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ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name...

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Factory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5 th Follow Up 31/10/2016 Date of 11 th Follow Up 17/09/2018 Report Received Date 17/08/2014 Date of 6 th Follow Up 03/01/2017 Date of 12 th Follow Up 25/03/2019 Date of 1 st Follow Up 06/03/2015 Date of 7 th Follow Up 04/04/2017 Date of 13 th Follow Up Date of 2 nd Follow Up 29/12/2015 Date of 8 th Follow Up 20/07/2017 Date of 14 th Follow Up Date of 3 rd Follow Up 20/04/2016 Date of 9 th Follow Up 18/12/2017 Date of 15 th Follow Up Date of 4 th Follow Up 29/06/2016 Date of 10 th Follow Up 08/04/2018 Date of 16 th Follow Up Item No Accord Inspection Observation Accord Action Plan (Recommendation ) Accord Time line (given in report ) Comments from Accord (After Physical Inspection ) Final Timeline (Approved timeline ) Final Action Plan (Factory) Progress Status (On the date of inspection ) Pictorial Evidence 1 Wiring drawn through flexible PVC conduit is not firmly fixed. Provide cable tray or PVC pipe instead of flexible pipe to support the cables. 3 WEEKS On 06/03/2015: Corrected. '20/02/2015 Corrected as per follow- up inspection on 6th March, 2015 Corrected 2 Phase barrier/ separators between different phases are not installed. Phase barriers between different phases supplied by the breaker manufacturer must be installed to avoid arc flashing. 3 WEEKS On 06/03/2015: Corrected. '31/08/2015 Corrected as per follow- up inspection on 6th March, 2015 Corrected Note: Inspected by ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12 th ) Palash Kumar Paul Electrical Safety Inspection dates Garib & Garib Company Ltd. Vogra, Gazipur Other Factory: Page 1 of 20
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Page 1: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

Factory Name

Address

Factory ID 9490

Initial Inspection Date 17/04/2014 Date of 5th

Follow Up 31/10/2016 Date of 11th

Follow Up 17/09/2018

Report Received Date 17/08/2014 Date of 6th

Follow Up 03/01/2017 Date of 12th

Follow Up 25/03/2019

Date of 1st Follow Up 06/03/2015 Date of 7

th Follow Up 04/04/2017 Date of 13

th Follow Up

Date of 2nd

Follow Up 29/12/2015 Date of 8th

Follow Up 20/07/2017 Date of 14th

Follow Up

Date of 3rd

Follow Up 20/04/2016 Date of 9th

Follow Up 18/12/2017 Date of 15th

Follow Up

Date of 4th

Follow Up 29/06/2016 Date of 10th

Follow Up 08/04/2018 Date of 16th

Follow Up

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

1

Wiring drawn through

flexible PVC conduit is

not firmly fixed.

Provide cable tray or PVC pipe

instead of flexible pipe to support

the cables.

3 WEEKS On 06/03/2015: Corrected. '20/02/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

2

Phase barrier/ separators

between different phases

are not installed.

Phase barriers between different

phases supplied by the breaker

manufacturer must be installed to

avoid arc flashing.

3 WEEKS On 06/03/2015: Corrected. '31/08/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

Note:

Inspected by

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Palash Kumar Paul

Electrical Safety Inspection dates

Garib & Garib Company Ltd.

Vogra, Gazipur

Other Factory:

Page 1 of 20

Page 2: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

3

Panel doors not

connected with earth

bond.

Provide earth connection for

panel doors of metallic

distribution boards using green

cables preferably braid so that the

metallic door remains at zero

potential all the time.

3 WEEKS On 06/03/2015: Corrected. '30/09/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

4Not enough working

space around the panel.

Maintain enough working space

around the panel. 12 WEEKS On 20/04/2016: Corrected. '20/02/2015

Corrected as per follow-

up inspection on 20th

April, 2016

Corrected

5

11kV HT cable is not

supported and Cable laid

on concrete floor without

mechanical guard.

Install cable duct with cover to

protect the HT cables as well as

prevent the ingress of debris, dust

and lint.

12 WEEKS On 06/03/2015: Corrected. '30/09/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

Page 2 of 20Garib & Garib Company Ltd.

Page 3: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

6Transformers are

guarded with grill.

The transformer must be installed

with barrier walls (instead of grill)

between transformer and other

panels. The walls must be fire

resistant and should have height

up to the ceiling or Assign a

qualified engineer to design a

required transformer room

according to BNBC, Section-2.6.3.

25 WEEKS On 29/12/2015: Corrected. '30/09/2015

Corrected as per follow-

up inspection on 29th

December, 2015

Corrected

7

Oil cup below

transformer breather is

empty.

Breather oil cup must be filled

with transformer oil to required

level as instructed by the

manufacturer.

3 WEEKS On 06/03/2015: Corrected. '30/09/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

8

Joint in down conductors

of lightning arrester are

not spliced firmly.

Mid-length joints in earth down

conductor must be avoided.12 WEEKS On 06/03/2015: Corrected. '20/02/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

Page 3 of 20Garib & Garib Company Ltd.

Page 4: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

9Generator output cable is

not supported.

Cable must be supported by cable

tray or ladder with cover to ensure

the mechanical protection of the

cables.

12 WEEKS On 06/03/2015: Corrected. '23/05/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

10

Panel entering or leaving

changeover switches is

not supported and not

firmly fixed.

Cable entering or leaving

changeover switch must be

supported by cable ladder and

must be firmly fixed.

12 WEEKS On 06/03/2015: Corrected. '30/09/2015

Corrected as per follow-

up inspection on 6th

March, 2015

Corrected

11

New Finding:

Heat source is close to

cable channel.

Need to maintain at least 900mm

distance between cable channel

and heat source or provide proper

insulation to disallow the heat to

transfer into the electrical cable

channel.

2 Months On 29/12/2015: Corrected. '31/10/2015

Corrected as per follow-

up inspection on 29th

December, 2015

Corrected

Page 4 of 20Garib & Garib Company Ltd.

Page 5: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

12

New Finding:

Circuit is drawn without

incorporating any

protection or circuit

breaker.

All circuits shall be drawn with

protection/ circuit breaker at both

end.

3 Months

On 20/04/2016: Not Corrected. New

Timeline 30/05/2016.

On 29/06/2016: Not corrected.

Factory is behind the timeline.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Corrected

'30/05/2016 Corrected Corrected

13

New Finding:

Multiple cables

terminated at MCCB

terminals/ Bus bar.

Terminate each power cable at

single terminal and use proper

sized cable lug. Multiple cables

termination is allowed if all are

soldered properly and powering to

a single circuit.

1 Month

On 20/04/2016: Corrected.

On 29/06/2016: Corrected at

previous follow up but this issue raise

again because of poor maintenance.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Corrected

'30/04/2016 Corrected Corrected

14

New Finding:

Electrical Single Line

Diagram (SLD) has

inadequate information

which has no

effectiveness.

Prepare SLD more informative

thus anyone can understand it.2 Months

On 20/04/2016: Not Corrected.

On 29/06/2016: Not corrected.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017:Not Corrected.

On 08/04/2018:Not corrected. Do cable

identification properly.

On 17/09/2018: Not Corrected.

Factory should resubmit SLD to ACCORD

for another Review with CAD file.

On 25/03/2019: Not Corrected.

'30/09/2016

We already completed

the SLD with Cable

Identity but due to set

up of new jacquard

machine and floors SLD

will change.

In Progress

Page 5 of 20Garib & Garib Company Ltd.

Page 6: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

15

New Finding:

Battery terminals are left

open.

Use insulated rubber cap to cover

all the battery terminals1 Month On 29/12/2015: Corrected. '20/02/2015

Corrected as per follow-

up inspection on 29th

December, 2015

Corrected

16

New Finding:

Cables terminated at

electrical bus bar/

MCCB without cable

lugs.

Terminate all the

power/earth/neutral cable with

proper sized cable lug

1 Month

On 29/12/2015: Corrected.

On 29/06/2016: Corrected at

previous follow up but this issue raise

again because of poor maintenance.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Corrected.

'29/12/2015

Corrected as per follow-

up inspection on 04th

April, 2017

Corrected

17

New Finding:

MCCBs are not adjusted

accordingly.

Adjust all the MCCBs according

to cable ampacity (connected

load). Avoid using different sized

cable at the terminals.

2 Months

On 20/04/2016: Not Corrected.

On 29/06/2016: Not corrected.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Corrected

'15/07/2016 Corrected Corrected

Page 6 of 20Garib & Garib Company Ltd.

Page 7: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

18

New Finding:

Lightning Protections

System (LPS) is

inadequate for the

factory.

Redesign/modify LPS for your

factory to increase safety.3 Months

On 20/04/2016: Not Corrected. New

Timeline 30/05/2016.

On 29/06/2016: Not corrected.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected. Metal

bonding is not done in proper way, Earth

pit, shed building and lift roof was not

accessible to verify.

On 08/04/2018: Not corrected. LPS

design/drawing shall be adequately

informative. Inadequate conductor joint. Air

terminal installation distance not

maintained. Due to civil work all earth pits

are not prepared properly.

On 17/09/2018: Not Corrected.

On 25/03/2019: Corrected.

'30/05/2016 Completed Corrected

19

New Finding:

Cable duct/ channels are

allowing to be filled with

fluffs (Lint/ dust).

Clean all the cable channels/ducts;

then seal them for permanent (you

may use checkered/ perforated

plate at the bottom). But ensure

that you have used proper sized

cable for all of your electrical

loads.

2 Months

On 20/04/2016: Not Corrected. New

Timeline 30/05/2016.

On 29/06/2016: Not corrected.

On 31/10/2016: Not Corrected.

On 03/01/2017: Corrected.

'30/05/2016

Corrected as per follow-

up inspection on 3rd

January , 2017

Corrected

20

New Finding:

Thermo graphic scanning

of the entire electrical

system is due.

Thermo graphic scanning for the

entire electrical system must be

performed on a bi-annual basis

and recorded

2 Months

On 29/12/2015: Corrected.

On 29/06/2016: Corrected at previous

follow up but this issue raise again because

of poor maintenance.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected. Hot spot

also found

On 08/04/2018:Not corrected. Ambiguity

found in repot.

On 17/09/2018: Not Corrected.

On 25/03/2019: Corrected.

'30/09/2015 Completed Corrected

Page 7 of 20Garib & Garib Company Ltd.

Page 8: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

21

New Finding:

Insulation resistance test

and earth resistance test

of electrical equipment is

not performed.

Insulation resistant test and earth

resistance test of all the cables

must be performed once every 1

year cycle and recorded (this must

require a complete power shut

off)

2 Months On 20/04/2016: Corrected. '30/09/2015 Corrected Corrected

22

New Finding:

Earth lead cable/ Earth

Continuity Conductor

size is inadequate/ under

size.

Resize earth lead cable/ECC for

LT panel/MDB/DB; follow

BNBC 2006 Part 8 chapter 2

section 2.8 for sizing your earthing

cables (Usually ECC should be

equal to the half of the respective

phase cable).

2 Months

On 29/12/2015: Corrected.

On 29/06/2016: Corrected at

previous follow up but this issue raise

again because of poor maintenance.

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Corrected

'30/09/2015 Corrected Corrected

23

New Finding:

No space around

transformer for

performing any

maintenance work

Ensure minimum 1.07m working

space around the transformer1 Month On 29/12/2015: Corrected. '23/05/2015

Corrected as per follow-

up inspection on 29th

December, 2015

Corrected

Page 8 of 20Garib & Garib Company Ltd.

Page 9: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

24

New Finding:

No separation between

LT panels and HT units

(Transformer, HT

switchgear ).

Make a brick built separation

between LT and HT units; ensure

that after making separator you

have adequate ventilation (cross

ventilation) and working clearance

around each electrical equipment

1 Month On 29/12/2015: Corrected. '23/05/2015

Corrected as per follow-

up inspection on 29th

December, 2015

Corrected

25

New Finding:

Generator body has been

earthed by inadequate/

improper sized (type)

cable.

Ensure minimum two earthing

connection for generator body

(consult with your generator

supplier).

2 Months On 20/04/2016: Corrected. '10/03/2016

Corrected as per follow-

up inspection on 20th

April, 2016

Corrected

26

New Finding:

No/ Inadequate rubber

(insulation) mat on the

working are of

distribution board/

Panel.

Put electrical insulation (rubber

mat, thickness minimum 5mm) on

the working area of each electrical

installation (Transformer/LT

panel/MDB/DB/SDB/ other

manual operated machineries).

1 Month On 31/10/2016: Corrected. '25/07/2016

Corrected as per follow-

up inspection on 31

October, 2016

Corrected

Page 9 of 20Garib & Garib Company Ltd.

Page 10: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

27

New Finding:

Boiler room has poor/

inadequate ventilation.

Ensure cross ventilation for boiler

room. 2 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Not Corrected.

On 03/01/2017: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

28

New Finding:

(1)Cables in service are

joined (splicing) between

terminations.

(2)Unterminated

wire/busbar is kept

inside the electrical

panel/cable tray.

(1)Joints of cable shall be avoided.

For unavoidable cases, existing

cables with joints must be spliced

using butt splicing kits and then

should be insulated with electrical

tapes. Joints must be supported

and protected.

(2)All unterminated wires/busbar

shall be removed.

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Not corrected since

electrical renovation work is going on at

several places.

On 17/09/2018: Not Corrected.

On 25/03/2019: Not Corrected.

'09/09/2016 In Progress

29

New Finding:

Cables are hanging

without proper support.

Use ladder type cable tray to

support cables at any where to

keep cable out of tension or

arrange adequate support.

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 04

April , 2017

Corrected

Page 10 of 20Garib & Garib Company Ltd.

Page 11: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

30

New Finding:

Panel/ Distribution

boxes are not readily

accessible .

Take necessary initiative thus

every panel/distribution board

can be easily accessible

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Not Corrected.

On 03/01/2017: Not corrected.

On 04/04/2017: Not Corrected.

On 20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Not corrected

On 17/09/2018: Not Corrected.

On 25/03/2019: Corrected.

'09/09/2016 Completed Corrected

31

New Finding:

(1)Transformer Body

earthing is inadequate.

(2)Neutral earthling is

not separated from body

earthing of the electrical

system.

(1)Two separate and distinct earth

connection & one separate and distinct

Neutral connection must be provided

for Transformer. Transformer body

must have earth connection with half

of phase conductor. Or follow

manufacturer/ suppliers

recommendation.

(2)Need to improve the earthling

system for the whole electrical system

so that neutral earthling is separated

from body earthling of the electrical

system.

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 31

October, 2016

Corrected

32

New Finding:

(1)MCCB/ MCB is

installed without any

enclosure.

(2)Three phase MCCB

connected to control two

phases or less.

(1)All MCCBs/ MCBs must put inside

the end-closer made of non-

combustible material preferably metallic

sheet to protect the cables from

physical damage as well as prevent

entering debris, dust and lint.

(2)Check and redesign the requirements

to control the circuits. If three phase

control is not required, then replace

with suitable control devices.

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 31

October, 2016

Corrected

Page 11 of 20Garib & Garib Company Ltd.

Page 12: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

33

New Finding:

Electric safety training

program is not initiated/

conducted.

Electrical safety training and

awareness program for the

electrical personal and workers

must be initiated and

recorded(NFPA 70E may be

followed).

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Not Corrected.

On 03/01/2017: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

34

New Finding:

(1)Power bus bar/

MCCB are installed

congested; and power

cables touch opposite

phased bus bar.

(2)Phase separators

between phases are not

installed.

(1)Ensure that no power cable

touches bare bus bar. Use

insulated bus bar (just covering

existing bus bar by heat shrink)

(2)Phase barriers between phases

must be installed.

1 Month

Timeline extended from 09.08.2016 to

09.09.2016

On 31/10/2016: Corrected.

'09/09/2016

Corrected as per follow-

up inspection on 31

October, 2016

Corrected

35

New Finding:

Transformer Silica gel is

discolored.

Silica gel shall be changed; or

reuse can be done, if color regains

after sundry.

1 Month On 03/01/2017: Corrected. '10/12/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

Page 12 of 20Garib & Garib Company Ltd.

Page 13: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

36

New Finding:

Cables passing through

wall/ floor slab are not

protected at the entry/

exit point(s).

Cables passing through permanent

wall/ floor slab must be protected.

Floor to floor openings shall be

sealed by proper type materials

(consult with fire expert).

1 Month

On 03/01/2017: Not corrected. New

committed timeline is given till

10/02/2017.

On 04/04/2017: Corrected.

'10/02/2017

Corrected as per follow-

up inspection on 04

April , 2017

Corrected

37

New Findings:

Change Over Switch

contacts covered with

bearing grease.

Clean excess grease from the

contacts. Use of grease may be

avoided as it collects (sticks) dusts

on the contacts. Otherwise

electrically contact grease could be

used.

1 Month On 03/01/2017: Corrected. '10/12/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

38

New Finding:

Distribution boards are

filled with fluffs

(Lint/dust).

Distribution board must be kept

neat and clean; these must be

sealed properly thus no scope of

ingression of fluffs.

1 Month On 03/01/2017: Corrected. '10/12/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

Page 13 of 20Garib & Garib Company Ltd.

Page 14: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

39

New Finding:

Earthing terminals are

filled with rust and left

open.

Earthing terminals must be

covered/capped and rust must be

cleaned.

1 Month On 03/01/2017: Corrected. '10/12/2016

Corrected as per follow-

up inspection on 03

January , 2017

Corrected

40

New Finding:

Power cables are bent

excessively.

Power cables must be installed as

straight as possible; in unavoidable

case not less than 135 degree

bending can be allowed.

1 Month

On 03/01/2017: Not corrected. New

committed timeline is given till

10/02/2017.

On 04/04/2017: Not Corrected. On

20/07/2017: Not Corrected.

On 18/12/2017: Not Corrected.

On 08/04/2018: Not corrected

On 17/09/2018: Not Corrected.

On 25/03/2019: Corrected.

'10/02/2017 Completed Corrected

41

New Finding:

Cable trench is found

wet and cables are not

arranged properly.

Cable trench must be kept always

dry, and shall be covered by

checkered plate. Cable should be

arranged properly and should use

cable tray/ ladder inside cable

trench.

1 Month

On 03/01/2017: Not corrected. New

committed timeline is given till

10/02/2017.

On 04/04/2017: Corrected.

'10/02/2017

Corrected as per follow-

up inspection on 04

April , 2017

Corrected

Page 14 of 20Garib & Garib Company Ltd.

Page 15: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

42

New Finding:

Periodicity of

Transformer Oil Test

(dielectric strength,

moisture content and

flash point) survey is not

continued.

Transformer oil test (dielectric

strength, moisture, and flash point

test for oil) shall be done at least

once in a year. If the operation of

transformer is 24/7 in the facility

twice in a year is a better practice.

1 Month

On 08/04/2018: Not corrected.

Prepare report adequately.

On 17/09/2018: Found Corrected.

'30/01/2017 Corrected Corrected

43

New Finding:

Insulation resistance

record (cable

information) doesn't

match with field.

Field information must be

reflected in the record and

significantly lower sized cables'

record shall be avoided.

1 Month

On 08/04/2018: Not corrected.

Prepare report adequately.

On 17/09/2018: Not Corrected.

Insulation resistance test of electrical

power cables is manipulated

On 25/03/2019: Corrected.

'30/01/2017 Completed Corrected

44

New Finding:

Power Cables are

hanging without proper

support.

Power cables must be supported

by cable tray (ladder- where

needed). Outdoor arrangement

must be covered.

1 Month

On 08/04/2018: Not corrected

On 17/09/2018: Not Corrected.

On 25/03/2019: Outdoor cable shall

be covered.

'30/01/2017 In Progress

Page 15 of 20Garib & Garib Company Ltd.

Page 16: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

45

New Finding:

Inadequate working

clearance around the

transformer/s

Maintenance movement

is obstacle due to

improper cable trench

cover in the utility area

(Generator/Substation/

Boiler/Compressor).

Working clearance around each

transformer shall be 1.07m. If

multiple transformers are installed

then the gap between two

transformers must be equal to the

width of bigger transformer.

Covered cable trench must be

equal to working floor height. If

not, extended area must be sloped

at both sides to avoid obstacle.

1 Month

On 08/04/2018: Not corrected.

Installation must comply with multiple

equipment accommodation

recommendation.

On 17/09/2018: Not Corrected.

On 25/03/2019: Not Corrected.

'30/01/2017

Factory already got

approval of the drawing

of transformer room

from accord. (Required

from accord fund)

In Progress

46

New Finding:

Cable channel/duct

terminals are left open

for ingression of lint,

dust or fluffs.

Power cables inside cable

trench are buried by

sand/soil & concrete.

cable ducts must be properly

sealed to avoid ingression of any

foreign particles.

Power cables should not be buried

directly in any case. If it is not

designed through sand/soil &

concrete, removal of sand/soil &

concrete must be done.

1 Month On 25/03/2019: Not Corrected. '29/10/2018 In Progress

47

New Finding:

No policies for PPE &

LOTO (Lock-Out-Tag-Out)

are introduced for safety of

the personnel during any

kind of maintenance work.

Uninsulated electrical tools

are used by maintenance

personnel in the factory

Electric safety training

program document is not

enriched enough.

Need to introduce and implement PPE

& LOTO policy with LOTO (Lock-

Out-Tag-Out) device instead of any

other means to ensure safety of the

personnel during any maintenance.

Need to keep all records of using

LOTO.

For maintenance purposes, all the

electrical tools shall be properly

insulated and these insulations shall be

checked periodically.

It is a periodic task which factory has to

continue to improve overall electrical

safety situation for the staffs.(Factory

may follow NFPA 70E)

1 Month On 25/03/2019: Not Corrected. '29/10/2018 Completed In Progress

Page 16 of 20Garib & Garib Company Ltd.

Page 17: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

48

New Finding:

Panel doors are not

connected with earth.

All metal installation which are

part of electrical system must be

connected to earth to avoid

electrical shock or electrocution.

1 Month On 25/03/2019: Corrected. '29/10/2018 Completed Corrected

49

New Finding:

Distribution boards have no

clear identification markings.

Instruction for CPR

(Cardiopulmonary

Resuscitation) or Electrical

shock restoration is not

present.

No/Inadequate rubber

(insulation) mat at the

working area of distribution

board/panel.

All distribution boards, switchboards,

sub main boards and switches shall be

marked clearly for proper identification.

CPR instruction shall be hanged near

all electrical installations (LT panel,

MDB, FDB, DB, SDB) at visible

location

Electrical insulation (not less than 3

mm thick in case of rubber mat) at the

working area of each electrical

installation (Transformer/LT

panel/MDB/DB/SDB/ other manual

operated machineries) must be ensured.

1 Month On 25/03/2019: Corrected. '29/10/2018 Completed Corrected

50

New Finding:

Manually operated

machines (may have

chance to be touched by

operator/user) have no

earth connection.

Each manually operated machine

(may have chance to be touched

by user/operator) must have earth

connection. Cable selection shall

be made per CB response and

circuit's power demand.

1 MonthOn 25/03/2019: All metal shall be

connected to earthing.'29/10/2018 In Progress

Page 17 of 20Garib & Garib Company Ltd.

Page 18: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

51

New Finding:

Lead acid battery

terminals are left open &

kept in combustible

material.

MCCB is installed

without any enclosure.

Lead acid battery terminals must

be covered/capped and rust must

be checked and cleaned.

Remove the combustible material

Each MCCB/MCB must be

enclosed by proper type material.

the material must not be more

than 18 SWG graded.

1 Month On 25/03/2019: Corrected. '29/10/2018 Corrected

52

New Finding:

Hazardous lights in store

room / storage areas are

uncovered.

Hazardous lights in store room /

storage areas shall be covered by

proper type material; or non-

hazardous lights shall be installed

in these areas.

1 Month On 25/03/2019: Not Corrected. '29/10/2018 In Progress

53

New Finding:

Gland holes in cable base

plates left open.

Gland holes not used for cable

entry shall be sealed with blanking

plates or plugs & clean

panel/distribution board

periodically.

1 Month On 25/03/2019: Corrected. '29/10/2018 Completed Corrected

Page 18 of 20Garib & Garib Company Ltd.

Page 19: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

54

New Finding:

Earth Pit resistance

record is manipulated.

All earthing systems shall be tested

for resistance on any dry day not

less than once in every two years.

A record of every earth test made

and the result shall be kept for not

less than two years and shall be

available to the Inspector when

required.

1 Month On 25/03/2019: Corrected. '29/10/2018 Completed Corrected

55

New Finding:

Phase barrier/separators

are missing in MCCBs.

Phases must be separated by

insulator (a rubber type no-

flammable materials shall be used

for it)

1 Month On 25/03/2019: Not Corrected. '29/10/2018 In Progress

56

New Finding:

Motor connection

terminal left exposed.

Provide motor terminal box and

terminate all power cables in its

termination point. The enclosure

of motor shall be such that no

dust/ other particles can enter

into it.

1 Month 30/04/2019

Page 19 of 20Garib & Garib Company Ltd.

Page 20: ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT … ELECTRICAL SAFETY INSPECTION.pdfFactory Name Address Factory ID 9490 Initial Inspection Date 17/04/2014 Date of 5th Follow Up 31/10/2016

ELECTRICAL SAFETY FOLLOW UP INSPECTION REPORT (12th)

Item

No

Accord Inspection

Observation

Accord Action Plan

(Recommendation )

Accord Time line

(given in report )

Comments from Accord

(After Physical Inspection )

Final Timeline

(Approved

timeline )

Final Action Plan (Factory)

Progress Status

(On the date of

inspection )

Pictorial Evidence

57

New Finding:

The size of copper

busbar used as

connection point of

multiple grounding

electrode conductors is

inadequate.

The copper or aluminum busbar

used for junction of multiple

grounding electrode conductors

shall not be less than 6mm thick X

50mm wide and of sufficient

length to accommodate the

number of termination necessary

for the installation.

1 Month 30/04/2019

Page 20 of 20Garib & Garib Company Ltd.


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