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Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate...

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Reduce Scrap at the Extrusion DMAIC Plastec-Stream
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Page 1: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Reduce Scrap at the Extrusion

DMAICDMAIC

Plastec-Stream

Page 2: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

DMAICDMAIC

Page 3: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

DMAICDMAIC

Grinder

Regrind SILOSRegrind

Polystyrene

Color ConcentrateFeeders

Winder

S-wrap

Mandrel

Die/Air Ring

Primary Extruder

Secondary Extruder

ScreenButane

Blender

Foam Rollstock

Testing

Page 4: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Project Progress Overview

D1.Project Charter• Problem statement.• Primary Metric• Goal statement• Purpose and scope• Team

D2 SIPOC

D3 CTQ: Roll stock Specs

M0 Measure outcomes

M1.Extrusion Current Process Map

M21 Summary of descriptive statistics on daily Extrusion scrap

M22 Control charts

M3 Actual yield, cost and process sigma and goals.

M41 Extrusion Scrap per cause

M42 Causes Tree Diagram

A0 Analyze outcomes

A1 Detailed process map

A2 Vital Few Identification

Pareto and Regression Analysis

A31 T- test conclusionA32 Hypothesis test on Vital Few Causes

A33 Root Cause Analysis

Fishbone Diagram

A4 List of Identified and verified main root causes of scrap.

I0 Improve outcomes

I1 Possible solutions to verified root causes.

I2 Evaluate and select

best solution(low

risk/high reward)

I3 Pilot and test solutions.• Actual key perf.indicator

Vs baseline test

I4.Implement the optimized process model.

C0 Control outcomes

C1. Sustain the improvement:

control and monitoring plan:

control chart

Key Deliverables: • Project Charter• Key performance

indicator • Defined goal• Project timeline

• Baseline calculation.• Target performance

outputs calculation.• Identify all x causing

problems.

• Vital few causes• Cause and Effect

results.• Regression model

• Optimal solution.• Pilot and test.• Implementation

• Monitoring and control.• Ownership

Milestone:Planned

Completed

1/4/2014 1/26/2014 2/16/2014 3/16/2014 4/6/2014

1/25/2014 2/15/2014 3/15/2014 4/5/2014 5/26/2014

Steps:

Tools: Project charter. SIPOC CTQ Tree diagram.

Daily scrap data Descriptive statistics. Control chart Capability analysis Brainstorming Process map

Detailed process map Pareto analysis Regression Analysis Hypothesis test. Fishbone/5 Whys

Brainstorming Impact/Effort & cost

Matrix Descriptive statistics Control chart. Capability study.

Control plan. Visual management

tools Mistake proof methods Control Charts SOP/ODS

Define Measure Analyze Improve Control

RoadmapRoadmap

Day 21 21 28 21 21

Cumulative(%) 18.75 37.50 62.50 81.25 100.00

Time and progress:

Page 5: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

In Scope:Extrusion Department

Defect: Rollstock scrap.

Metric :LBS rollstock scrap per day

Business Case: Plastec-Stream Inc ,a packaging company that mainly produce egg cartons, has an excessive amount of rollstock sheet scrap at the Extrusion department.

This create a loss in raw materials and a big challenge on delivering on time customer orders.

Problem Statement:

Manufacturing and delivering on time egg cartons can

not be sustained with the tremendous amount of scrap(Average 3,326 LBS/day) which cost more than

$3,357 per day or $1,208,520 a year.

Goal Statement: Reduce Extrusion line daily scrap from 3,325 LBS to 1500 LBS by end of June 2014 for a saving of $544,320 a year.

Start / Stop Points for Project: Extrusion Silos /Extrusion S-wrap Station

Define - Step D1Define - Step D1

Team/Key Stakeholder.• Ben Williamson Plant Manager Sponsor• Dennis Prayer QA Manager Champion• Ted Davis Extrusion Mgr Subject

Expert• Donatien Toni Lean Six Sigma Black Belt• Sipola Ongewe Lean Six Sigma Black Belt

Project Charter

Page 6: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Define - Step D2Define - Step D2Extrusion SIPOC Map

SIPOC Suppliers   Inputs   Process   Outputs   Customers   Requirements

           

Blender 

 

ScrewsSegment Weight

Crystal Polystrene  

Raw materials Virgin Forming Thickness

Suppliers ColorDie

Foam sheet (Rollstock)

   

Talc Cell size

Butane Printing  

MandrelColor

 

Grinders Regrind Orientation

 S-wrap

 

 

Winder In specs

External Customers

Page 7: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Outcome of Measure Phase

The Goal of Measure Phase – To establish current baseline:• Current Process Map• Descriptive Statistics

• Daily Scrap Average• Daily Prime Average

• Variation Analysis • Can we trust data we obtain from the process?

• Determine Process Capability• Can we produce a product which will meet the customers tolerances?

• Scrap per cause• Identify our baseline list of scrap causes

Measure-Step M0Measure-Step M0

Page 8: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Measure-Step M1Measure-Step M1

Baseline

Extrusion Current Process Map

Start

Blender

Primary Extruder

Secondary Extruder

Die

Foam Color UniformNot contaminated

Scrap/Regrind

Silos

Regrind,Virgin,Color,ButaneRepelletized

Scrap.

Mandrel

No

Yes

Transfer Screens

Foam sheet in Spec./Shiny

And thick

S-wrap

EndYes

No

Winder

EXTRUDERS DIE MANDREL S-WRAPBLENDER

Air ring

Page 9: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Measure-Step M21Measure-Step M21Baseline Statistics

Extrusion daily yield

720006400056000480004000032000

Median

Mean

58000570005600055000540005300052000

1st Quartile 46877Median 551143rd Quartile 61833Maximum 70937

51628 55557

51704 58096

8890 11697

A-Squared 1.18P-Value < 0.005

Mean 53593StDev 10101Variance 102030627Skewness -0.576500Kurtosis -0.304088N 104

Minimum 27922

Anderson-Darling Normality Test

95% Confidence Interval for Mean

95% Confidence Interval for Median

95% Confidence Interval for StDev95% Confidence I ntervals

Daily Prime(Good Sheet)Date Prime Scrap Yield10/1/13 55536 3594 93.510/2/13 58973 3159 94.610/3/13 39053 1418 96.410/4/13 41844 2793 93.310/5/13 58659 2116 96.410/6/13 55753 1278 97.710/7/13 43299 3614 91.710/8/13 45082 2615 94.210/9/13 63920 2225 96.510/11/13 47917 5416 88.710/12/13 60870 881 98.610/13/13 63668 2282 96.410/14/13 63527 972 98.510/15/13 47258 1524 96.810/16/13 36006 2315 93.610/17/13 48245 3186 93.410/18/13 50529 6793 86.610/19/13 44889 1278 97.2

1st Quartile 1757.0Median 3121.03rd Quartile 4764.0Maximum 7496.0

2970.5 3681.3

2412.8 3612.7

1599.5 2107.4

A-Squared 1.55P-Value <0.005

Mean 3325.9StDev 1818.5Variance 3306791.0Skewness 0.447159Kurtosis -0.848292N 103

Minimum 475.0

Anderson-Darling Normality Test

95% Confidence Interval for Mean

95% Confidence Interval for Median

95% Confidence Interval for StDev

75006000450030001500

Median

Mean

375035003250300027502500

95% Confidence Intervals

Summary Report for Daily Scrap

Mean daily Scrap = 3,326 LBS Mean daily prime = 53,536 LBS

N=103

Period = 10/1/2013 thru 1/24/2014

Page 10: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

• Variation Analysis

• IMR charts determined that the process variation is in control

• Process Capability• Cpk was calculated at 0.64• Well below expected

Baseline on Extrusion Daily Scrap Measure-Step M22Measure-Step M22

Page 11: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Measure-Step M3Measure-Step M3Baseline on yield, cost and goals

Actual/Goal

Scrap(lbs) Yield(%) Cost($) Sigma LevelActual 3,326 93.4 3,357 2.5Goal 1,500 97.3 1,514 3

x-bar 93.4 x-bar 97.3

s 4.79 s 1.45

USL 100 USL 100

LSL 86 LSL 94.6

Sigma Shift (typically +1.5 for long term data)1.5 Sigma Shift (typically +1.5 for long term data)1.5

84121.6 31296.7

8.41% 3.13%

61187.0 31296.7

6.12% 3.13%

145308.6 62593.4

85.47% 93.74%

2.557 3.033

Expected yield (overall) %

Process Sigma Level

Expected yield (overall) %

Process Sigma Level

Process Sigma Level Calculator - Continuous Data

(Assumes that data are normally distributed)

Sample Data (user inputs):

Mean

Standard Deviation

Upper Specification Limit

Lower Specification Limit

Results:

Expected dpm > USL

Expected % > USL

Expected dpm < LSL

Expected % < LSL

Expected dpm (overall)

Expected dpm > USL

Expected % > USL

Expected dpm < LSL

Expected % < LSL

Expected dpm (overall)

Standard Deviation

Upper Specification Limit

Lower Specification Limit

Results:

DailyProcess Sigma Level Calculator - Continuous Data

(Assumes that data are normally distributed)

Sample Data (user inputs):

Mean

Page 12: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Measure-Step M42Measure-Step M42Causes Tree Diagram

SCRAP

Color Change Mechanical Start Up Contaminated Out of Spec Feed Syst. Trash in Die Break Out Butane Issues Runout of Runout of Runout of Shutdouwn

CC MECH SU Regrind(CR) OS Failure(FSF) TD BO BI Regrind(RR) Virgin(RV) Color(RC) SD

Change over Screens Inventory Different 4.5 RPM Low Light CR Trash Not at setpoint Low light Clumps in Inventory

CO Heaters Maint. regrind color Blade dull Compressed Dirty Mandrel Pump not working Hopper Maintenance

CR Mandrel Unschedule Trash Spots on air Water flow Empty Silos Feeder Stop Unschedule

FSF Water flow shutdown Water Sheet Auger Electrical Jams Compressed shutdown

RR Valve Power out 4.5 Amps Feeder Clumps air ` Power out

RC Compressed Operator Pump Trash

Operator air Water flow Shaker Operator

Colorator 4.5 RPM Pressure Compressed

4.5 AMPS Butane air

Power out S-wrap Speed Bent auger

Feeder Talc Feeder Power out

pump Die Gap Feeder pump

Die CC

Air ring

Water leak

Die /mandrel

change

Colorator

Extrusion Scrap per Cause

Page 13: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Outcome of Analyze Phase

Our Objective is to narrow to the vital few1. By looking at each step and seeing where the problems are originating from.

• Detailed Process Map with root cause analysis2. By narrowing down to the vital few using the following tools.

• Pareto Analysis – 80 percent of our Scrap was produced by 20% of the causes • 6 key causes identified

• Regression Analysis – Proved that the six identified were significant • Hypothesis Testing – The vital few were identified (Color Change and Mechanical Issues)

3. Summarizing the root causes of our vital few • By identifying variation of our causes• Root cause analysis

Analyze-Step A0Analyze-Step A0

Page 14: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Analyze-Step A1Analyze-Step A1Detailed Process Map

Root Cause Analysis

Start Blender

· Mix· Butane· Temperature· Pressure· RPM

· Melt temp. Zone 9

Inputs

Controls

PrimaryExtruder

Transfer Screens

SecondaryExtruder

OrMixer Cooler

Die Air ring Mandrel

S-wrap Winder End

RegrindSilos

Virgin,ColorTalc

· Temperature· Zone 1 up to· Zone 6· Ext. RPM· Set point· Butane Flow

Pressure· Transfer· Inlet· Outlet· Delta· Melt Temp.

Temperature· Roter Zone 2· Zone 3-4· Ext. RPM

Temperature· M/C Die Zone 11· Die body zone 12· Zone 13-15· Die Pressure

Ring Pressure

Mandrel· Pressure· Water

Temp.

Speed Speed

Controls Controls

Controls Controls Controls Controls

Controls Controls

· Mix· Pressure· Temperature

· Mix· Pressure· Temperature· RPM

· Mix· Pressure· Temperature

· Mix· Pressure

· Foam· Pressure· Temperature· Water

· Foam Sheet· Foam

Sheet

Inputs

Inputs InputsInputs Inputs

Inputs Inputs

Controls

· Feeders Throughput (speed)

Potential FailuresMech,Feed System Failure (FSF)Contaminated Regrind(CR),Runout of Regrind(RR),Runout of Color(RC),Butane Issues(BI )

EffectColor Change(CC)

Potential FailuresMech (Heater bands,Screens,Pomps,Valves,..) =>Temp./Pressure Issues

EffectWeight/tickness Out of Specs.

Potential FailuresMech (Heater bands,Screens,Pomps,Valves,..) =>Temp./Pressure Issues

EffectWeight/tickness Out of Specs.

Potential FailuresMech,Trash in Die(TD)

EffectColor Change(CC),Breakout(BO),Out of Specs(OS)

Potential FailuresMech(Water flow) =>Cooling Temperature

EffectBreakout(BO),Out of Specs(OS)=>Tickness,Scratches

Potential FailuresMech,Speed Variation

EffectBreakout(BO),Out of Specs(OS) =>Weight,Tickness

Potential FailuresMech,Speed Variation and Testing.

EffectBreakout(BO),Out of Specs(OS)

=>Orientation,Weight,Tichness,Color

Page 15: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Analyze-Step A2Analyze-Step A2Vital Few Identification

Pareto Analysis

82% Of scrap are due to:• Color Change(CC) procedure - 21 %• Mechanical (MECH)Issues – 19 %• Out of Specifications (OS) – 13 %• Start Up (SU) issues - 11 %• Contaminated Regrind(CR) – 9 %• Feed System Failure(FSF) – 9%

Scrap 10662 1436173803 65019 47364 38613 31292 30986 17338 13079Percent 3.1 4.221.5 19.0 13.8 11.3 9.1 9.0 5.1 3.8Cum % 95.8 100.021.5 40.5 54.4 65.6 74.8 83.8 88.9 92.7

Cause OtherRRBOTDFSFCRSUOSMECHCC

350000

300000

250000

200000

150000

100000

50000

0

100

80

60

40

20

0

Scra

p

Perc

ent

Pareto Chart of Cause Regression EquationScrap = 706.534 + 0.978373 CC + 0.91847 MECH + 0.795376 OS + 0.883489 SU + 1.10903 CR + 1.01107 FSF

Coefficients

Term Coef SE Coef T P valueConstant706.534 155.355 4.54786 0.000CC 0.978 0.108 9.08724 0.000MECH 0.918 0.093 9.87326 0.000OS 0.795 0.106 7.53331 0.000SU 0.883 0.125 7.09266 0.000CR 1.109 0.127 8.72552 0.000FSF 1.011 0.136 7.40936 0.000

Summary of Model

S = 810.594 R-Sq = 81.30% R-Sq(adj) = 80.13%PRESS = 69633608 R-Sq(pred) = 79.35%

Regression Analysis

Page 16: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Conclusion from the Hypothesis Testing

Alternate hypothesis (: < There is a difference between the mean of scrap with “tested cause” and mean of scrap without “tested cause”>.

• With α=0.05.Results with P value less than α are more significant.

• The test produced the following P-values:• Scrap vs. Scrap w.CC: 0.004• Scrap vs. Scrap w.Mech 0.010

CC* MECH* OS* SU* CR* FSF*0

100

200

300

400

500

600

700

800

Difference w/o Scrap Cause

Scrap w/o Cause

Pounds of Scrap

Hypothesis Testing on vital few - T-Test

T-test conclusion Analyze-Step A31

Analyze-Step A31

Page 17: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

List of Vital Few Analyze-Step A4

Analyze-Step A4

Problem Vital Few Root Causes

Changeover proceduresGrindng at wrong grinder

Grinder TrashGrinder connected to wrong silos

Color Change(CC) Extruder type(Tandem vs Mixer & Cooler)Mech Running out of raw material(empty containers

Feed System Failure,Clots ,raw material clumps)

6 heating zones on primary extruderButane control system

Compressed air and chilling water supply system

Color Change(CC)

Scrap

Mech

Page 18: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Improve Step I0Improve Step I0

Outcomes of Improve phaseOutcomes of Improve phase

1. Possible solutions to verified root causes

2. Evaluate and select best solution(low risk/high reward)

3. Pilot and test solutions.• Actual key performance indicator Vs baseline test

4. Implement the optimized process model.

Page 19: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Possible solutions Improve Step I1Improve Step I1

Problem Vital Few Root Causes Solution Data

Color Change(CC)

Changeover procedures Changeover schedule by color Scrap per color

Grindng at wrong grinder Dedicate one Extruder to run white (White,Yellow)

Grinder Trash Grinding Matrix and training Scrap per cause

Grinder connected to wrong silos CR

Scrap

Color Change(CC) Extruder type(Tandem vs Mixer & Cooler) Convert E2 to tandem Extruder Cause by Extruder

Mech Running out of raw material(empty containers More failure detection tools CC on M/C vs Tandem

Feed System Failure,Clots ,raw material clumps) (mistake proofing devices/Poke Yoke) Extruder

PM program and training Scrap by cause FSF

6 heating zones on primary extruder

PM program

Scrap by Cause

Mech Butane control system Mech

Compressed air and chilling water supply system

Page 20: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Best solutions Improve Step I2Improve Step I2

1 Grinding Matrix and Training2 PM Program3 Changeover Schedule by Color4 Dedicate one Extruder to run White

5 More Feed System Failure detection Tools6 Convert E2 to Tandem Extruder

Easy

Hard

Impl

emen

tatio

n

Buy more Grinders7

Cost

($)

High

Low

ImpactHigh Low

Impact/Effort & Cost Matrix

Page 21: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Improve Step I3Improve Step I3Implement Solutions

Pilot and Implementation Activities

OK complete = done with no remaining actionsgreen = confirmed with few remaining actionsyellow = confirmed with remaining actions that are on trackred = not confirmed; not yet started; significantly behind schedule

Status Owner Goal Date Notes

1.0 Grinding Matrix and Training OK Dennis Prayer 1/31/20141.1 Develop recycled products and scrap grinding matrix by color1.2 Train Operators how to use it.

2.0 Bi-weekly Changeover Schedule by color OK Ted Davis 2/14/20142.1 Develop a production schedule with changeover by adjacent colors. Adjacents colors = Neighbor colors on the color wheel.2.2 Train and Implement the schedule

3.0 Annual PM Program OK Ken Willis 1/31/20143.1 Develop an Annual PM and Sanitation Cleaning Schedule for Extrusion3.2 Train and Implement the schedule

4.0 Dedecate Extruder E4 to run only White Ted Davis 6/6/2014 Ongoing pilot test phase as 5/19/2014

Pilot and Implementation Tasks listTeam: Ted Davis,Dennis Prayer,Ken Willis,Donatien Toni,Sipola Ongewe and Extrusion

Department Operators.

Page 22: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Improve Step I4Improve Step I4Pilot and Test SolutionsBefore & After Performance Assessment

Have I Reached My Goal?

Scrap(lbs) Yield(%) Cost($) Sigma LevelBefore(Improve) 3,326 93.4 3,357 2.5After(Improve) 1,809 96.2 1,826 3.4

Daily Daily Extrusion Scrap decreased by 46 %

736557494133251791

4800

3600

2400

1200

0

Observation

Individual Value

_X=1809

UCL=4315

LCL=-697

736557494133251791

3000

2000

1000

0

Observation

Moving Range

__MR=942

UCL=3079

LCL=0

I-MR Chart of Scrap

Page 23: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

How Can I Sustain the Improvement?

Control Step C0Control Step C0

Outcomes of Control phaseOutcomes of Control phase

Sustain the improvement:

control and monitoring plan control chart

Page 24: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

Defect MeasurementDaily Extrusion Scrap(lbs) Weight Scrap

How Can I Sustain the Improvement?

• Has the business agreed to accept this process? YES • Who owns the new process? Ted Davis Extrusion Department Manager• Who runs the new process? Ted Davis and Extruder Operators

Has this person(s) been properly trained? YES • Who monitors the new process and metrics? Ted Davis ,Extrusion Operators and QA Department

Turnover to the BusinessTurnover to the Business

Process Control Control Step C1Control Step C1

MonitoringMonitoring

736557494133251791

4800

3600

2400

1200

0

Observation

Individual Value

_X=1809

UCL=4315

LCL=-697

736557494133251791

3000

2000

1000

0

Observation

Moving Range

__MR=942

UCL=3079

LCL=0

I-MR Chart of Scrap

Page 25: Reduce Scrap at the Extrusion DMAIC. Grinder Regrind SILOS Regrind Polystyrene Color Concentrate Feeders Winder S-wrap Mandrel Die/ Air Ring Primary.

APPENDIX

Appendix

1 Grinding Matrix

2 Bi-weekly Changeover Schedule by color

3 Annual PM Program

4 Color wheel


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