+ All Categories
Home > Documents > Operational Excellence SStSuccess Story

Operational Excellence SStSuccess Story

Date post: 10-Apr-2022
Category:
Upload: others
View: 1 times
Download: 0 times
Share this document with a friend
15
Operational Excellence S St Success Story Clairefontaine PM 6: Energy Savings in Paper Machine Vacuum Systems Jussi Lahtinen RTS ALLIANCE PO Box 1775 Dahlonega, GA 30533 PaperCon 2011 Page 1521
Transcript
Page 1: Operational Excellence SStSuccess Story

Operational ExcellenceS StSuccess Story

Clairefontaine PM 6: Energy Savings in Paper Machine Vacuum Systems

Jussi Lahtinen

RTS ALLIANCEPO Box 1775

Dahlonega, GA 30533

PaperCon 2011 Page 1521

Page 2: Operational Excellence SStSuccess Story

Clairefontaine Mill Overview

• Clairefontaine paper mill is located north-east of France in EtivalC a e o ta e pape s ocated o t east o a ce t a(approx 1 hour from Strasbourg)

PaperCon 2011 Page 1522

Page 3: Operational Excellence SStSuccess Story

Clairefontaine Mill Overview

• Clairefontaine paper mill is founded 1858T hi (PM5 d PM6) ith t t l it f• Two paper machines (PM5 and PM6) with total capacity of 160 000 mt/year

• Main paper grades:- Uncoated Woodfree/Freesheet- Uncoated Woodfree/Freesheet Cut Size/Copy Paper- Envelope PaperEnvelope Paper- Specialty Uncoated Woodfree/Freesheet

• Non integrated mill

PaperCon 2011 Page 1523

Page 4: Operational Excellence SStSuccess Story

Paper Machine PM6

• Installed 1974, last rebuilt 2004• Twin-wire forming section and tri-nip press with 2 x shoe presses

(new press section installed 2004)• Size press• Trim width 3 4 m max speed 1 000 m/minTrim width 3.4 m, max. speed 1,000 m/min• Total capacity: 100,000 mt/y• Grades produced: Uncoated woodfree/freesheet.

PaperCon 2011 Page 1524

Page 5: Operational Excellence SStSuccess Story

Project Background

• Sealing water system was totally open so there was a pressure to close the system This would have meant:close the system. This would have meant:- Cooling towers- New piping- Increased water pumping costs- Chemical treatment

• Old vacuum system with liquid ring pumps started to be worn out y q g p pso there was lack of vacuum capacity

PaperCon 2011 Page 1525

Page 6: Operational Excellence SStSuccess Story

Old Vacuum System

PaperCon 2011 Page 1526

Page 7: Operational Excellence SStSuccess Story

Old Vacuum System

PaperCon 2011 Page 1527

Page 8: Operational Excellence SStSuccess Story

Project Scope

• Two variable speed turbo blowers replaced the existing system, this consisted of 6 water ring vacuum pumpsthis consisted of 6 water ring vacuum pumps.

• The mill decided to keep 2 of the old water ring pumps as back-ups, the others were dismantled

( )• New horizontal model water separators (2 pcs)• Oil lubrication units for the blowers• Vacuum system engineeringVacuum system engineering• Installation supervision, start-up and process optimization

PaperCon 2011 Page 1528

Page 9: Operational Excellence SStSuccess Story

New Technology - Variable Speed Turbo Blower

• 30….60 % power savings in the vacuum systemE t i t ll t fit i ti• Easy to install or retrofit existing vacuum pumps

• Water free solution• Excellent option when rebuildingExcellent option when rebuilding

the vacuum system• Easy and quick to optimize• Pumping energy recoverable• Pumping energy recoverable• Corrosion free materials• Economical system to operatey p• Fast and easy maintenance

PaperCon 2011 Page 1529

Page 10: Operational Excellence SStSuccess Story

Features- Variable Speed Turbo Blower

• Variable speed control, controls the vacuum level S t il d t t h i hi d• System easily adapts to changes in machine speed, grammage and felt age without the need of bleed valves

• Wide air capacity range eliminates bleed valves• Impeller mounts directly to the motor shaft• No gearbox is needed• Speeds up to 10 500 rpm• Speeds up to 10 500 rpm• Oil lubrication unit for the bearings• Online condition monitoringg

PaperCon 2011 Page 1530

Page 11: Operational Excellence SStSuccess Story

Compact Size Minimized Civil Work

PaperCon 2011 Page 1531

Page 12: Operational Excellence SStSuccess Story

Serial Connected Turbo #2 Unit – High Vacuums

WATER SEPARATOR

EXHAUST AIR

VARIABLE SPEED BLOWER

OIL LUBRICATION UNIT

PaperCon 2011 Page 1532

Page 13: Operational Excellence SStSuccess Story

New Vacuum System

PaperCon 2011 Page 1533

Page 14: Operational Excellence SStSuccess Story

Results

• Energy saving 840 kW (45% of the original situation)C l t i f th li t t th t b bl• Complete saving of the sealing water system, as the turbo blower process is dry. Water savings totally 770 000 m³/year

• More vacuum flexibility on the paper machine• Vacuum flexibility increased for the paper machine vacuum

system, enabling better runnibility. This was by increasing or reducing HiVac or LowVac levels according to the process needs.

• Vacuum levels are very stable and levels can be controlled from the DCS

• Annual savings 500 000 USD/yearAnnual savings 500 000 USD/year• ROI approx 2 years

PaperCon 2011 Page 1534

Page 15: Operational Excellence SStSuccess Story

Thanks for your Attention!

PaperCon 2011 Page 1535


Recommended