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Alignment And Stability Of The TPS Storage Ring Auto-tuning Girder System
Tse-Chuan Tseng NSRRC, Taiwan
IWAA’16 , OCT. 6, 2016
1
Outline
• Girder system design briefing • Girders Installation at TPS tunnel • Survey alignment works • Auto alignment preparation and
implementation • Girder stability during commissioning
period • Conclusions
2
The Dedication Ceremony of Taiwan Photon Source Inauguration
5
The Ceremony Officially Made the Facility Available to Researchers Worldwide With 7 beamlines in top-up mode 300mA
Design goals of the girder system for TPS • Firm support and precise positioning of magnets (30mm RMS),
Vacuum Chamber & BPM
• Higher nature frequency (above 30 Hz is better)
• Alignment accuracy between girders within 0.1mm(relative) Traditional alignment network simulation reveals an accuracy of 0.3mm typically. It
needs to be iterated several times to reduce to 0.1mm
• Precise resolution (mm)
Manual adjustment mechanism is of poor resolution and time consuming
• Toward whole ring automatic alignment (optional)
How to align the girders precisely and quickly with less manpower? Considering the deformation of the floor and limited space in the tunnel also frequent earthquakes in Taiwan .
6
A 6-axes motorized adjusting mechanism was thus proposed!
TPS Girder System Timeline
7
Date Event
2004 June TPS feasibility study started
2005 Dec. A preliminary study prototype bending section with 3 girders established
2009 Oct. A nearly real size testing mock-up system was set up in NSRRC lab .
2010~2013 Parts manufacturing, sub-systems assembling and calibration in a rental factory
2012 May A third mock-up system was set up
2013 Jan. Pedestals were to be set out, anchor bolts drilling and installed
2013 July 2 bending sections installed as an on-site mock-up testing system
2013 Oct. Entire system installation began
2014 Mar. The Last girder was craned
2014 Aug. A whole ring girder automatic alignment was really performed
2014 Aug. Phase I accelerator system test and commissioning started
2014 Oct. A second automatic alignment was performed
2014.12.31 First synchrotron light from TPS
Cam mover type adjustment mechanism
8
Girder of Swiss Light Source
From “Handbook of Accelerator Physics and Engineering” Alexander Wu Chao, P377.
From “Precision Machine Design” Alexander H. Slocum, P377.
Types of kinematic mounting
A 3 grooves type kinematic mounting modification to 6 stands girder design
9
One girder system configuration
More contact points with locking system to raise natural frequency and reduce deflection. All contact points persist rolling contact condition when adjusting to reduce friction and
remain high mobility . Contact stress less than elastic limitation to reduce friction wear and keep high reliability
Cam mover type mechanism modification and adjusting algorithm
Two coordinate systems are to be established at girders and movers separately, from the rigid body assumption, the adjustment of center position of each ball can be calculated.
Due to the kinematic V groove type arrangement, the girder moving range in horizontal direction is only ½ of the mover range in horizontal(X) direction (4.5mm) and √3/2 in longitudinal(Z) direction (7mm)
10
Modification of point contact type cam to line contact to reduce stress
Kinematic mounting situation preserved. The contact position of the ball and the cam
remains the same for adjusting algorithm. the contact situation changes from point contact to
line contact. the stress is reduced drastically to 12.4% and far
below the elastic limitation of the cam. Steps of the stepping motor is 5000 and plus with the gearbox ratio of 160, it comes with a resolution of 800000 per turn and also refers to a step resolution of at least 0.03um in girder coordinate system
11
Heidenhain ECN425
harmonic drive 1: 160
constant torque : 35 kg.m
Heidenhain
ECN425
rotary encoder
Magnets assembling on girder design
12
• 3 magnet installation referencing channels precisely machined within 15mm tolerance • The magnet mounting base also precisely machined within 15mm tolerance* • two side channels can keep the magnets on the same height with minimized rotation • the mounting base will be pushed to closely touch the side of center channels with an
inclined clamper • The clamper produces a horizontal pushing force to make sure the magnet base
contact with the certer reference channel • The right screw for the clamper is locked with a constant 1400 kg.cm torque, while
the left screw 1000 kg.cm (with a shim underneath)
Shim
* J. C. Jan, et al., "Magnet Design and Control of Field Quality for TPS Booster and Storage
Ring", IPAC’15.
13
TPS storage ring girder system design
One girder section(1/24) with magnets and vacuum system
One girder section
1/6 ring symmetry super-period configuration
3 kinds and 5 types of girder
Leica Nevil220 tilting sensors
Heidenhain Acanto
AT1218 absolute length gauge
No sensor for length measurement of straight section
Control system Architectures
14
• Each local control system controls 3 girders of a bending section.
• A NI PC-based PXI platform • Consists of 6 sub-systems: 1. cam mover control(18) 2. rotational encoder (18) 3. touch sensor reading(16) 4. tilting sensor reading(3) 5. PSD reading(4) 6. locking control(18)
* H.S. Wang et al, “Design and testing of a girder control system at NSRRC”, ICALEPCS(2011)
With dipole mag. Max.:18um Without dipole mag. Max.:45um
Girder flatness measurement after magnets assembled
15
Natural Frequency and damping testing of the mock-up system at the rental plant
Amplification with damper
The 1st NF can be raised from 24Hz to
33 Hz with locking mechanisms
The Peak amplitude is reduced
with dampers
One girder section was installed with dampers
and locking system for testing
16
TPS tunnel variation during 2012~2013
With the survey data from the sockets at tunnel walls, a small displacement of (-3,-1) and rotation of 0.0021 degree (about 5mm at lattice position) clockwise of the virtual center were derived and a coordinate values adjustment of all components were decided accordingly.
18
Shielding wall (y dir.)
Shielding wall (x dir.)
Pedestal set out, anchor bolts implanting, alignment ,grouting and cam movers installation
19
Started from Jan. 2013
Girder installation deviations
-3.00
-2.00
-1.00
0.00
1.00
2.00
3.00
mm
position
X
-3.00
-2.00
-1.00
0.00
1.00
2.00
3.00
mm
position
Y
-2.00
-1.00
0.00
1.00
2.00
mm
position
Z
before alignment
after alignment
22
Magnet centralizing
• Adjust Position Jig and Circular PSD jig
• Install two position jigs with PSD on girder
• Adjust laser to parallel and have equidistance to girder datum plane
• Replace the Position jig with the quadrupole and sextupole magnets
• Insert Circular PSD jig on the center of quadrupole and sextupole magnets
• The offset of beam position can be detected by PSD
• Insert the steel shims between magnet and girder for error compensation
23
Magnet Centralizing Results
-80.0
-60.0
-40.0
-20.0
0.0
20.0
40.0
60.0
Magnet Error at Vertical Magnets of TPS
-80.0
-60.0
-40.0
-20.0
0.0
20.0
40.0
60.0
Magnet Error At Horizontal Magnets of TPS
RMS 18.53um
RMS 20.42um
24
Most magnets were acceptable but a few were still shimmed after double checked
Girder system completed installation
In May 2013, 2 mockup sections (R19 and R20) were installed at storage ring.
The full ring installation processes began from Oct. 2013 and the last girder was finished installation at March 2014.
25
Control system problems encountered
28
•Motor malfunction → check and changed
•Touch sensor or connector damaged → check and changed
•Touch sensor signal direction inversed → check and adjusted
•Laser optical fiber damaged → check and changed
•Laser holder being moved → check and adjusted
•PSD module holder replaced (conflicted with frontend)
The data base for auto-alignment
• Linear encoder distance measurement data between 2 adjacent girders
• Girder reference point distance measurement data with a laser interferometer
• Laser interferometer distance measurement data compensation chart
• Linear encoder distance measurement data compensation chart
• PSD beam profile curve fitting • PSD1 / PSD2 coefficient
calibration • PSD to linear encoder calibration
29
Girder sensor reading variations with respect to temperature change
1℃ in temperature change induces 0.1mm deviation between girders
30
Laser tracker measurement data
Girder adjusting individually with a laser tracker (a few motor failures encontered)
Girder auto-alignment in 1/3 ring each (1mm drop protection)
-0.50-0.40-0.30-0.20-0.100.000.100.200.300.400.500.600.700.80
SR1
_…
SR1
_…
SR2
_…
SR2
_…
SR3
_…
SR3
_…
SR4
_…
SR4
_…
SR5
_…
SR5
_…
SR6
_…
SR6
_…
SR7
_…
SR7
_…
SR8
_…
SR8
_…
SR9
_…
SR9
_…
SR1
0…
SR1
0…
SR1
1…
SR1
1…
SR1
2…
SR1
2…
SR1
3…
SR1
3…
SR1
4…
SR1
4…
SR1
5…
SR1
5…
SR1
6…
SR1
6…
SR1
7…
SR1
7…
SR1
8…
SR1
8…
SR1
9…
SR1
9…
SR2
0…
SR2
0…
SR2
1…
SR2
1…
SR2
2…
SR2
2…
SR2
3…
SR2
3…
SR2
4…
SR2
4…
:mm
Girder position
TPS SR girder position deviations (2014,7)
Z(Longitudinal)
X(Transverse)
Y(Vertical)
Girder auto-alignment in 1/3 ring each (vertical direction only) 31
Laser tracker measurement data
-0.8
-0.6
-0.4
-0.2
0
0.2
0.4
0.6
0.8
SR1
_G
1-1
SR1
_G
2-3
SR2
_G
1-1
SR2
_G
2-3
SR3
_G
1-1
SR3
_G
2-3
SR4
_G
1-1
SR4
_G
2-3
SR5
_G
1-1
SR5
_G
2-3
SR6
_G
1-1
SR6
_G
2-3
SR7
_G
1-1
SR7
_G
2-3
SR8
_G
1-1
SR8
_G
2-3
SR9
_G
1-1
SR9
_G
2-3
SR1
0_
G1
-1
SR1
0_
G2
-3
SR1
1_
G1
-1
SR1
1_
G2
-3
SR1
2_
G1
-1
SR1
2_
G2
-3
SR1
3_
G1
-1
SR1
3_
G2
-3
SR1
4_
G1
-1
SR1
4_
G2
-3
SR1
5_
G1
-1
SR1
5_
G2
-3
SR1
6_
G1
-1
SR1
6_
G2
-3
SR1
7_
G1
-1
SR1
7_
G2
-3
SR1
8_
G1
-1
SR1
8_
G2
-3
SR1
9_
G1
-1
SR1
9_
G2
-3
SR2
0_
G1
-1
SR2
0_
G2
-3
SR2
1_
G1
-1
SR2
1_
G2
-3
SR2
2_
G1
-1
SR2
2_
G2
-3
SR2
3_
G1
-1
SR2
3_
G2
-3
SR2
4_
G1
-1
SR2
4_
G2
-3
mm
TPS SR girder position deviations (2014,8)
Z(Longitudinal)
X(Transverse)
Y(Vertical)
First girder auto-alignment in full ring
32
-0.80
-0.60
-0.40
-0.20
0.00
0.20
0.40
0.60
0.80
SR1
_G
1-1
SR1
_G
2-3
SR2
_G
1-1
SR2
_G
2-3
SR3
_G
1-1
SR3
_G
2-3
SR4
_G
1-1
SR4
_G
2-3
SR5
_G
1-1
SR5
_G
2-3
SR6
_G
1-1
SR6
_G
2-3
SR7
_G
1-1
SR7
_G
2-3
SR8
_G
1-1
SR8
_G
2-3
SR9
_G
1-1
SR9
_G
2-3
SR1
0_
G1
-1
SR1
0_
G2
-3
SR1
1_
G1
-1
SR1
1_
G2
-3
SR1
2_
G1
-1
SR1
2_
G2
-3
SR1
3_
G1
-1
SR1
3_
G2
-3
SR1
4_
G1
-1
SR1
4_
G2
-3
SR1
5_
G1
-1
SR1
5_
G2
-3
SR1
6_
G1
-1
SR1
6_
G2
-3
SR1
7_
G1
-1
SR1
7_
G2
-3
SR1
8_
G1
-1
SR1
8_
G2
-3
SR1
9_
G1
-1
SR1
9_
G2
-3
SR2
0_
G1
-1
SR2
0_
G2
-3
SR2
1_
G1
-1
SR2
1_
G2
-3
SR2
2_
G1
-1
SR2
2_
G2
-3
SR2
3_
G1
-1
SR2
3_
G2
-3
SR2
4_
G1
-1
SR2
4_
G2
-3
Un
it :
mm
TPS SR girder Position Deviations(2014.10.27)
Z(Long.)
X(Hori.)
Y(Vert.)
Second girder auto-alignment in full ring
Auto alignment processes
33
1. Load laser tracker measurement data (XL,YL) 2. Load touch sensor matrix and calibration coeff. , PSD calibration coeff. ,
girder length… initial data 3. Read touch sensor, PSD, Nivell, Encoder initial data 4. Calculate local dz(longitudinal deviation), dx(transverse deviation) Touch sensor matrix and PSD reading to calculate local (dzs , dxs) Local (dzs , dxs) transfer to global (dXs,dYs) (dXs,dYs) of each girder Calculate new position by average with the laser tracker data
• P2(X_new,Y_new) = ½ *[ P1(XL,YL) + ½ *(dXs1,dYs1) +1/2*(P2(XL,YL)- P1(XL,YL))+ P3(XL,YL) – ½ *(dXs2, dYs2) - 1/2*( P3(XL,YL) - P2(XL,YL) )]
• Calculate all P1(X_new, Y_new)~P72(X_new, Y_new) • Compare with (P1_theory~P72_theory) to calculate adjusting values • Adjust girder 1 of each section and record touch sensor 1st readings • Adjust girder 2 of each section and record touch sensor 2nd readings • Adjust girder 3 of each section and record touch sensor 3rd readings • Accord to the 3 touch sensor readings to calculate the real
movement of each girder • Renew each girder postions P(X’,Y’) = P(X_new,Y_new)+movement
P(dX,dY) • Iteration till converge
-0.800
-0.600
-0.400
-0.200
0.000
0.200
0.400
1 3 5 7 9 11 13 15 17 19 21 23 25 27 29 31 33 35 37 39 41 43 45 47 49 51 53 55 57 59 61 63 65 67 69 71
d_move_x d_move_y d_move_z
SR girder auto alignment first adjustment values
Second adjustment values
Mistakes
To be check
Auto alignment calculated values
The full ring adjustment takes about 1900 seconds (32min) in 5 iteration
longitudinal(mm)
transverse(mm)
34
Girder positions comparison between from sensors and laser tracker
35
0 50 100 150-40
-20
0
20
40
電子
束方
向lo
cal
0 50 100 150-30
-20
-10
0
10
20
垂直
電子
束方
向lo
cal
Longitudinal
Transverse
Due to sensor initial conditions are corrupted, two steps are to be adopted 1. Applied optimizing method to calculate 2. Re-calibration
Booster ring alignment
3 teams with 3 laser trackers and 4 weeks to align the booster ring manually
36
TPS COD before correction
37
1.78 mm rms horizontal 1.04 mm rms vertical
Measured COD with all correctors off After LOCO and BBA
Simulated COD with all correctors off from alignment errors, dipole field errors
* C. C. Kuo, et al., "Commissioning of the Taiwan Photon Source", IPAC’15 .
The measured data were even better shows good alignment conditions
The deviation between girders from a Richter scale 6.6 earthquake
Girder
Section
Max. Deviation Between
Earthquake
Sensor ID
Max. Deviation
After Earthquake
Sensor ID
R1 0.0033 16 0.0015 3
R2 0.0062 16 0.0035 16
R3 0.0025 16 0.0013 7
R4 0.0025 7 0.0013 11(Y)
R5 0.0017 3 0.0016 5(Y)
R6 0.004 3 0.0028 3
R7 0.0052 8 9.00E-04 5(Y)
R8 0.0027 16 0.0015 16
R9 none none none None
R10 0.0054 12 0.0034 16
R11 0.0043 3 0.0034 3
R12 0.0017 16 0.0011 16
R13 none none none none
R14 0.0083 3 0.0026 3
R15 0.0029 16 0.0018 16
R16 0.0018 12 9.00E-04 12
R17 0.0043 16 0.0015 16
R18 0.0016 5(Y) 0.0015 5(Y)
R19 0.0017 12 0.0011 3
R20 0.0078 7 0.0018 8
R21 0.0023 7 0.0019 11(Y)
R22 0.0048 16 0.0039 16
R23 0.0016 8 1.00E-03 8
R24 0.0035 3 0.002 3
38 However, the intensity in Hsinchu is only 2~3
Laser tracker measurement data(2015-2016)
-1.00
-0.50
0.00
0.50
1.00SR
1_
G1
-1
SR1
_G
3-1
SR2
_G
2-1
SR3
_G
1-1
SR3
_G
3-1
SR4
_G
2-1
SR5
_G
1-1
SR5
_G
3-1
SR6
_G
2-1
SR7
_G
1-1
SR7
_G
3-1
SR8
_G
2-1
SR9
_G
1-1
SR9
_G
3-1
SR1
0_
G2
-1
SR1
1_
G1
-1
SR1
1_
G3
-1
SR1
2_
G2
-1
SR1
3_
G1
-1
SR1
3_
G3
-1
SR1
4_
G2
-1
SR1
5_
G1
-1
SR1
5_
G3
-1
SR1
6_
G2
-1
SR1
7_
G1
-1
SR1
7_
G3
-1
SR1
8_
G2
-1
SR1
9_
G1
-1
SR1
9_
G3
-1
SR2
0_
G2
-1
SR2
1_
G1
-1
SR2
1_
G3
-1
SR2
2_
G2
-1
SR2
3_
G1
-1
SR2
3_
G3
-1
SR2
4_
G2
-1
Un
it :
mm
TPS SR Girder Position Deviations (X Transverse)
ALL2015-06-08_USMN(RMS = 0.22 mm)
SR2015-07-13_USMN(RMS = 0.27 mm)
SR2016-01-04_USMN(RMS = 0.19 mm)
SR2016-07-06_USMN(RMS = 0.25 mm)
-1.00
-0.50
0.00
0.50
1.00
SR1
_G
1-1
SR1
_G
3-1
SR2
_G
2-1
SR3
_G
1-1
SR3
_G
3-1
SR4
_G
2-1
SR5
_G
1-1
SR5
_G
3-1
SR6
_G
2-1
SR7
_G
1-1
SR7
_G
3-1
SR8
_G
2-1
SR9
_G
1-1
SR9
_G
3-1
SR1
0_
G2
-1
SR1
1_
G1
-1
SR1
1_
G3
-1
SR1
2_
G2
-1
SR1
3_
G1
-1
SR1
3_
G3
-1
SR1
4_
G2
-1
SR1
5_
G1
-1
SR1
5_
G3
-1
SR1
6_
G2
-1
SR1
7_
G1
-1
SR1
7_
G3
-1
SR1
8_
G2
-1
SR1
9_
G1
-1
SR1
9_
G3
-1
SR2
0_
G2
-1
SR2
1_
G1
-1
SR2
1_
G3
-1
SR2
2_
G2
-1
SR2
3_
G1
-1
SR2
3_
G3
-1
SR2
4_
G2
-1
Un
it :
mm
TPS SR Girder Position Variations (Y Vertical)
ALL2015-06-08_USMN(RMS = 0.32 mm)
SR2015-07-13_USMN(RMS = 0.33 mm)
SR2016-01-04_USMN(RMS = 0.31 mm)
SR2016-07-06_USMN(RMS = 0.23 mm)
儲存環磁鐵Girder定位與設計差值 Z,X,Y=±0.50 mm -1.00
-0.50
0.00
0.50
1.00
SR1
_G1
-1
SR1
_G3
-1
SR2
_G2
-1
SR3
_G1
-1
SR3
_G3
-1
SR4
_G2
-1
SR5
_G1
-1
SR5
_G3
-1
SR6
_G2
-1
SR7
_G1
-1
SR7
_G3
-1
SR8
_G2
-1
SR9
_G1
-1
SR9
_G3
-1
SR1
0_G
2-1
SR1
1_G
1-1
SR1
1_G
3-1
SR1
2_G
2-1
SR1
3_G
1-1
SR1
3_G
3-1
SR1
4_G
2-1
SR1
5_G
1-1
SR1
5_G
3-1
SR1
6_G
2-1
SR1
7_G
1-1
SR1
7_G
3-1
SR1
8_G
2-1
SR1
9_G
1-1
SR1
9_G
3-1
SR2
0_G
2-1
SR2
1_G
1-1
SR2
1_G
3-1
SR2
2_G
2-1
SR2
3_G
1-1
SR2
3_G
3-1
SR2
4_G
2-1
Un
it :
mm
TPS SR Girder Position Deviations (Z Longtudinal)
ALL2015-06-08_USMN(RMS = 0.26 mm)
SR2015-07-13_USMN(RMS = 0.28 mm)
SR2016-01-04_USMN(RMS = 0.24 mm)
SR2016-07-06_USMN(RMS = 0.27 mm)
Ground Variation Due to Temperature and Tide
40
10M quartz glass bar on 4 girder section
Commissioning team found there is about 90~100um circumference variation correlated to daily environment temperature change and tide
Conclusions
• TPS girder system including storage ring, booster ring and transport line were finished installation August 2014.
• A laser tracker survey data based full ring auto-alignment had been performed and shows good conditions for smoothly commissioning and the stability is still good during 2 years operation.
• The laser tracker survey results show that the full ring accuracy is about ± 0.5mm.
• The sensor’s durability is quite a problem for the auto-alignment system, however, the quartz glass bar test shows a feasible solution toward the sensor based girder auto-alignment.
41