hindering the heat transfer. Trials Conducted:

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Two trials were conducted to reduce hexane loss from existing DTDC by doing little modifications. Trial-1: Bed thickness reduced from 400mm to 250mm keeping direct steam &

indirect steam in the desolventisation compartment constant. Trial-2: Bed thickness reduced from 400mm to 250mm and direct steam

increased from 2 Kg/cm2 to 2.5 Kg/cm2 without changing indirect steam supply.

Direct steam

Height of bed Hexane loss in MD discharging gas

* 2. 0 kg/m2 400mm 2.053 ppm, (100%) 2.0 400 1,642 ppm (80%) 2.5 250 1,241 ppm (60%)

• 2.0Kg/m2 400 mm: standard condition during usual operation (i) However, increase in direct steam in the DTDC brought about lower Urease

Activity (UA) which is used as an indicator for proper heat treatment of DOC for animal feeding. Since the presently available seed is having very low UA compared to the previous few years due to unfavorable weather conditions, the feasibility of implementation of this trial can be worked out.

Conclusion: 1. As shown in the above Table, the hexane loss was decreased substantially by

increasing the direct steam in DTDC and decreasing the height of bed. 2. The desirable UA should not be greater than 0.3 mg/M/gm/at 30 oC and not

less than 0.1 mg/M/gm/at 30 oC. If the value is less than 0.1 mg/M/gm/at 30 oC, the available lysine content will be low and, hence Poultry Farm will not accept. Also, if the value is greater than 0.3 mg/M/gm/at 30 oC, it will retard the growth of chicken. Therefore, the permissible value is between 0.1 to 0.3 mg/M/gm/at 30 oC.

Due to variation in quality of the seed, the effect of UA were found out, and is tabulated below:

Urease activity

Different process stages of seed

Today's value (mg/M/gm/at 30 oC)

3-years before (mg/M/gm/at 30 oC)

Seed 1.8 2.5 Flakes 1.5 2.4 Expander 0.7 1.5 DOC 0.07 to 0.1 0.25

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Operational Control: ♦ By increasing direct steam in Desolventisation compartment of DTDC, UA will go

down. ♦ By increasing the retention time in cooker, indirect steam can be increased; thus

reducing the value of UA. Observation: Based on the above analysis, it was identified that the existing steam supply to the SEP is not sufficient. The identified reasons are summarised below: (iii) Low capacity & efficiency of existing Boilers (iv) Inadequate heating surface area in DT. Effects: Inadequate supply of steam and less heating surface area leads to hexane being carried over through meal dryer air, resulting more hexane losses. GP option evolved: To minimize the adverse effect due to inadequate steam supply & less heating surface area in DT, following GP options were evolved:

1. Ensure adequate steam supply 2. Increasing heating surface by providing more limpets in DT

6.3.2.3 Main Cause: Inadequate drainage in the extractor It has already been discussed in WASTE STREAM- " RESIDUAL OIL CONTENT IN DOC" 6.3.2.4 Main Cause: Inadequate recuperation Best practices: The function of recuperation unit is to recover the uncondensed hexane vapor from the common condenser (DTDC & Distillation). The mineral oil is used as an absorbent to recover the hexane after heating it through Plate Heat Exchanger (PHE).

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Field study data: A trial has been conducted by increasing the flow rate of mineral oil to reduce the hexane concentration in the final vent but this lowers down the temperature of mineral oil. Therefore, the need of increasing the heating surface area of Plate Heater Exchanger came into existence for proper absorption and release of hexane at desired production rate. The increase in flow rate of chilled water in vent condenser further results in lowering the mineral oil temperature before absorption results in better recuperation. Observation: Based on the above trial, it was identified that the existing recuperation system is inadequate. The identified reasons are summarized below:

(i) Low flow rate of mineral oil (ii) Less Heating surface area of Plate Heat Exchanger (PHE) (iii) Low flow rate of chilled water

Effects: Due to poor recuperation system, the recovery of the uncondensed hexane in the common condenser is low resulting in high hexane loss. GP option evolved: To minimize the adverse effect due to inadequate recuperation system, following GP options were evolved:

1. Increase mineral Oil Flow rate 2. Increase heating surface area of PHE 3. Increase chilled water flow rate in vent condenser

6.3.2.5 Main Cause: Inadequate crude oil stripping Best practices: Stripping of crude oil is carried out to remove traces of hexane present in the crude oil. The minimum flash point test for crude oil should be more than 120 deg C. The vacuum maintained for efficient stripping should be 450 mmHg. FIELD STUDY DATA: The vacuum in the stripper was found to be 380 mmHg. The flash point has been analyzed to be more than 120 deg C. The hexane carried along with crude oil has been estimated to be 1-2%.

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It can be further improved, if vacuum in the system could be increased upto 450 mmHg. The problem was discussed with the external consultant and was found that the size of the condenser is small. The separate condenser with ejector is required for better stripping. Observation: Based on the above study, it was identified that the existing oil stripping system is inadequate. The identified reasons for this is:

(i) Inadequate vacuum due to small sized condenser Effects: Due to poor oil stripping, the hexane loss increases. It also affects the quality of the crude oil. GP option evolved: To minimize the adverse effect due to inadequate stripping, following GP option was evolved:

1. Install separate condenser with steam ejector in stripper to increase vacuum

66..44 WWAASSTTEEWWAATTEERR FFRROOMM RREEFFIINNEERRYY && IITTSS TTRREEAATTMMEENNTT PPRROOBBLLEEMM""

6.4.1 (A) General observations & present practices

The major sources of wastewater generation are (i) refinery process wastewater and (ii) acid oil recovery plant (AORP) process wastewater.

In refinery, process wastewater is generated from washing of traces of soap stock present in the oil after degumming & Neutralisation operation in the washing separator. The quantity of wastewater generation from refinery is 62 m3/day. The flow and characteristics of wastewater is discussed in Chapter-5.

The seal cooling wastewater in refinery also discharged along with washing wastewater. This results in high wastewater generation. The quantity of seal cooling wastewater is about 25-30 m3/day. The characteristics of wastewater are discussed in Chapter-5.

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In AORP, the process wastewater is generated from reaction tank. The quantity of wastewater from AORP is 25 m3/day. The characteristics of wastewater are discussed in Chapter-5.

The flow meters installed in the short-mixed plant for water addition was found to be faulty. It was crosschecked with the bucket-stop watch method. Due to faulty water flow meters, the excess water addition to the ETP is 14 m3/day.

The washing operation is carried out through single separator instead of recommended two by the supplier. Analysis results shows there was high Pollution load due to non-availability of one washing separator.

The wastewater generated from refinery section & acid oil recovery plant is treated in the existing ETP The performance evaluation of ETP (discussed in chapter-5) indicates the poor performance of ETP.

Baseline data: Sources of water = Bore Well & Tankers Average Cost of Raw Water = Rs. 15 per m3 Cost of soft water = Rs. 20 per m3 300 m3/d make up Total water in circuit (450 m3/d) 150 m3/d recycled Areas of water loss:

• ETP discharge • Evaporation from Cooling Towers • Moisture added in products • Direct steam evaporation • Other discharges-blow down, Softener's backwash etc.

Average makeup water = 300 m3 per day Annual cost of make up water (soft) = Rs. 18 lakhs per year (B) Concerned process steps

Refinery Section : Washing separator Seal Cooling Water Separator cleaning Acid Oil Recovery Plant (AORP) : Reaction Tank Settling Tank

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(C) Environmental pollution problem: The wastewater from above mentioned sources create high pollution load. Presently the treated wastewater from ETP is not meeting the discharge standard stipulated by the M.P. Pollution Control Board, therefore it is polluting the receiving media. Causes of waste water generation & its treatment problem

1. High water consumption in short mix plant due to faulty Flow Meter 2. Discharge of Seal Cooling Water to ETP 3. High pollution load due to non-availability of one washing separator in short-

mix plant. 4. Poor performance of the existing ETP due to high pollution load from Refinery

washing separator and Reaction & settling tanks of Acid Oil Recovery Plant. The details of the causes are discussed subsequently. 6.4.2.1 Cause: High water consumption in short mix plant due to faulty

flow meter Refer: " Oil loss in refinery" 6.4.2.2 Cause: " Discharge of seal cooling water to ETP" Best Practices: The seal cooling water used in the separator flows indirectly and there is no mixing/contamination of oil/soap-stock during degumming and neutralisation or washing of oil. It should be in a closed circuit and not be discharged into the drain. Field study: Presently the seal cooling water is mixed in the slop oil tank along with refinery wash water and sent to the ETP for treatment. The excess quantity of wastewater generated due to mixing of seal cooling water was monitored to be 25-30 m3/day. Observation: Keeping in mind the scarcity of water in the region and scope of recycling of seal cooling water after minor treatment, the potential of recycling of seal cooling water was recommended.

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Effect: The mixing of seal cooling water into the other wastewater streams results in the high hydraulic load to the ETP. GP options: To minimize the adverse effect due to mixing of seal cooling water into the other wastewater streams, following GP option was evolved:

1. Provide separate collection & treatment systems for seal cooling water & recycle.

6.4.2.3 Cause: " High pollution load due to scarcity of one washing

separator in short-mix plant "

Refer: " Oil loss in refinery " 6.4.2.4 Cause: " Poor performance of the existing ETP due to high

pollution load from Refinery washing separator and Reaction & settling tanks of Acid Oil Recovery Plant "

Best Practices: The wastewater generated from refinery & acid oil recovery plant should be pre-treated to recover free oil & soap-stock. The nature of Refinery wastewater is alkaline and AORP wastewater is acidic. It should be mixed properly before treatment in the ETP. A proper retention time need to be provided for breaking the oil emulsion. Field study: The wastewater from Refinery is pre-treated in the Slop Oil Tank for the recovery of free oil and soap-stock. The retention time in the slop oil is not adequate resulting in poor recovery. It increases the pollution load to the ETP. The acidic wastewater from AORP is not mixed properly with the alkaline wastewater of refinery in the channel. It results in poor splitting of oil emulsion, high consumption of lime and inconsistent characteristic at the inlet of ETP. It leads to poor operation & maintenance of ETP. The detailed performance evaluation of the ETP has been discussed in Chapter-5.

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Observation: The performance evaluation of the ETP shows that the treated wastewater is not meeting the discharge standard stipulated by the Pollution Control Board. Further, the treated water not meeting the various process water quality for recycling into the system. Effect: Due to poor performance of ETP, the treated wastewater does not meet the norms stipulated by law. GP options: To minimize the adverse effect due to poor performance of the ETP, following GP option was evolved:

1. Design & Upgradation of the ETP to treat & meet surface discharge standards stipulated by the Madhya Pradesh Pollution Control Board.

66..55 EENNEERRGGYY LLOOSSSS 6.5.1(A) General observations & present practices Following areas have been identified during detailed study as energy loss areas where the potential of energy saving exists:

• Cooling Tower (electrical energy) • Thermic Fluid Heater • De-odoriser (steam) • Steam distribution lines (un-insulated) • Steam loss (steam trap)

(B) Concerned process steps:

♦ Cooling of water in SEP & Refinery by Cooling Tower ♦ Diesel fired Thermic Fluid Heater ♦ Generation of high vacuum in de-odorisation ♦ Steam pipelines, flanges & valves. ♦ Steam trap.

(D) Environmental pollution problem: The electrical & thermal energies losses are directly or indirectly affects the environment. The coal used for steam and power generation pollutes the environment. It is also a loss of natural resources.

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6.5.2 Cause effect analysis: The critical examination of production processes and utilities led to identification of the causes for energy loss in the plant as mentioned in section 6.5.1(B). . The causes are summaries below: Causes of energy loss:

1. High electricity consumption due to Aluminium Blade in Cooling Towers fans. 2. Higher cost of energy due to diesel as fuel in Thermic Fluid Heater 3. Supply of low pressure steam ( 7 Kg/cm2 against 10 Kg/cm2 required) 4. Heat losses from un-insulated steam lines, flanges and valves 5. Passing of steam traps leading to steam loss

The details of the causes are discussed below: 6.5.2.1 Cause: High electrical consumption due to Aluminium Blade in

Cooling Towers Best practices: Being lighter in weight and less power consumption, the utilities of FRP blade is increasing day-by day over aluminium blade. Most of the units have already installed cooling tower with FRP blade. Observation & field study: The blades of the Cooling towers have been found to be made up of Aluminium. There are two Cooling Towers for the Solvent Extraction Plant. The capacity of each pump is 15 HP. Similarly, there are two Cooling towers in the Refinery Section, each fan of 10 HP capacity. Studies suggested that fan with FRP blade consumes 20-25% less current than that of fan with Aluminium blade of similar dimensions. The monitored data on electrical consumption with Aluminium blade is given below:

Particulars Load on AL Fan SEP-Tower-1 10.7 Amp

SEP-Tower-2 10.7 Amp

Refinery – Tower-1 8.5 Amp

Refinery-Tower – 2 9.5 Amp

Total Current 39.4 Amp Keeping in view the electrical saving potential of 20-25%, the replacement of Aluminium blade with FRP was recommended.

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GP option: To minimize the adverse effect of Aluminium blade, following GP option was evolved.

♦ Replace Aluminium Fan Blade with FRP Blade in Cooling Towers 6.5.2.2 Cause: Higher cost of energy due to diesel as fuel in Thermic

Fluid Heater Best practices: With the rapid increase in the cost of diesel compared to coal, the coal-fired Thermic Fluid Heater is a better option. Observation & field study: Thermic Fluid Heater is used to raise temperature of circulating fluid to 240oC which in turn is used to heat the bleached oil in de-odorize. The diesel consumption in thermic fluid heater is 500 litres/day costing Rs. 9,500/- per day.. Effect: The operating cost of diesel-fired thermic fluid heater is more than the coal-fired thermic fluid heater leading to high-energy cost. GP option: To minimize the adverse effect of diesel fired Thermic Fluid Heater, following GP option was evolved.

1. Replacement of diesel by Coal in Thermic Fluid Heater 6.5.2.3 Cause: Supply of low pressure steams (7 Kg/cm2 against 10

Kg/cm2 required). Best practices: The vacuum required in the existing de-odorizer is 730 mmHg. For this, the appropriate sized nozzle should be installed in the steam ejector. The designed nozzle of the ejector is to function at 10kg/cm2.

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Observation & field study: Steam ejector is the source of vacuum in De-odoriser in the Refinery section. An ejector with motive steam pressure of 7 Kg/cm2 was installed. Due to inadequate supply of steam from the boiler, both in quantity & pressure, the required vacuum is not achieved. Because of low vacuum in De-odoriser, steam consumption increased. There is a proposal to install 15 TPH, 14.5 Kg/cm2 pressure Fluidized Bed Combustion (FBC) Boiler. After installation of FBC Boiler, the requisite steam, both in quantity & pressure would be available in the de-osoriser. Effect: It results in high steam consumption. GP option: To minimize the adverse effect due to low vacuum generating nozzle, following GP option was evolved. 1. Installation of high vacuum generating nozzle 6.5.2.4 Cause: Heat losses from un-insulated steam line, flanges &

valves. Best practices: The pipe-lines carrying steam and flanges, to connect the two steam pipelines, and valves, to control the supply of steam, should be insulated by appropriate insulating material for reduction of heat loss from the surface. Observation & field study: During detailed study, it has been observed that steam insulation over the steam-carrying pipeline is not present in various portions. The flanges & valves in most of the cases are un-insulated leading to loss of thermal energy through radiation. It increases the steam demand and, consequently leads to high fuel consumption. The un-insulated portion of the steam pipelines was measured. The total number of un-insulated flanges and valves present in the steam carrying pipelines has also been quantified. The details are: ♦ Total length of un-insulated pipelines =20 metres ♦ Number of un-insulated flanes =30 ♦ Number of un-insulated valves =40

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Effect: It results in high steam consumption. GP option: To minimize the adverse effect due to un-insulated steam pipe-lines, flanges & valves, following GP option was evolved. 1. Provide insulation to expose steam line, flanges & valves. 6.5.2.5 Cause: By-passing of steam traps leading to steam loss. Best practices: Steam traps are provided to trap un-condensed steam at the Condensate pipeline for recycling. Observation & field study: Most of the steam traps are bypassed because in the existing Boiler the steam requirement is not fully met in the process. The rapid gain in temperature in the production unit is achieved through bypassing of steam traps. It is expected that reduction of nearly 15-20% steam consumption can be achieved if bypass is closed. Effect: It results in high steam consumption. GP option: With the new FBC Boiler, the required steam quality as well as quantity is ensured and hence, to minimize the adverse effect due to by-passing of steam traps, following GP option was evolved.

1. Entire steam bypass should be closed and the bypass connections

may be disconnected with condense line.

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66..66 IINNAADDEEQQUUAATTEE SSTTEEAAMM GGEENNEERRAATTIIOONN LLEEAADDIINNGG TTOO HHIIGGHH OOIILL && HHEEXXAANNEE

LLOOSSSS 6.6.1(A) General observations & present practices The unit has two stationary grate coal-fired water tube boilers. The rated capacities of boilers are 6TPH & 3TPH. But due to high demand, the boilers operate at Maximum Continuous Rating (MCR). The efficiency of boiler is only 65%. There is problem of fluctuation of steam resulting in high residual oil content in DOC and hexane loss. In addition, there is no recovery of heat from the flue gas. (B) Concerned process steps: AREA : Boiler (E) Environmental pollution problem: The running of boilers at MCR with low efficiency leading to excess pollution in the environment. Causes for inadequate steam generation: The inadequate steam generation is evident from the performance evaluation of existing Boilers carried out during detailed study. Therefore, main cause of the inadequate steam generation is less efficient boilers. 6.6.2 Cause: Less efficient boiler Best practices: The boiler should supply appropriate steam at desired pressure in the Solvent Extraction Plant for efficient distillation of Miscella and desolventisation of wet DOC. The efficiency of boiler should be about 75-80% for proper burning of coal and efficient utilization of heat. Therefore, the Upgradation/replacement of the boilers is suggested. Field visit and observation: The unit has two stationary grate coal-fired water tube boilers. The rated capacities of boilers are 6TPH & 3TPH.

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The boilers capacities were assessed with heat transfer area & existing grate area and it was worked out that with manual firing boiler can generate steam of 5.4 TPH & 2.3 TPH respectively at Maximum Continuous Rating (MCR). In normal operating condition, the Boiler can generate only 7.55 TPH. It is suggested that Boiler should not operate at MCR, otherwise it will increase the boiler maintenance cost. The average steam requirement of plant is 8.1 TPH. In order to meet the process steam requirement, the boiler should always operate at the peak load. Even the Boiler operating at the peak load, the quantity as well as quality of the steam can not meet to fulfill the process requirement. During the course of study, it was observed that deteriorating steam quality is due to carryover of water. Steam pressure is inadequate in certain processes increasing the cycle time as well as material losses etc. Need & reasons for installing FBC boiler: • Constraints in existing steam generation capacity: Calculated steam generation

capacity & shortfall is discussed below:

Steam Generation (Calculated)

Boiler Heat Transfer Area ft2

Grate Area ft2

Grate Loading Factor Kg/Ft2/Ft

Coal Firing Rate Kg/Hr

@ 5.5 Kg/Kg Coal TPH

@4.5 Lb/Ft2 Basis TPH

Ave. Gen. TPH

Big 2450 75 13 (with WHR)

975 5.4 5.01 5.3

Small 1280 35 12 420 2.3 2.70 2.45 1395 7.55 Total steam generation Total steam demand(185 T/d+10 T/d loss)/24

7.55 8.10

Constraints: shortfall at MCR (8.1-7.75) Shortfall at NCR (8.1-7.25

0.35 0.85

• Due to shortfall, inadequate steam supplies as a result of lower pressure & more

wetness in steam. Therefore, to increase steam generation (quantity & quality) further may not be possible with existing boilers as already operating at MCR. So, need for more efficient FBC boiler

Effect: The low efficient boilers lead to high oil content in DOC and hexane loss in SEP.

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GP options: In order to maintain the required quality & quantity of steam, following GP options were evolved:

1. Improve the efficiency of the boiler by installing Waste Heat Recovery (WHR) system (For Short Term Measure)

2. Install more efficient Fluidized Bed Combustion (FBC) boiler of higher capacity (For medium term measure).

66..77 FFUUGGIITTIIVVEE EEMMIISSSSIIOONN LLEEAADDIINNGG TTOO AAIIRR PPOOLLLLUUTTIIOONN IINN WWOORRKK

EENNVVIIRROONNMMEENNTT 6.7.1(A) General observation & present practices The seed is un-bagged and poured into the hopper manually. From hopper, seed is transferred to the Vibrating Screen for cleaning. The dust & other foreign materials in the seed are sucked by Dust Extraction System and taken to the Cyclone, the Air Pollution Control Devices [APCD]. It was observed that un-bagging, transferring, screening gives rise to dust emission. The high fugitive dust emission is also attributed to the poor performance of existing APCD including dust extraction system. The seed is conveyed by means of Redler / In-Mass conveyors and bucket elevators to & from seed cleaner to storage silos/ day silo. Normally, poor seed cleaning, open conveyors and absence of dust extraction system at seed transfer points leads to dust entrainment into the environment (B) Concerned process steps:

Cleaning section – vibratory screen Areas:

• Seed unloading & vibrating screening system • Bucket Elevator discharge to Cracking Section

(C) Environmental pollution problem:

The fine dust (not collected in cyclone) released to atmosphere, pollutes the surrounding environment.

Causes of fugitive emission: 1 Inadequate extraction of fine dust from vibrating screen, fine dust escaping

from Cyclone discharge through Chimney 2 Inadequate extraction & control of fine dust emitted from the seed at Bucket

Elevator discharging to Cracker

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6.7.2.1 Cause: Inadequate extraction of fine dust from vibrating

screen, fine dust escaping from Cyclone discharge through Chimney

Best Practices: The dust in the seed should be sucked by proper dust extraction followed by air pollution control devices (APCD) before discharging into the atmosphere. Field measurement data-& observation

The procured seed contain 2.5 to 3.25% foreign matters. The dust concentration is in the range of 1.0 to 1.5%. During seed cleaning operation, the heavy foreign matters get separated by vibratory screen. The fine dust is sucked through the existing dust extraction system followed by Cyclone. A stack monitoring study was carried out for the performance evaluation of the dust extraction system. The detail is discussed in Chapter-5. Though the cyclone efficiency is 88.5%, the SPM at the outlet is more (330 mg/Nm3) than the regulatory norms (150 mg/Nm3). Therefore, dust extraction and control system need to be modified. Effects: Due to poor performance of dust extraction system & air pollution control devices (APCS), the dust spread over in the working environment and affects the health of the workers. GP options: To minimize the adverse effect due to poor extraction of dust in the seed cleaning section, following GP options were evolved: 1. Improve extraction capacity/efficiency by way of additional extraction point &

higher extraction capacity. 2. Install bag filter house in place/in addition to cyclone for capturing fine dust. 6.7.2.2 Cause: Inadequate extraction & control of fine dust emitted

from the seed at Bucket Elevator discharging to Cracker Best Practices: The seed transfer points should be connected with the common dust extraction system followed by Air Pollution Control Devices.

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Field measurement data & observation: The seed containing high dust is not cleaned properly in the seed cleaning section through the vibrating screen and the dust extraction & control system. Subsequently, the dust carries over to the preparatory section. Therefore, during transfer of seed from day-silo to the cracker through the conveyor, the free dust partly come out at the transfer point. Effects: The dust generation at the transfer point in the preparatory section badly effects the working environment. The dust is deposited over the machines of the preparatory section. Further, due to running of machines like cracker, flaker etc., dust re-intrapped into the working environment. GP options: To minimize the adverse effect due to poor extraction of dust in the seed cleaning section and subsequently dust generation in the preparatory section, following GP options were evolved:

1. Improve extraction capacity/efficiency by way of additional extraction point & higher extraction capacity.

2. Install bag filter house in place/in addition to cyclone for capturing fine

dust. The above options are already discussed in previous section. 6.8 IMPROPER MATERIAL HANDLING & HOUSE KEEPING PRACTICES A study was conducted to assess prevailing material handling and house keeping practices. Keeping in view improvement in productivity in terms of saving of time (man-power and machine hour), material and space. The observation of the study is mentioned at section 5.2 in Chapter-5. In view of the observations, measures have been recommended for improvement in material handling and house keeping practices. Section/unit wise recommendation is given in Table-6.3.

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Table-6.3 Recommendations for material handling & House keeping

Seed Charging Section Sr. No.

Recommendations

1.0 Truck Movement and Parking area: (Refer Figure-6.8) • Token system should be introduced based on FIFO (First-in-first-out)

systems for parking Trucks in specified location.

2.0 Seed Unloading Area (Refer Figure-6.9) •

A plat form should be constructed and used for unloading the soybean bags After charging soybean in the hopper, the empty bags should be kept in a grill. A grill similar to cattle track should be provided in the area where trucks are parked during charging.

3.0 Seed Sampling Area (Refer Figure-6.10)

• •

During sieving operation, the material should be collected directly in a bag. Stacking area should be specified and marked. The ramp should be constructed connecting sampling area and charging area so that the material is moved through optimum route and safe walking conditions. Trucks should be cleaned in charging area so as to collect the material in the Grill.

Preparatory Section Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1)

Solvent Extraction Plant

Sr. No.

Recommendations

1.0 For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1).

Refinery Section Sr. No.

Recommendations

1.0

For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1).

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Oil Packing Section

Sr. No.

Recommendations

1.0 Filling of oil in Drums (Refer Figure-6.11) • Filling of oil and weighment should be carried out simultaneously to avoid

double handling of drums as well as the spillage of oil

2.0

Oil Filling and Packaging Section (Refer Figure-6.12) •

• •

A chute should be constructed to move the material from first floor to ground floor. Separate designated area should be used to store empty tins, jars, filled tins, jars and packing materials. Open rack should be provided to store packing materials Rack should be provided to store 15 litres filled jars in storage area The stacks with proper length, breadth and height shall be marked in the storage area. The stack card should be introduced to keep proper accounting of stocks Worktable of filling 15 litres tins and jars should be shifted to packing area

3.0 Oil Filling and Packing of 15 litres tins (Refer Figure-6.13)

• A taper should be provided in oil opening to eliminate the spillage of oil.

4.0 Oil Filling and Packing of 5 litres jar (Refer Figure-6.14) • •

The empty jars should be stored near work center. For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided

DOC Packing Section

Sr. No.

Recommendations

1.0 • • • • •

• •

Stacking area should be marked with stacking plan as well as stack no. DOC should be stacked based on FIFO (first-in-first-out) system Storage area for empty gunny bags, trolley, bin etc. Area for storage of trolleys are not specified resulting in blockage of spaceIt should be standard practice to fill the bags to appropriate height to avoid spillage during movement and packing. Jute thread should be kept collected properly in a bin. For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided

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Stores Section Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1)

Laboratory Section

Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1).

Mechanical Workshop

Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1).

Electrical Workshop

Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1)

ETP & Boiler Section

Sr. No.

Recommendations

1.0 • For continuous improvement in shop floor activities, conduct regular housekeeping audit based on 5S Checklist provided (refer Annexure-6.1)

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66..99 SSUUMMMMAARRYY OOFF CCAAUUSSEE--EEFFFFEECCTT AANNAALLYYSSIISS The summary of cause-effect analysis as mentioned in section 6.1 through section 6.8 is compiled and presented at Table 6.4 for ease in understanding and interpretation.

Table-6.4: Cause of waste streams/problem areas & their effect Waste Streams Causes Effects

Less efficient Cracking (non-graded seed, worn out Roller, & presence of stone in seed)

Less efficient cracking leads to inefficient cooking, flaking and extraction subsequently.

Inadequate Cooking (small cooker, and less heating surface)

Inadequate cooking leads to incomplete flaking and extraction subsequently

Less efficient Flaking (worn out Roller, inadequate Cracking & Cooking)

As the thickness of the flake increases, oil content in DOC increases.

Oil Loss in DOC

Less efficient Extraction (low drainage time, improper hexane spray, inadequate Cracking, Cooking & Flaking)

Poor extraction leads to high residual oil content in DOC.

Excess water addition in hydration & neutralization (faulty Flow Meter)

Excess water hydrolyses the oil and forms emulsion and concentration of soap stock reduces, leading to excess oil loss and generation of excess wastewater.

Absence of one washing separator

Gives rise to hydrated soluble gums in wastewater rendering it difficult to treat. Also, contribute to oil loss in refinery.

Oil loss in Refinery

Possibilities of excess caustic addition in neutralization: (no Flow Meter, manual dosing, excess Saponification)

♦ oil loss due to Saponification

♦ Increased consumption Sulfuric acid for acid oil production

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Waste Streams Causes Effects Use of low grade bleaching earth

♦ Poor color removal efficiency.

♦ Color reversal problems ♦ High oil carry over with

spent bleached earth (by weight)

Improper bleaching earth addition (addition of powder in place of slurry)

♦ Poor bleaching of oil ♦ Loss of bleaching earth ♦ Increase in cost of

production

Oil loss in Refinery-continue

Oil leakage from pump (worn out seal)

♦ Low yield of oil ♦ High load to ETP

Inadequate vacuum in DTDC & distillation (inadequate steam, inadequate cooling & condenser)

♦ Leads to poor separation of hexane in the DTDC and distillation unit increasing the specific consumption of hexane.

♦ The quality of crude oil & DOC may further degrade due to high concentration of hexane.

Inadequate de-solventisation in DTDC (inadequate steam, inadequate heating surface area)

♦ Leads to hexane carry over along with meal dryer air, resulting hexane losses.

Inadequate drainage in extractor (inadequate drainage time, higher hexane concentration in wet DOC)

♦ Leads to additional hexane carry over with wet DOC.

Inadequate recuperation (inadequate absorption / release of hexane)

♦ Recovery of the uncondensed hexane in is not completed

Hexane Loss

Inadequate crude oil stripping (inadequate steam & vacuum, inadequate condenser size)

Poor oil stripping leads to hexane loss and also affects the quality of the crude oil.

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Waste Streams Causes Effects High water consumption in short mix plant due to faulty Flow Meter

Increase in the hydraulic & pollution load to ETP.

Discharge of Seal Cooling Water to ETP

Increase in hydraulic load to ETP

Non-availability of second washing separator in short-mix plant.

Leads to high pollution load to ETP

Excessive Wastewater generation and poor treatment

Poor performance of the existing ETP

Non compliance with effluent discharge standard

High electricity consumption due to Aluminium Blade in Cooling Towers fans.

Leads to 20-25% excess energy consumption compared to FRP impellers.

Higher cost of energy due to diesel as fuel in Thermic Fluid Heater

Contributes to higher cost of product.

Supply of low pressure steam ( 7 Kg/cm2 against 10 Kg/cm2 required)

It results in excess steam consumption.

Heat losses from un-insulated steam lines, flanges and valves

It results in excess steam consumption.

Energy Loss

Passing of steam traps leading to steam loss

It results in excess steam consumption.

Inadequate steam generation

less efficient boilers Less efficient boilers leads to high oil content in DOC and hexane loss in SEP.

Inadequate air pollution control system (APCS), in the seed cleaning section

Leads to air pollution in the work environment

Emission in work environment

Absence of air pollution control system (APCS), in the seed preparatory section

Leads to air pollution in the work environment

Improper Material Handling & House Keeping practices

Principle of Industrial Engineering and 5S not applied

Loss of man & machine hour, and loss of space resulting in overall loss of productivity

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66..1100 GGRREEEENN PPRROODDUUCCTTIIVVIITTYY OOPPTTIIOONNSS In view of cause-effect analysis Green Productivity options were generated with an objective to minimize or eliminate the causes and associated impacts/effects of waste streams/problem areas. The GP options generated against waste streams/problem areas are mentioned along with cause-effect analysis in section 6.1 through section 6.8. Total 36 GP options were generated. The GP options evolved were classified into 5 groups based on the techniques viz. (I) housekeeping improvement, (II) material substitution, (III) recycle/reuse, (IV) recovery and (V) technology (equipment) change. List of GP options under these 5 groups is given in Table-6.5. As mentioned in the Table 6.5, there are 11 GP options for housekeeping improvement, 3 for material substitution, 4 for recycle/reuse, 1 for recovery and 17 for technology (equipment) change. The technique wise distribution of GP options is depicted by Figure-6.16.

Figure-6.16: Distribution of GP options under various techniques

8%

11%3%

42%

36%

House Keeping Improvement

Material Subtitutions

Recycle/Reuse

Recovery

Technology (Equipment)Change

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Table-6.5 Classification of GP options based on techniques involved

GP Options Categories of GP

Option Description Code Section/

Unit Concerned

Repair worn-out roller of the Flaker

WS-I/GPO-6 Seed Preparatory

Recalibrate Water Flow Meter in Short Mix Plant

WS-II/GPO-1 Oil Refinery

Improve material handling and house keeping practices as per recommended measures

WS-VIII/GPO-1

All sections

Provide insulation for exposed steam lines, flanges & valves

WS-V/GPO-4 Steam using sections

Increase the hexane drainage time in Extractor

WS-I/GPO-8 Solvent Extraction

Introduce preventive maintenance of pump gland seals

WS-II/GPO-8 Oil Refinery

Ensure adequate steam (quantity & pressure) in SEP

WS-III/GPO-1 Solvent Extraction

Provide cold/chilled water for effective condenser cooling

WS-III/GPO-2 Solvent Extraction

Increase mineral oil flow rate in TFH

WS-III/GPO-4 Solvent Extraction

Increase chilled water flow rate in vent condenser

WS-III/GPO-6 Solvent Extraction

Cat-I: House keeping improvement

Eliminate by-passing of steam traps.

WS-V/GPO-5 Steam using sections

Use Tonsil in place of local (Indian) Bleaching Earth

WS-II/GPO-5 Oil Refinery

Replace diesel fuel by coal in TFH

WS-V/GPO-2 Oil Refinery

Cat-II: Material substitution

Replace aluminium impellers of Cooling Tower Fans by FRP impeller

WS-V/GPO-1 Cooling Tower

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GP Options Categories of GP

Option Description Code Section/

Unit Concerned

Put in to operation the existing De-stoner

WS-I/GPO-3 Seed Preparatory

Use two existing Washing Separators instead of one at present

WS-II/GPO-2 Oil Refinery

Reuse seal cooling water generated by short mix plant

WS-IV/GPO-1

Oil Refinery

Cat-III: Recycle/ Reuse

Replace 7 kg pressure steam nozzle by existing 10 kg pressure nozzle in De-odoriser

WS-V/GPO-3 Oil Refinery

Cat-IV: Recovery Install Waste Heat Recovery (WHR) system in existing boiler

WS-VI/GPO-1

Boiler

Install seed grader with conveyance system for the grading of seed before cracking

WS-I/GPO-1 Seed Preparatory

Replace worn-out roller of the Cracker

WS-I/GPO-2 Seed Preparatory

Increase the heating surface area in the cooker by adding more steam pipes (limpets)

WS-I/GPO-4 Seed Preparatory

Install a new cooker of requisite size

WS-I/GPO-5 Seed Preparatory

Replace irreparable roller of the Flaker

WS-I/GPO-7 Seed Preparatory

Improve the hexane spray system

WS-I/GPO-9 Solvent Extraction

Install automatic caustic dosing system

WS-II/GPO-4 Oil Refinery

Lower the earth dosing pipe in the bleacher below oil level

WS-II/GPO-7 Oil Refinery

Separate degumming & neutalization

WS-II/GPO-3 Oil Refinery

Cat-V: Technology ( Equipment) Change

Add bleaching earth in to Bleacher as slurry and not as powder

WS-II/GPO-6 Oil Refinery

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GP Options Categories of GP Option Description Code

Section/ Unit

Concerned

Increase heating surface by providing more limpets in DT

WS-III/GPO-3 Solvent Extraction

Increase heating surface area of PHE

WS-III/GPO-5 Solvent Extraction

Install separate condenser with steam ejector in stripper to increase vacuum

WS-III/GPO-7 Solvent Extraction

Upgrade Effluent Treatment Plant to meet surface discharge standards stipulated by MPPCB

WS-IV/GPO-2 ETP

Install FBC boiler of requisite capacity

WS-VI/GPO-2 Boiler

Improve dust extraction capacity & efficiency of existing Cyclone

WS-VII/GPO-1 Seed Cleaning

Cat-V: Technology ( Equipment) Change -continue

Install Bag Filter in addition to cyclone to capture fine dust

WS-VII/GPO-2 Seed Cleaning

*****

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