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Methodology of Mitigating Corrosion Mechanisms in Amine Gas Treating Units

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8/10/2019 Methodology of Mitigating Corrosion Mechanisms in Amine Gas Treating Units http://slidepdf.com/reader/full/methodology-of-mitigating-corrosion-mechanisms-in-amine-gas-treating-units 1/12 METHODOLOGY OF MITIGATING CORROSION MECHANISMS IN AMINE GAS TREATING UNITS A. M. Al-Zahrani and S. I. Al-Luqman Saudi Aramco, E-7600, Dhahran 31311, Saudi Arabia ABSTRACT Di-Glycol Amine (DGA) has been utilized for acid removal from hydrocarbon gas for many years by Aramco in Saudi Arabia. Over the years the gas demand increased significantly which resulted in operating some gas treating units in excess of the original design. Running gas treating units over the original design has impact on the process and utilities streams. This paper investigates the impact of operating DGA units over their design on the vessels and piping. This paper will present the methodology that was developed to evaluate the integrity of the units and how to discover wall thinning of piping and vessels. This methodology starts by evaluating the unit process parameters such as  pressure, temperature, H 2 S and CO 2  level, and line velocity, and then evaluates unit materials. Potential damage mechanisms and the appropriate locations for inspection are a critical part of the evaluation  process. INTRODUCTION The subject plant has four low pressure 150 psig (11.6 kg/cm 2 ) gas treating units. All units utilize DGA for acid gas removal (H 2 S and CO 2 ). These units worked smoothly, in terms of corrosion  problems, for about 20 years. However, the demand on gas processing increased sharply with time. As a result, serious corrosion problems developed at various locations. The material of construction for piping and equipment is principally carbon steel except for some locations such as reclaimer tubes that are made from type 304 stainless steel. DGA can be very corrosive to carbon steel at high temperatures and/or high velocity in the presence of H 2 S and CO 2 . 1 Typical damage mechanisms are erosion/corrosion and localized corrosion. Corrosion is most common in heated and/or high velocity areas of the units such as reboilers, reclaimer, stripper column, and rich amine  piping. 1 06441 Paper No. ©2006 NACE International. Requests for permission to publish this manuscript in any form, in part or in whole must be in writing to NACE International, Conferences Division, 1440 South Creek Drive, Houston, Texas 77084. The material presented and the views expressed in this paper are solely those of the author(s) and are not necessarily endorsed by the Association. Printed in the U.S.A. Copyright
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Page 1: Methodology of Mitigating Corrosion Mechanisms in Amine Gas Treating Units

8/10/2019 Methodology of Mitigating Corrosion Mechanisms in Amine Gas Treating Units

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METHODOLOGY OF MITIGATING CORROSION MECHANISMS IN AMINE GAS

TREATING UNITS

A. M. Al-Zahrani and S. I. Al-Luqman

Saudi Aramco,E-7600, Dhahran 31311,

Saudi Arabia

ABSTRACT

Di-Glycol Amine (DGA) has been utilized for acid removal from hydrocarbon gas for many

years by Aramco in Saudi Arabia. Over the years the gas demand increased significantly which resulted

in operating some gas treating units in excess of the original design. Running gas treating units over theoriginal design has impact on the process and utilities streams. This paper investigates the impact of

operating DGA units over their design on the vessels and piping. This paper will present the

methodology that was developed to evaluate the integrity of the units and how to discover wall thinning

of piping and vessels. This methodology starts by evaluating the unit process parameters such as pressure, temperature, H2S and CO2 level, and line velocity, and then evaluates unit materials. Potential

damage mechanisms and the appropriate locations for inspection are a critical part of the evaluation process.

INTRODUCTION

The subject plant has four low pressure 150 psig (11.6 kg/cm2) gas treating units. All units utilize

DGA for acid gas removal (H2S and CO2). These units worked smoothly, in terms of corrosion

 problems, for about 20 years. However, the demand on gas processing increased sharply with time. As a

result, serious corrosion problems developed at various locations.

The material of construction for piping and equipment is principally carbon steel except for somelocations such as reclaimer tubes that are made from type 304 stainless steel. DGA can be very corrosive

to carbon steel at high temperatures and/or high velocity in the presence of H2S and CO2.1

Typicaldamage mechanisms are erosion/corrosion and localized corrosion. Corrosion is most common in heated

and/or high velocity areas of the units such as reboilers, reclaimer, stripper column, and rich amine

 piping.

1

06441

Paper No.

©2006 NACE International. Requests for permission to publish this manuscript in any form, in part or in whole must be in writing to NACE International,Conferences Division, 1440 South Creek Drive, Houston, Texas 77084. The material presented and the views expressed in this paper are solely those ofthe author(s) and are not necessarily endorsed by the Association. Printed in the U.S.A.

Copyright

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Analysis of process parameters revealed that the low pressure gas treating units were operating at125-150% of their original design capacity. Also, the acid gas content in the sour gas varies between 13-

17 mole% and sometimes exceeds 17 mole%. Also, it was found that the amine circulation rate has

increased by 16% with DGA solution concentration of 47-50 wt%. However, this additional amount ofamine solution is still not sufficient to maintain the required rich amine acid gas loading below 0.4 mol

acid gas/ mol DGA to minimize corrosion development, as designed.

Degradation of DGA to other products is another concern in amine treating units. The most

common DGA degradation product is N,N'his (hydroxyethoxyethyl)urea (BHEEU) that has a higherviscosity and boiling point than DGA. Build-up of degradation product in the system will result in

lowering the heat transfer, increasing pressure drop, and reducing the sweetening efficiency. In a DGAunit, a reclaimer is used to purify lean DGA from chemical degradation products. BHEEU can be

reversed back to DGA in the reclaimer at temperature range of 360-380oF (182°C -193°C), per the

following reaction:

2R-NH2CO+ (H2O or H2S)↔2R-NH2+ (CO2 or COS) (1)

Lean DGA target limits are 10 wt% BHEEU and maximum of 6 wt% morphaline. Reclaimer process is limited to 360-380

oF to avoid morphaline formation because it cannot be reclaimed back to

DGA. Morphaline is usually formed at temperature higher than 380o

F (193°C).

On-stream inspection program (OSI) using ultrasonic wall thickness (UT) measurements was

used exclusively as the corrosion monitoring technique for process streams except utilities lines. This

 program is a non-destructive technique to measure corrosion rate and remaining life at specific locationsof vessels and piping but it is difficult to detect localized corrosion by using UT technique.

In 2002, a Risk Based Inspection (RBI) study was conducted on one of the subject gas treating

units as per API 5803. Some piping and vessels such as utilities lines were not covered by the RBI study.

Results of the RBI study support in identifying most of the high risk locations in the units.

Following the RBI study, an intensive assessment program was established to identify the rootcauses of corrosion problems and provide the required protective actions to ensure safe operations and

avoid reoccurrence of failures. The study was highly dependent on the inspection data and operating parameters such as acid gas loading, linear velocities, gas processing rates, operating pressures, and

operating temperatures.

PROCESS DESCRIPTION

Figure 1 shows the typical process streams and vessels of the DGA unit. Sour gas associated

with H2S and CO2 enters the feed filter separator to remove solid particles. Then, the sour gas enters the

contactor from bottom and as it rises to the top, it contacts lean DGA that flows to the base of thecolumn. When H2S and CO2 are transferred to the DGA, it is then referred to as rich DGA. The sweet

gas goes to gas compression area.

The rich DGA goes to the rich DGA flash drum that has a lower pressure (70 psig or 6 kg/cm2)

than the plant inlet pressure (150 psig or 11.6 kg/cm2). The drop in pressure causes gas to be released

from the rich DGA. This gas, which is called flash gas, goes to the boilers in the utility area as fuel gas.

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Inside the stripper, rich DGA gets rid of H2S and CO2 by utilizing steam. The heat required forstripping is supplied by four steam reboilers and a portion by the reclaimer return. The lean DGA is

returned to the contactor to continue the gas sweetening process. The acid gas leaves from the top of the

stripper to a fin fan cooler. The acid gas and water are separated in a reflux drum before sending the acidgas to sulfur recovery units.

PLANT CORROSION EXPERIENCES

Recently severe thinning and leaks were experienced in the DGA units. By reviewing the

available inspection, corrosion, and process data, it was found that the following locations are sufferingof high corrosion rates:

•  Line between contactor bottom and flash drum

•  Line between flash drum and stripper

•  Lines in the outlet of all reboilers

•  Lines in the outlet of contactor side coolers

•  Reclaimer tubes

•  Flush drum control valves

Areas of high velocity or turbulence such as reducers (located upstream and downstream ofcontrol valves) and elbows experienced high corrosion rates. Simply, increasing the gas processing rate

will definitely increase the amine circulation rate. Figure 2 shows the metal loss of an elbow upstream of

a flash drum’s level control valve. The metal loss was significantly increased after year 2000 as highergas feed rate was introduced to the gas treating units. The microscopy examinations specified the root

cause of this increase in metal loss as erosion attack due to high velocity.

METHODOLOGY

Over 25 years, the subject gas plant had several process changes that include increasing plantthroughputs, increasing water amount associated with gas, and H2S and CO2  levels in the feeding gas.

The number of failures has increased with time in the DGA units. Some of these failures occurred inlocations not classified as high corrosion locations because they were not included in the inspection

 program such as utilities lines. Other failure locations were found approximately a meter away from the

OSI points. Also, it was found that all OSI points were not modified since the start-up of the units (25years ago). Obviously, these points are not representative of the current critical locations, especially

after increasing the units’ throughputs.

The repetitive failures necessitated the engineering team to re-evaluate the system to develop an

evaluation method that enhances process engineers, corrosion engineers, and inspectors to maintain a

reliable system. Figure 3 presents the developed method that can be simplified in the following steps:

•  Review the process parameters and piping material.

•  Identify the suspected corrosion type (damage mechanism).

•  Include critical locations in the OSI program with specific non-destructive testing (NDT)method.

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•  Classify a corrosion control method to be used such as coating, upgrade utilized material, or

modify design (process modification).

The developed method is in line with API 5702 and API 580

3. This method is considered as the

road map for evaluating the existing systems. Applying of this method supports in identifying criticallocations in proactive manner. This paper will present in detail three cases reflecting the beneficial and

successful of this methodology in evaluating corrosion mechanisms in gas treating units and preventing

occurrence of additional failures.

CASE STUDIES

Case Study 1: Rich DGA Piping Spools

The rich DGA piping spool downstream of the level control valve (Figure 4) of the Flash Drumwas evaluated since it is an area subject to severe wall thinning. Inspection history showed that the

 piping spool downstream of the flash drum level control valve had experience a leakage. However, OSI

data did not report severe wall thinning. Also, the history showed all flash drums’ level control valves inthe four gas treating units had experienced severe damage.

Based on RBI study results, the rich DGA piping spool was identified as a critical circuit.

Accordingly, the circuit was evaluated using the above method. During the reviewing of the circuit process parameters, it was found that H2S and CO2 levels are 13500 ppm and 3.7 mol% respectively.

The line velocity was calculated by Computational Fluid Dynamics (CFD) program. The CFDresults (figures 5a and 5b) indicated that the control valve and the reducer have experienced high

velocities in the range of 19 ft/s (8.4 m/s). Also, it indicated that the 12 o’clock position had

experienced back flow which caused turbulence at this location after three years of increasing the plantthroughput.

The material of the reducer downstream of the control valve is carbon steel. Aramco internalguidelines and API 945

9 recommend both lean and rich amine velocities less than 6 ft/s (1.8 m/s). API

5718 recommends rich amine velocity between 3-6 ft/s (1-2 m/s) for rich amine and 20 ft/s (6 m/s) for

lean amine lines. Accordingly, the linear velocity of the reducer is considered as a very high velocity.

Therefore, the reducers are subject to severe metal loss based on the first and second steps of theevaluation method.

Third step in the evaluation method is reviewing the OSI data. OSI locations identified for thatcircuit were found at 3 and 9 o’clock positions. Historical data did not reveal severe metal loss at 3 and 9

o’clock positions. CFD data, Figures 5a and 5b showed the back flow at 12 o’clock position. The visual

inspection and UT measurement during the shutdown showed severe erosion-corrosion at the 12 o’clock

 position which confirms the CFD data. This shows that OSI selected points (3 and 9 o’clock) are not themost appropriate locations and 12 o’clock should be monitored.

CFD results also showed the velocity of the rich DGA main pipe upstream and downstream of

the control valve is lower than 6 ft/s (2 m/s). Visual examination and UT measurement of these linesrevealed no severe metal loss with linear velocity less than 6 ft/s (2 m/s). This supports the internal

Aramco guidelines and API 5718 that allow rich DGA velocity up to 6 ft/s (2 m/s).

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It is worth to mention that evaluating the lean DGA lines using the above methods indicatedsome piping spools reached up to 17 ft/s (5 m/s) without severe metal loss. Only severe metal loss was

found in locations that have velocities higher than 25.2 ft/s (8.4 m/s). This finding support API 5718 that

allows lean amine velocity to maximum of 20 ft/s (6 m/s).

To successfully provide maximum integrity assurance to the units, a combination of upgrading

the material and frequent UT inspection were recommended:

.

•  Regular UT measurements are recommended at the 12 o’clock position.•  Reducers downstream of the control valve are upgraded to type 316 stainless steel

•  The main rich DGA line should remain carbon steel.

Case Study 2: 75 psig Steam Line

Running the gas treating units over the original design impacts the utilities streams such as 75

 psig steam lines as well as the process streams. The 75 psig steam is used in the stripper’s reboilers and

the reclaimer to increase the DGA temperature and reduce H2S and BHEEU level in DGA. Therefore,

75 psig is essential for DGA processing and may cause unit shutdown if the steam line has a failure.

The 75 psig steam lines in the gas treating units were evaluated using the developed method. Theconstruction material of these lines is carbon steel schedule 40. The calculated line velocity at themaximum operating conditions is around 216 ft/s (65.8 m/s). This is above the maximum allowable

velocity required by internal Aramco guidelines of 175 ft/s (53.3 m/s). Accordingly, this high velocity

could cause erosion of the steam lines.

Utilities lines are not included in the plant OSI program. Also, 75 psig steam lines cannot be

inspected by the conventional UT machines since these lines are very hot and thermally insulated.

Visual inspection was used exclusively to inspect these lines. During the turnaround of one of the unit,three windows were opened in the 75 psig steam line for visual inspection. The inspection reveled that

very thin areas located at 9-12 o'clock position of the line. Figures 6 and 7 show detailed views of two

thinned areas. The pattern of thinning suggests a form of erosion or impingement. The thinned areaswere bright and shiny upon opening, whereas most of the section showed a dark grey color, typical of

the appearance of a well-passivated steam-system surface (magnetite film).

Failure analysis of a defective piping sample was performed to identify the damage mechanisms.

The root cause was related to excessive steam velocity, but other factors may have contributed namely:

•  Possibility of some condensation, giving wet steam and possible impingement.

•  Reports of loud noises as hammering that indicates water presence (condensation) in the system

As a result of applying the evaluation method steps, following corrective action was

recommended to provide maximum integrity assurance of 75 psig steam piping in amine treating units:

•  Conduct visual inspection and UT measurements on the 75 psig steam line during futureturnaround.

•  Consider installing extra steam traps to reduce chances of wet steam.

•  Conduct a monthly survey on all steam traps installed in the 75 psig steam system and fix/replace as required to eliminate oxygen contamination.

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•  Evaluate the adequacy of the existing steam traps for handling the increased steam condensation

load versus the original design.

•  Maintain the line velocity below 175 ft/s which can be achieved by increasing steam piping sizes

as per internal company guidelines.

Case Study 3: DGA Reclaimer Tube

Lean DGA requires continual reclaiming to convert BHEEU degradation products back to DGA.

All gas treating units use reclaimer (kettle type heat exchanger) with lean DGA in the shell side andsteam in the tube side. Each reclaimer has 951 tubes and made from carbon steel (shell side) and type304 stainless steel (tube side). BHEEU is converted back to DGA at temperature around 360°F (182°C).

Operating reclaimer at higher temperature will convert DGA to morphaline (irreversible product).Reclaimers are quite tolerant--60% of the tubes can be plugged before there is a significant impact.

Impurities such as chloride can cause pitting and stress corrosion cracking to type 304 stainless

steel materials. According to the unit analysis, chloride level in lean DGA is usually in the range of 100-200 ppm but sometimes it reaches above 600 ppm. Based on Aramco experience, chloride level is

maintained less than 1000 ppm. Limited information is available in the literature about the

recommended chloride level in DGA. API 945 indicated that type 304 stainless steel can be exposed to

DGA solutions containing chloride up to 4000 ppm without specify the system temperature   9. As ageneral rule, chloride SCC of process equipment occurs only at temperature above 145°F (65°C)

10.

However, the following presented case dose not support the proposed API limits.

Reviewing the reclaimers’ historical inspection data revealed that two tube bundles were

replaced by new ones. The other two tube bundles have between 309 and 449 tube plugged. Also,history showed a few bundle failures occurred during shutdown periods, when Maintenance pulled out

the tube bundle. Because of these frequent tubes failures, reclaimers were evaluated utilizing the

developed methodology.

Based on the reclaimer process parameters, equipment material, and inspection history, all

susceptible damage mechanisms were identified. The most common damage mechanisms that have beenexperienced are:

•  Pitting corrosion

•  Fretting Corrosion

•  Chloride stress corrosion cracking

•  Mechanical damage

Pitting and chloride stress corrosion cracking had been experienced in the reclaimer tubes. Theexperience of Saudi Aramco and other oil companies showed cracking developed in the units, when

chloride level reaches higher than 500 ppm. Fretting corrosion in reclaimer was at the interface between

tube bundle and baffle surfaces under load. Agitation resulting in the movement of the tubes against the baffle surfaces was probably caused by the downward flow of the DGA solution through the reclaimershell. Mechanical Damage was taking place during installation and removing of tube bundles due to

improper handling.

From the history of all reclaimer units, it can be noticed that sludge accumulation at the bottom

of each unit has direct impact on tube failures. All reclaimer units are equipped with sparging steam line

which is installed below the reclaimer tube bundle. The main advantage of the sparging steam line is

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 preventing settling of the accumulated sludge and solids around the reclaimer tube bundle. In addition,the sparging line is helpful in removing sludge at the end of the reclaimer cycle. Failure analysis

examinations refer corrosion of the DGA reclaimer as a result of:

•  Excessive reclaimer cycle period

•  Improper boil down procedure at the end of each cycle

•  Excessive flux rates of the tube bundle

•  High chloride content

Sometimes, the reclaimer ran with insufficient level. The low liquid level on the shell side

usually gives the chance for the upper tubes to be hotter than lower tubes that will subsequently increase

the possibility of corrosion occurrence at the upper tubes. According to the operational history of thereclaimers, bottom tubes and mostly upper tubes have experienced failure.

Currently, the OSI program is monitoring lean DGA piping feeding and coming out of the

reclaimer. Reclaimers’ tubes are not included in the OSI program because of accessibility. As a result,the following targets of process parameters are used to monitor reclaimers’ tubes corrosion:

•  Solids target is less than 100 ppm

•  Chloride target is less than 500 ppm

•  BHEEU target is less than 6%

•  Morphaline target is less than 10%

•  Acid gas loading target is less than 0.4% mole acid/mole DGA

•  DGA concentration target is between 47-50%.

•  DGA concentration “in steam return condensate drum” should be 0.

By following the evaluation methodology, the following recommendations were proposed tocontrol the failure mechanisms in the DGA reclaimers:

•  Utilize higher corrosion resistance material such as type 316 stainless steel with reclaimer’s

tubes.•  Maintain liquid level above tubes during normal operation to prevent upper tube form over

heating.

•  Use sparging steam line in the reclaimer every 40-60 days in order to control sludgeaccumulation.

•  Maintain chloride level below 500 ppm in the lean DGA. Controlling chloride at lower limit like

100 to 150 ppm will help on controlling pitting corrosion and chloride stress corrosion cracking.

•  Consider limiting maximum heat flux rates rather than average flux rates. The maximum heat

flux for type 304 stainless steel is 12,000 BTU/hr/ft2 6

.

•   New tube bundles should be designed in a way to maintain a minimum vibration inside reclaimershell. This will minimize fretting corrosion.

CONCLUSIONS

It is clear that increasing of gas processing rates in amine treating units must not be done withoutconsidering the effects this will have on corrosion performance. This corrosion evaluation must be one

 part of a thorough (Management of Change) review. During the evaluation, it was noticed that different

corrosion mechanisms attacked the amine treating units; however, the most likely corrosion type

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classified as the root cause is erosion/corrosion attack due high stream velocities. In this paper, amethodology was introduced that can assist in controlling corrosion in amine treating units. This

methodology calls for an evaluation of the process parameters including pH, pressure, and temperature.

Also, an attention to stream velocity since it plays a major role of most erosion/corrosion attack. Inaddition, OSI program must be optimized to ensure accurate measurements of piping and vessels wall

thickness. Not all corrosion mechanisms can be detected by conventional UT measurement, but

selecting the most appropriate NDT method is essential to detect corrosion before a failure. Corrosion

control options for these systems include materials selection, improved chemical treatments, reduction in

line velocities, and careful process control will help on having a safe and reliable system.

ACKNOWLEDGMENTS

The authors wish to recognize Yousif Al-Said, Mohammed Al-Anazi, and Salamah Al-Anazi,from Saudi Aramco who assisted in this study.

REFERENCES 

1.  M.K. Seubett and G. D. Wallace, “Corrosion in DGA Gas Treating Plants” Corrosion 85. 1985.2.  API 570” Piping Inspection Code”.3.  API 580 “Risk Based Inspection”.

4.  Malcow Huval and Harry Van De Venne “Gas Sweetening in Saudi Aramco in Large DGA

Plants”, Gas Conditioning Conference, 1981.5.  A M. Al-Zahrani, Y. A. Al-Said, A. A. Al-Safran and H. Busalih “75 PSI Steam Line Erosion in

Gas Treating Units”, Saudi Aramco Report, 2004.6.  T. F. Moore, J. C. Digman, and F. L. Johnsone, Jr “A Review of Current Diglycolamine Agent

Gas Treating Applications”, Engineromental Progress, Vol. 3, No.3, 207-212 (1984).

7.  R. B. Nilsen, K. R. Lewis, J. G McCullough and D. A. Hansen, “Corrosion in Refinery AmineSystem” Corrosion 95, paper 571.

8.  API 571 “Damage Mechanisms Affecting Fixed Equipment in the Refining Industry”.9.  API 945 “Avoiding Environmental Cracking in Amine Unit”.

10. J. Guzeit, R. D. Merrick, L. R. Scharfstein, “Corrosion in Petroleum Refining and PetrochemicalOperations, Metals Handbook, 9 Edition, Vol. 13.

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Figure 1: Process flow diagram of amine treating unit.

0.6

0.62

0.64

0.66

0.68

0.7

0.72

Jan-93 Oct-95 Jul-98 Apr-01 Jan-04Date

   T   h   i  c   k  n  e  s  s ,

   I  n  e  c

   h

 1 mpy

10 mpy

Figure 2: Corrosion rate of an elbow upstream of a flash drum control valve.

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 Figure 5a: Computational fluid dynamics program results.

Turbulence

Figure 5b: Close-up of piping spool downstream of the level control valve.

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 Figure 6: Detail view of defective 75 psig steam line.

Figure 7: Close picture shows localized corrosion attacking 75 psig steam line.

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