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. _ _ _ Gs.o'ge Power Comrwiy * .. 333 P.tdmont Aenae Atenta, Goafgia 303D6 inep? vie 404 !4'0 3195 ..; , * * * * Maang Add'ent , * 40 invemess Center Puksay Post O!!ce Dan 1?DS D.munf am, Alabama 35201 Telermone 20$ 660 55B1 t*w scwcrn A c sc. tem W G. Hairston, lit sensor V,ce Presdent Nacteat CWrations ELV-Oll87 0179 December 22, 1989 Docket No. 50-425 U. S. Nuclear Regulatory Commission ATTN: Document Control l'esk Washington, D. C. 20555 Gentlemen: V0GTLE ELECTRIC GENERATING PLANT LICENSFE EVENT REPORT HEATER DRAIN dNK VALVE REASSEMBLY ERROR LEADS TO TURGi.*!E/ REACTOR TRIP in accordance with 10 CFR 50.73, Georg a Power Company hereby submits the enclosed report relating to an event which occurred on December 2,1989. Sincerely, at)/f (b$ W,. G. Hairston, 111 WGH,Ill/NJS/gm Enclosure: LER 50-425/1989-031 xc: Georaia Power Company Mr. C. K. McCoy Mr. G. Bockhold, Jr. Mr. P. D. Rushton Mr. R. M. Odom NORMS U. S. Nuclear Reaulatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. J. B. Hopkins, Licensing Project Manager., NRR Mr. J. F. Rogge, Senior Resident inspector, Vogtle 9001020207 891222 PDR ADOCK 05000425 [621 S PDC
Transcript
Page 1: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

. _ _ _

Gs.o'ge Power Comrwiy*..333 P.tdmont AenaeAtenta, Goafgia 303D6inep? vie 404 !4'0 3195..;,

* * * * Maang Add'ent,* 40 invemess Center Puksay

Post O!!ce Dan 1?DSD.munf am, Alabama 35201Telermone 20$ 660 55B1

t*w scwcrn A c sc. tem

W G. Hairston, litsensor V,ce PresdentNacteat CWrations

ELV-Oll870179December 22, 1989

Docket No. 50-425

U. S. Nuclear Regulatory CommissionATTN: Document Control l'eskWashington, D. C. 20555

Gentlemen:

V0GTLE ELECTRIC GENERATING PLANTLICENSFE EVENT REPORT

HEATER DRAIN dNK VALVE REASSEMBLY ERRORLEADS TO TURGi.*!E/ REACTOR TRIP

in accordance with 10 CFR 50.73, Georg a Power Company hereby submits theenclosed report relating to an event which occurred on December 2,1989.

Sincerely,

at)/f (b$W,. G. Hairston, 111

WGH,Ill/NJS/gm

Enclosure: LER 50-425/1989-031

xc: Georaia Power CompanyMr. C. K. McCoyMr. G. Bockhold, Jr.Mr. P. D. RushtonMr. R. M. OdomNORMS

U. S. Nuclear Reaulatory Commission

Mr. S. D. Ebneter, Regional AdministratorMr. J. B. Hopkins, Licensing Project Manager., NRRMr. J. F. Rogge, Senior Resident inspector, Vogtle

9001020207 891222PDR ADOCK 05000425 [621S PDC

. . .

Page 2: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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On 12-2-89, plant personnel were releasing a clearance on Heater Drain Tank(HDT) high level dump valve 2LV-4334. The high level dump valve for MoistureSeparator Reheater (MSR)"D", 2LV-4525, was in a 50% jacked-opened position dueto 2LV-4334 being isolated. Upon opening the valve which isolated P.LV-4334, itbecame evident that 2LV-4334 was not closed. The HDT level decreased and thenormal level control valve, 2LV-4332, closed. The isolation valve was reclosedand HDT level rose; however, 2LV-4332 failed to reopen resulting in risingfeedwater heater levels and, due to the configuration of 2LV-4525, MSR D levelrose as well. At 0341 CST, MSR D level reached the high level setpoint giving aturbine / reactor trip.

The root cause for the event was cognitive personnel error involving reassemblyof 2LV-4334. The valve was reassembled such that its position indication showedclosed when it was actually full open. For 2LV-4332, the level control sensinglines were discovered to be clogged which resulted in its malfunction.

Actions to prevent recurrence include discussing this event in maintenance shopmeetings, n..plementation of a periodic task to blowdown the level controlsensing lines associated with 2LV-4332, and inclusion of this event in operatorcontinuing training.

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Page 3: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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A. REQUIREMENT FOR REPORT

This report is required per 10 CFR 50.73 (a)(2)hv), since the eventresulted in an automatic actuation of the Reactu Protection System (RPS),'

B. UNIT STATUS AT TIME OF EVENT

At the time of this event, Unit 2 was in Mode 1 (Power Operation) at 100% ofrated thermal. power. Moisture Separator Drain Tank (MSDT) "D" high leveldump valve, 2LV-4525, was in a 50% jacked-opened position to reduce flow toHeater Drain Tank (HDT) "B" since HDT "B" high level dump valve, 2LV-4334,was out of service for maintenance. No other plant equioment was inoperableor otherwise in an off-normal status such that it contriauted to theoccurrence of this event.

C. DESCRIP110N OF EVENT

On 12-2-89, plant personnel were in the process of releasing a clearance on2LV-4334 in order to perform post maintenance functional testing on thisvalve. At approximately 0330 CST, a plant equipment operator (PEO) beganopening manual isolation valve 2-1304-U4-052, t1ereby unisolating 2LV-4334.Due to problems which had been experienced on 11-5-89 (reference LER425/89-029), when restoring the HDT "A" high level dump valve to service,the activities were being directed by an on-shift operations supervisor(0S05) who was present at the valve with a maintenance supervisor, amaintenance foreman, and an instrumentation and controls foreman. Al so,preparations had been made to establish direct communication with the Unit 2Control Room; however, communication had not yet been established when thePE0 was directed to open the manual isolation valve.

With the manual isolation valve approximately 10% open, the line startedmoving and it became evident that 2LV-4334 was not closed even though thelocal indication showed full closed. This allowed HDT "B" to start dumpingto the main condenser. The Control Room observed HDT "B" level decrease andthen the normal level control valve (i.e., Heater Drain Pump "B" dischargecontrol valve), 2LV-4332, closed on low level.

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Page 4: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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The PE0 was directed to reclose the manual isolation valve and HDT *B" level! started increasing. Main feedwater pump "A" and "B" suction pressure had ;

dropped due to valve 2LV-4332 being closed and the standby condensate pump !was started to restore suction pressure. As HDT "B" level increased, valve2LV-4332 failed to reopen. This caused HDT "B" level to go off-scale high !

and the levels in feedwater heater "4B", feedwater heater "5B", MSDT "C", |MSDT *D", and Moisture Separator Reheater (MSR) "D" began to increase as I

well. The OSOS then proceeded to 2LV-4332 to attempt to open this valve iusing the handwheel. The Support Shift Supervisor similarly proceeded to |2LV-4525 to attempt to further jack it open. However, before either of lthese actions could be accomplished, MSR "D" level reached the high levelsetpoint causing a turbine trip which resulted in a reactor trip at 0341CST. !

On the reactor trip, all control rods fully inserted, the Main feedwaterSystem isolated and the Auxiliary feedwater (AFW) System actuated asdesigned. Control Room operators entered emergency operating Procedure19000-C, "E-0 Reactor Trip or Safety Injection," and then responded tothrottle AFW flow and maintain steam generator water levels. By 0353 CST,the plant had been stabilized in Mode 3 and unit operating Procedure12006-C, " Unit Cooldown to Cold Shutdown," was entered.

Several abnormalities occurred following the reactor trip but had no impacton the ability to shutdown the reactor and maintain it in a safe shutdown

,

condition. These occurrences included the lifting and reclosing of steamgenerator atmospheric relief valve 2PV-3020, at a steam line pressure belowthe lift setpoint; an apparent waterhammer involving feedwater heater "4B";and the trip of breakers 2NBL1-04 and 2NBL1-13 during the residual transferof 4160 V switchgear 2NA01. The trip of breakers 2NBL1-04 and 2NBL1-13resulted in normal lighting not being restored to portions of the AuxiliaryBuilding and the Control Building following completion of the residualtransfer of 2NA01. Operators responded to reset these breakers and restorelighting to these areas.

D. CAUSE OF EVENT

The maintenance of 2LV-4334 had required the removal of the pneumaticactuator from the valve to allow rebuilding of the actuator in themaintenance shop. Since the valve was not to be removed from the line, themaintenance crew that removed the actuator had match-marked the valve in theopen position. A second maintenance crew had rebuilt the actuator andreinstalled it using the maintenance match marks. A third crew had testedthe valve operation and reinstalled the position indication to match theactuator piston position.

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Page 5: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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After the reactor tripped, the maintenance match marks were checked and werefound to disagree with the valve position indication by 90 degrees. It wasthen realized that a reassembly error had occurred in that the actuatorpiston had been in the closed position when the actuator was reinstalled onthe valve which had been match-marked in the open position.

This reassembly error was not recognized when the lever which connects theactuator piston connecting rod to the valve shaft was ) laced back onto thevalve shaft since this lever will fit onto the valve s1 aft with the actuatorpiston in either an open or closed position. Stroking of the valve, afterreinstallation of the actuator but with the downstream isolation valve still '

closed, had also failed to reveal the error since the valve ball is free torotate 360 degrees (i.e., the valve was actually being stroked between theopen position and a position 90 degrees beyond open). Therefore, when thedownstream isolation valve was opened, 2LV-4334 was actually in a full openposition even though its position indication showed full closed. This lead -

to the reactor trip as previously discussed.

The root cause for the reassembly error was cognitive personnel error. The ,

maintenance crew that reinstalled the actuator failed to recognize the needto verify the correct actuator piston position as compared to the valve ballposition. The maintenance work order controlling the work on 2LV-4334contained instructions to use both the vendor valve instruction manual andthe vendor actuator instruction manual for performing the work. Subsequentinterviews of involved personnel revealed that only the actuator instructionmanual was used. The valve instruction manual contains details ondetermining the correct lever / valve shaft orientation based on fcctory indexmarks located on these individual parts and therefore should have been usedas well.

The failure of the normal level control valve, 2LV-4332, to reopen as HDT"B" level increased also contributed directly to the reactor trip. Had thisvalve responded properly, the reactor trip would not have occurred.Flushing of the associated level control sensing lines and pot after the i

reactor trip revealed that these lines had become clogged with a gunk type ;substance. The root cause for the failure of 2LV-4332 was the clogged I

sensing lines and a contributing cause was that no preventive maintenance 1

(PM) task presently exists to periodically blow down or otherwise flushthes+ sensing lines.

The cause for steam generator atmospheric relief valve 2PV-3020 opening |below its setpoint and the cause for the trip of breakers 2NBil-04 and2NBL1-13 is still being investigated.

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Page 6: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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E. ANALYSIS OF EVENT )On the reactor trip, all control rods were observed to fully insert into thecore. Main feedwater isolated and Auxiliary Feedwater actuated as designed. ]The MSR high level setpoint turbine trip actuated as designed to trip theturbine and protect it from water induction damage. No operator action was ,

required to reclose 2PV-3020. The loss of lighting in portions of the i

Auxiliary and Control Buildings was an operator inconvenience which was ,

promptly corrected by resetting bra xers 2NBL1-04 and 2NBL1-13. The *

apparent waterhammer involving feedwater heater "48" resulted in no damageto any safety related equipment. Based on these considerations, there wasno adverse effect on plant safety or on the health and safety of the public.

F. CORRECTIVE ACTIONS

1. The actuator was removed from 2LV-4334 and reinstalled with the actuatorpiston correctly aligned with the valve ball position.

2. This event, including the need to ensure proper use of vendor manualswhen required by maintenance work order instructions and the need toensure all pertinent information is conveyed to the next maintenancecrew, will be discussed in maintenance shop meetings by 2-1-90,

3. The level control sensing lines and the pot which provides the normallevel control for HDT "B" were flushed with demineralized water andnormal operation of 2LV-4332 was restored. A PM task will beimplemented by 1-15-90 to provide for a periodic blowdown or flush oflevel control sensing lines and condensate pots for the Heater DrainTanks.

4. This event, including a discussion of alternative methods of reducingflow to a heater drain tank, will be covered in operator continuingtraining by 4-1-90.

5. A walkdown of secondary piping and components associated with feedwaterheater "4B" was performed after the waterhammer occurred. Two pressureindicators and a pin for a pipe hanger were found damaged. No otherdamage was found.

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Page 7: LER 89-031-00:on 891202,moisture separator reheater (MSR ... · epe.c team 33. u s nucli ah mopl&tdat cowbesion approvtd du$ wd siptim-licensee event report (ler) * * *'a' 5 "' "l

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6. The control circuit for 2PV-3020 will be investigated and calibrated orrepaired as required by 12-27-89.

.

7. Engineering will investigate the trip of breakers 2NBL1-04 and 2NBL1-13! by 1-31-90 to determine if any corrective action is required.

G. ADDITIONAL INFORMATION

1. Failed Components Identification

HDT "B" High Level Dump Valve 2LV-4334Fisher Controls 12 - Inch Design V100 Vee-Ball Valve with Type 1061Pneumatic Piston Rotary Actuator.

HDT "B" Normal Level Controls Loop 2LCL-4332Fisher Controls 14 - Inch Cage Style Level-Trol Model No. 2502-2498.

2. Previous Similar Events

The event which resulted in a reactor trip on 11-5-89 (reference LER425/89-029) was similar in that the event was initiated when a HDT highlevel dump valve was restored to service. However, the root causes forthese two events differ in that operator actions were appropriate inresponding to the current event.

3. Energy Industry Identification System Codes

Main Feedwater System - SJ

High Pressure Heaters and Moisture Separator Reheater Drains and VentsSystem - SN

'

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