+ All Categories
Home > Documents > Use of DoE to increase process understanding of a de ...

Use of DoE to increase process understanding of a de ...

Date post: 16-Oct-2021
Category:
Upload: others
View: 1 times
Download: 0 times
Share this document with a friend
20
Use of DoE to increase process understanding of a de-bromination reaction Evotec AG, API update: 7 June 2018 Francesco Tinazzi Senior Scientist API Development and Manufacturing Aptuit Verona
Transcript
Page 1: Use of DoE to increase process understanding of a de ...

Use of DoE to increase process understanding of a de-bromination reaction

Evotec AG, API update: 7 June 2018

Francesco Tinazzi Senior ScientistAPI Development and ManufacturingAptuit Verona

Page 2: Use of DoE to increase process understanding of a de ...

PAGE

Development of a chemical process

1

Page 3: Use of DoE to increase process understanding of a de ...

PAGE

Ideal Synthetic Route

2

Minimum number of steps Fast and easy Reagents commercially available and cheap High yields Minimum amount of by-products Minimum amount of waste Minimum quantity of solvents Not expensive Robust and Reproducible Low risk of failure No scale up issues No chromatographic purifications High purity of the final product

Page 4: Use of DoE to increase process understanding of a de ...

PAGE

Statistical methods

3

Some statistical tools (PCA, PLS and DoE) can be applied to each step of the development of the chemical route

Advantages: Lower number of reactions Less time, especially if combined with parallel equipment Better understanding of the chemical process Higher precision in the determination of optimal values Knowledge of the critical process parameters Determination of the interactions among studied parameters Evaluation of the robustness of the process

Page 5: Use of DoE to increase process understanding of a de ...

PAGE

Application of Statistical Tools to Chemistry

4

Optimization RobustnessScreening

Understanding Confidence

PCA-PLS: identify best Solvent/base/reagent

combination

DoE Optimization: increase yield and reduce impurity

formation

DoE Robustness: increase confidence of

the process

Verification in Pilot Plant

Page 6: Use of DoE to increase process understanding of a de ...

PAGE

Resistance to statistical tools

5

Despite these advantages, a high resistance to use statistical tools is encountered

Main reasons: We don’t have enough time to do it We can understand everything with a reduced number of

reactions I can change one parameter at time and optimize the reaction We don’t need process understanding: if it works in lab, it will

work in the pilot plant I’m a chemist, not a statistic

Page 7: Use of DoE to increase process understanding of a de ...

PAGE

Case study

6

A case study will be presented where the DoE was applied successfully to a chemical reaction

The reaction was previously tried in lab Some “a priori” considerations were applied to the chemistry No systematic study carried out Process understanding needed to reduce impurity formation Reproducibility and robustness not tested Used parallel equipment to reduce time

Page 8: Use of DoE to increase process understanding of a de ...

PAGE

De-bromination via catalytic transfer hydrogenation (CTH)

7

Catalyst: Pd/C 5% (0.3wt/wt)

Hydrogen donor: formic acid (2eq)

Solvent: 2-propanol

Temperature: reflux (ca.82C)

Conversion: ca. 95%a/a after 3hrs

Page 9: Use of DoE to increase process understanding of a de ...

PAGE

Main Issues

8

Formation of 3 main impurities

Dimer= ca.0.5%

Formyl= ca.2% after 3hrs, ca.4% after 6hrs

Tetrahydro= ca.2% after 3hrs, ca.6% after 6hrs

Total Imps= ca.5% after 3hrs

All impurities (except for the formyl) can react in the following step interfering with the precipitation of the API

Final API obtained contaminated with the wrong crystalline form

Page 10: Use of DoE to increase process understanding of a de ...

PAGE

Initial information

9

High quantity of formic acid used to generate the required amount of hydrogen

High quantity of catalyst needed to obtain a good conversion High amount of formyl imp can be reduced by using a high

amount of catalyst High temperature to increase reaction rate Reaction must be stopped after 3hrs to reduce impurity formation

and degradation of final product

Page 11: Use of DoE to increase process understanding of a de ...

PAGE

DoE on the CTH

10

A DoE was carried out to define better reaction conditions and increase robustness

Objectives: 1. Increase the yield up to 97%2. Reduce each impurity below 0.5% (Formyl<1%)

Four factors considered 1. Quantity of catalyst2. Quantity of formic acid3. Temperature4. Concentration

A yellow Fractional Factorial Design was selected to identify main factors and interactions when not aliased

Ten reactions were carried out using parallel equipment (1block, two center points)

Page 12: Use of DoE to increase process understanding of a de ...

PAGE

Yield

11

Design-Expert® SoftwareYield

Error estimates

Shapiro-Wilk testW-value = 0.957p-value = 0.759A: CatalystB: Formic acidC: TempD: IPA

Positive Effects Negative Effects

0.00 1.96 3.92 5.89 7.85

0

10

20

30

50

70

80

90

95

Half-Normal Plot

|Standardized Effect|

Hal

f-Nor

mal

% P

roba

bilit

y

A-Catalyst

B-Formic acid

AB

Design-Expert® SoftwareFactor Coding: ActualYield (%)

Design points above predicted value98.63

81.74

X1 = A: CatalystX2 = B: Formic acid

Actual FactorsC: Temp = 75D: IPA = 7.5

0.1 0.2

0.3 0.4

0.5 0.6

0.7 0.8

0.9 1

0.1

0.15

0.2

0.25

0.3

84

87.2

90.4

93.6

96.8

100

Yiel

d (%

)

A: Catalyst (wt)

B: Formic acid (eq)Response range between 81.7 and 98.6% Factors affecting the yield:A) CatalystB) Formic acidAB) Interaction Pd-HCOOHHigh conversions: low quantities of formic acid and high quantities of catalystEffect of the catalyst highly reduced when using a low quantity of acid

Page 13: Use of DoE to increase process understanding of a de ...

PAGE

Tetrahydro and Dimer Impurities

12

Tetrahydro (range from 0 to 2.2%)A) CatalystAB) Interaction Pd-HCOOH B) Quantity of formic acid

Dimer (range from 0.02 to 0.33%: A) Catalyst

Design-Expert® SoftwareFactor Coding: ActualOriginal ScaleTetrahydro (%)

Design Points

X1 = A: CatalystX2 = B: Formic acid

Actual FactorsC: Temp = 75D: IPA = 7.5

B- 0.1B+ 1

A: Catalyst (wt)

B: Formic acid (eq)

0.1 0.15 0.2 0.25 0.3

Tetra

hydr

o (%

)

-1

0

1

2

3

4

Interaction Design-Expert® SoftwareFactor Coding: ActualOriginal ScaleDimer (%)

Design Points

X1 = A: Catalyst

Actual FactorsB: Formic acid = 0.55C: Temp = 75D: IPA = 7.5

A: Catalyst (wt)

0.1 0.15 0.2 0.25 0.3

Dim

er (%

)

0

0.1

0.2

0.3

0.4

One Factor

No formation of the impurity

Page 14: Use of DoE to increase process understanding of a de ...

PAGE

Formyl Impurity

13

Response range between 0.19 and 6.9% Factors affecting the formation of the Formyl Impurity:

A) CatalystB) Formic acidAB) Interaction Pd-HCOOH

Design-Expert® SoftwareLogit(Formyl)

Error estimates

Shapiro-Wilk testW-value = 0.730p-value = 0.025A: CatalystB: Formic acidC: TempD: IPA

Positive Effects Negative Effects

0.00 0.43 0.85 1.28 1.70

0

10

20

30

50

70

80

90

95

Half-Normal Plot

|Standardized Effect|

Hal

f-Nor

mal

% P

roba

bilit

y

A-Catalyst

B-Formic acid

AB

Design-Expert® SoftwareFactor Coding: ActualOriginal ScaleFormyl (%)

Design points above predicted valueDesign points below predicted value6.99

0.19

X1 = A: CatalystX2 = B: Formic acid

Actual FactorsC: Temp = 75D: IPA = 7.5

0.1 0.2

0.3 0.4

0.5 0.6

0.7 0.8

0.9 1

0.1

0.15

0.2

0.25

0.3

0

1.4

2.8

4.2

5.6

7

Form

yl (%

)

A: Catalyst (wt)B: Formic acid (eq)

Page 15: Use of DoE to increase process understanding of a de ...

PAGE

DoE results: Summary

14

A strong interaction between formic acid and catalyst was highlighted

The quantity of formic acid was reduced improving the impurity profile, but without affecting the yield

Thanks to the interaction, expensive Palladium was reduced

Solvent didn’t affect the responses, so was reduced, increasing the capacity of the reactor

Page 16: Use of DoE to increase process understanding of a de ...

PAGE

Robustness

15

New conditions were moved towards a more robust region

Pd reduced from 0.3 to 0.15wt/wt

Formic acid from 2 to 1.2eq

New conditions tested on a small scale in lab

Results after 2.5hrs:

o Yield=98.9%

o Tetrahydro imp=n.d.

o Dimer=0.06%a/a

o Formyl imp=0.3%a/a

Page 17: Use of DoE to increase process understanding of a de ...

PAGE

Reaction and impurity kinetic

16

Reaction fast: almost complete conversion after 1hr

Reaction stable with time

No formation of the two impurities after 2.5hrs (effect of reduced formic acid)

0

20

40

60

80

100

0 2 4 6 8 10 12 14

Yield

0

0.1

0.2

0.3

0.4

0.5

0 2 4 6 8 10 12 14

Dimer

Formyl

Page 18: Use of DoE to increase process understanding of a de ...

PAGE

Reaction scale up

17

Reaction tested in the JLR (kilo-labo) giving very good results

Scale up in the Pilot Plant Verona

Obtained 11.3kg of solid product

Yield= ca.75% including crystallization

Assay= 99.75%a/a

Product used to test following steps

Final API obtained with good assay (99.2%w/w) and suitable solid form

No major issues observed

Page 19: Use of DoE to increase process understanding of a de ...

PAGE

Conclusions

18

The DoE was applied successfully to a chemical reaction, reaching the following targets:

Process understanding

Interactions between parameters identified

Yield increased

Impurities reduced

Expensive catalyst loading reduced

Robust region identified

Ca. 1 week work

Reaction moved to Pilot Plant obtaining expected results

Page 20: Use of DoE to increase process understanding of a de ...

Recommended