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Integrated Testing of a Membrane CO 2 Capture Process with a Coal-Fired Boiler NETL CO 2 Capture Technology Review Meeting August 22, 2017 DE-FE0026414 Thomas Hofmann, Jay Kniep, Tim Merkel, Vincent Nguyen, Alvin Prakash, Han Wang, Bob Watson, Erik Westling - MTR Hamid Farzan, Jason Fennell, Andrew Mackrory, Larry Mohr, Prasanna Seshadri, Jennifer Sivy – B&W
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  • Integrated Testing of a Membrane CO2 Capture Process with

    a Coal-Fired Boiler

    NETL CO2 Capture Technology Review MeetingAugust 22, 2017

    DE-FE0026414

    Thomas Hofmann, Jay Kniep, Tim Merkel, Vincent Nguyen, Alvin Prakash, Han Wang, Bob Watson, Erik Westling - MTR

    Hamid Farzan, Jason Fennell, Andrew Mackrory, Larry Mohr, Prasanna Seshadri, Jennifer Sivy – B&W

  • Project Overview

    2

    Award name: Integrated Testing of a Membrane CO2 Capture Process with a Coal-Fired Boiler

    Project period: 7/1/15 to 3/31/18

    Funding: $3.6 million DOE; $0.9 million cost share ($4.5 million total)

    DOE program manager: José Figueroa

    Participants: MTR and Babcock & Wilcox

    Project scope: Demonstrate integrated operation of the MTR small pilot capturesystem with B&W’s SBS-II pilot coal boiler.

    Project plan: The project is organized in three phases:

    • Phase 1 – Site preparation and system modification/installation

    • Phase 2 – Commissioning, testing, and data analysis

    • Phase 3 – Decommissioning and reporting

  • Background: MTR CO2 Capture Process

    3

    Benefits of selective recycle:• Increases CO2 concentration going to the capture step, and • Reduces the fractional CO2 removal required by the capture step

    20% 10%

    2%

    8%

    65%

    U.S. Patents 7,964,020 and 8,025,715

    (1) Membrane performance

    studied at NCCC

    (2) Impact of CO2 recycle

    studied at B&W

  • MTR CO2 Capture Development TimelineFeasibility study (DE-NT43085)• Sweep concept proposed• Polaris membrane conceived

    APS Red Hawk NGCC Demo• First Polaris flue gas test• 250 lb/d CO2 used for algae farm

    APS Cholla Demo (DE-NT5312)• First Polaris coal flue gas test• 1 TPD CO2 captured (50 kWe)

    NCCC 1 MWe Demo (DE-FE5795)• 11,000 hours of 1 TPD system operation• 1,500 hours of 20 TPD system operation

    2006 2008 2010 2012 2014 2016 2018 2020

    TRL6 TRL7 TRL8TRL5TRL4

    Hybrid Capture (DE-FE13118)• Membrane-solvent hybrids with UT, Austin

    Low Pressure Mega Module (DE-FE7553)• Design and build a 500 m2 optimized module

    TRL3

    B&W Integrated Test (DE-FE26414)

    4

  • 5

    MTR system

    • In June 2015, MTR pilot system completed 1,500 hours of successful operation at NCCC

    • System was then moved to B&W in Spring 2016 for integrated boiler testing

    • Membranes are simple and compact compared to competing technologies

    • In previous 1 TPD testing, Polaris modules completed ~11,000 hours of operation at NCCC

    Prior Testing of 20 TPD System at NCCC

    5

  • 6

    20 TPD System ShowsStable Performance

    • System operated in slipstream mode (no recycle to boiler)

    • Stable performance, reaching up to 90% capture

    • System goes from cold start to steady state in ~15 minutes

    Run time (hours)

    CO2capture

    rate(%)

    Figure data from NCCC campaign PO3 (May to July 2015)

    PO-3 run time (hours)

    CO2capture

    rate(%)

  • Prior B&W Studies of CO2 Recycle Impact on Boiler Performance

    Phase I – CFD modeling• B&W modeled 2 boiler configurations (radiant boiler firing bituminous coal

    and SWUP firing PRB coal) and 2 sweep recycle cases (constant secondary air flow and constant stoichiometry)

    • Main conclusion of modeling study: secondary air laden with CO2 appears feasible as a retrofit in either of the boiler configurations examined if oxygen mass flow to boiler is fixed

    Phase II – Pilot testing • B&W’s SBS-II 1.8 MWth pilot boiler operated with CO2-laden combustion air• Two coals evaluated: a western sub-bituminous coal and a highly volatile

    bituminous coal • O2 content of windbox air varied from 21% to 16% through CO2 dilution• Monitored flame stability, length, and shape; unburned combustibles in fly

    ash, and furnace exit gas temperature• Radiant furnace and convective pass heat absorptions were measured• Boiler efficiencies for air and sweep firing were determined

    77

  • Highlights from Testing with CO2-laden Air on B&W Boiler

    8

    • Stable and attached flames with air (21% O2) and CO2-enriched air (16-18% O2)

    • CO2-enriched flame was less luminous than air-fired case

    • Lower furnace heat absorption but higher convection pass/air heater heat transfer for CO2-enriched operation relative to air

    • For bituminous coal, 30% lower NOxemissions with CO2-enriched air

    • No burner modifications necessary• Net reduction in plant efficiency of ~0.75%

    at 18% O2

    Flame image from combustionof PRB coal with air (21% O2)

    Flame image from combustion of PRB coal with CO2–enriched (18% O2)

  • Boiler Efficiency Versus Windbox O2

    9

    • Increased CO2 recycle reduces windbox O2 content through dilution, which reduces plant efficiency almost linearly

    • However, increased CO2 recycle reduces capture energy; net benefit

    • 18% O2 appears to be optimum for retrofit; beyond this point tube erosion, abrasion, and slagging may become important

    • Because flame is stable to 16% O2, this level of recycle should be further evaluated for new plants

    0

    0.2

    0.4

    0.6

    0.8

    1

    1.2

    16 17 18 19 20 21 22

    Plant efficiency loss (%)

    Windbox O2 content (%)

  • 10

    Objectives of Integrated Project(DE-FE0026414)

    • Use an existing 20 TPD MTR small pilot membrane system to test integrated operation (with CO2 recycle to boiler) on an appropriately-sized boiler (B&W SBS-II)

    • Validate prior B&W modeling and testing showing modest effect of recycled CO2 on boiler performance

    • Understanding how the various membrane parameters impact performance of a dynamic boiler system

    • Reduce risk prior to scaling up to larger demos

  • 11

    Schematic of Integrated Test

  • MTR Skid During Transport and Installation at B&W

    1212

    Skid arriving at B&W

    Installation of 2nd floor

    12

  • MTR Skids at B&W’s SBS-II Research Facility

    1313

    Main skid and smaller low-pressure drop sweep module anchored to

    foundation

    Main skidSweep module

  • Sample Results from B&W Integrated Tests

    14

    20% 10%

    2%

    8%

    65%

    2 – 6.7%

    7.3 – 17.4%

    14.3 – 20.6%

    6.2 – 10.8%

    Oxygen at Boiler Windbox:17.0 – 21%

    Membrane-Boiler Integrated Test Plan• 5 weeks of testing on natural gas, Powder River Basin

    (PRB) Coal, and Eastern Bituminius Coal• 90% capture achieved and a variety of partial capture

    conditions• CO2 content of flue gas increased as expected in

    simulations• Boiler flame was stable allowing a full battery of stream

    conditions and boiler efficiency measurements to be conducted (analysis is ongoing)

    14

  • 1 MWe System Sweep Flow Rate Parametric Results from Integrated Tests

    15

    50

    60

    70

    80

    90

    100

    0 500 1,000 1,500 2,000 2,500

    CO2

    capture rate(%)

    Sweep flow rate (lb/h)

    Feed = 30 psia

    0

    20

    40

    60

    80

    100

    0 500 1,000 1,500 2,000 2,500

    Sweep-stepCO

    2 capture

    rate (%)

    Sweep flow rate (lb/h)

    Feed = 30 psia

    Influence on the Overall CO2 Capture RateInfluence on Sweep Step CO2Capture Rate Efficiency

    15

  • Integrated Boiler/Membrane Systems Transition Response

    16

    0

    3

    6

    9

    12

    15

    18

    21

    0

    1000

    2000

    3000

    4000

    5000

    6000

    7000

    8:10 8:20 8:30 8:40 8:50 9:00 9:10 9:20 9:30 9:40 9:50 10:00

    Gas C

    once

    ntra

    tion

    (Vol

    . %, d

    ry)

    Gas F

    low

    Rat

    es (l

    b/hr

    )

    11/3/2016

    Fresh Air Intake Flow

    Sweep Gas Flow

    Convection Pass Flow

    Windbox O2

    Convection Pass O2

    Convection Pass CO2

    0

    3

    6

    9

    12

    15

    18

    21

    0

    1000

    2000

    3000

    4000

    5000

    6000

    7000

    12:00 12:07 12:14 12:21 12:28 12:36 12:43 12:50

    Gas C

    once

    ntra

    tion

    (Vol

    . %, d

    ry)

    Gas F

    low

    Rat

    es (l

    b/hr

    )

    11/16/2016

    Fresh Air Intake Flow

    Sweep Gas Flow

    Convection Pass Flow

    Windbox O2

    Convection Pass O2

    Convection Pass CO2

    16

  • Integrated Boiler/Membrane Systems Transition Response to E-Stop

    1717

  • B&W’s Analysis of CO2 Recycle Impact on Boiler Operation

    • Furnace heat absorption is lower

    • “Furnace” refers to the radiant heat transfer section of the boiler upstream of the tube banks in the convection pass.

    • Convection pass heat absorption is higher

    • Convection pass outlet heat flux is higher

    • Air heater heat absorption is higher

    • Air heater flue gas outlet heat flux is higher

    • Total heat absorption is slightly reduced

    18

    Coal 30P M1 & M2 Coal 27P M2 Only 20-Oct-16 18-Oct-16

    Test Duration (h:mm) 7:00 7:15PRB PRB

    Load (MW) 1.5 1.4FEGT (°C) 1,179 1,259Convection Pass Exit Temperature (°C) 397 380Air Heater Exit Temperature (Flue Gas) (°C) 217 210

    53% 0%Furnace Absorption (MW) 0.52 0.66Convection Pass Absorption (MW) 0.96 0.91Convection Pass Outlet Heat Flux (MW) 0.50 0.43Total Heat Absorption (MW) 1.62 1.68Air Heater Absorption (MW) 0.19 0.16Air Heater Outlet Heat Flux (Flue Gas) (MW) 0.31 0.27

    Date

    Fuel

    Membrane Secondary Air Ratio

    Test Name

    18

  • Decommissioning and Site Restoration Activities Have Been Completed

    19

    • All skids decommissioned and removed from site by June 2017

    • Site clean-up and smooth-out of concrete foundation has been finished

    • Final reporting and analysis is underway

    19

  • Summary

    • CO2 capture membrane performance continues to improve and has been validated on the 0.05 MWe slipstream system with over 11,000 hours of runtime at NCCC

    • 1 MWe small pilot operation at NCCC was completed in 2015. Testing successfully demonstrated optimized modules (low ∆p, low cost) with over 1,500 hours of runtime

    • 1 MWe small pilot was successfully integrated with the B&W research boiler for five weeks of integrated testing with CO2recycle to the boiler in late 2016

    • The integrated membrane-boiler field test experimentally validated simulated system performance

    • Boiler flame was stable throughout parametric testing allowing a full battery of stream conditions and boiler efficiency measurements

    20

  • Acknowledgements

    2121

    • U.S. Department of Energy,National Energy Technology Laboratory

    – José Figueroa– Mike Mosser

    • Southern Company Services (NCCC)– Tony Wu

    • Babcock & Wilcox– Hamid Farzan– Jennifer Sivy– Andrew Mackrory

    Slide Number 1Project OverviewBackground: MTR CO2 Capture ProcessSlide Number 4Slide Number 5Slide Number 6Slide Number 7Slide Number 8Slide Number 9Slide Number 10Slide Number 11MTR Skid During Transport and Installation at B&WMTR Skids at B&W’s �SBS-II Research FacilitySample Results from B&W Integrated Tests1 MWe System Sweep Flow Rate Parametric Results from Integrated TestsIntegrated Boiler/Membrane Systems Transition ResponseIntegrated Boiler/Membrane Systems Transition Response to E-StopB&W’s Analysis of CO2 Recycle Impact on Boiler OperationDecommissioning and Site Restoration Activities Have Been CompletedSummarySlide Number 21


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