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1 Hospet Steels Limited DRIVING INNOVATION Infinite resolve September 1 st & 2 nd – 2010 Chennai. 11 th National Award for “Excellence in Energy Management – 2010” Team Leader : Mr.Ananda Bhattacharjee - DGM Energy Managers : Mr.Naresh - Manager : Mr.Y.D.Guruprasad – Dy.Mgr Green field project conceived in 1995. Strategic Alliance between “Mukand” & “Kalyani” groups to produce world class Alloy steel. Both the groups are Leaders in Alloy & Special Steels. Capacity : 7,00,000 MT /Annum. HSL product ranges are - Bloom - Billet - Rolled products Energy Cost as % of Manufacturing cost is 53. ISO TS 16949, ISO 14001, OHSAS 18001 & TPM certified company. COMPANY PROFILE Infinite resolve DRIVING INNOVATION
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Page 1: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

1

Hospet Steels LimitedDRIVING INNOVATION Infinite resolve

September 1st & 2nd – 2010 Chennai.

11thNational Award for “Excellence in Energy Management – 2010”

Team Leader : Mr.Ananda Bhattacharjee - DGM

Energy Managers : Mr.Naresh - Manager

: Mr.Y.D.Guruprasad – Dy.Mgr

Ø Green field project conceived in 1995.Ø Strategic Alliance between “Mukand” & “Kalyani”

groups to produce world class Alloy steel.Ø Both the groups are Leaders in Alloy & Special

Steels.Ø Capacity : 7,00,000 MT /Annum.Ø HSL product ranges are - Bloom - Billet - Rolled

products Ø Energy Cost as % of Manufacturing cost is 53.Ø ISO TS 16949, ISO 14001, OHSAS 18001 & TPM

certified company.

COMPANY PROFILEInfinite resolveDRIVING INNOVATION

Page 2: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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IRON ORE COKE FLUXES

MINI BLAST FURNACE (250M³ X 2 Nos.& 350M3X 1Nos)

ENERGY OPTIMISING FURNACE50 T CAPACITY

IRON & STEELSCRAP

(15–30%)

FERRO LLOYS

REFINING

FLUX ( LIME &

DOLOMITE )

VD50/55 T

O2 BLOWING

FERRO ALLOYS

REFINING

TRIMMING OF CHEMISTRYUNDER VACUUM

CLOSED STREAM CASTING

LF-1 50 T

LF-250 T

BLOOM CASTER10/18 m Radius

BILLET CASTER9/16 m Radius

ROLLING MILL750 mm, 2Hi

CLOSED STREAM CASTING

CPP

PROCESS FLOW

15 min

10 min

3 min

4 min

Total HM Transfer time – 32 min

ENERGY CONSERVATION PROJECTS IMPLEMENTED IN

LAST 3 YEARS

DRIVING INNOVATION Infinite resolve

Hospet Steels Limited

Page 3: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

3

Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

1

Reduction of LPG & O2consumption in CCM byoptimizing cutting torch speed &idle movment

2007-08 - - 40% 70 Nil Immediate 1.24

2 Automation of Mould Cooling pump2007-08 660000 43.74 - - 29.7 8 months 495

3 Modification of M/C cooling pump impeller

2007-08 403325 19.81 - - Nil Immediate 302.49

4 RMS Furnace Cooling Pump impeller design change

2007-08 176514 8.0 - - 0 Immediate 132.38

Total Carbon Reduction in Tons ofCO2 annualy

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

5

Auto switch off of EMS, sensingthe mould level (if any one strandis stopped during other strandsare running)

2007-08 5760 0.26 - - Nil Immediate 4.32

6 Reduction of power in BloomMould Cooling system SMS utility 2007-08 224437 10.23 - - 32 38 168

7 Installation of heat exchanger inbloom mould cooling system

2007-08 14175 10.65 - - 32 3 10.63

8 Installation of turbo ventilators 2007-08 328000 6.232 - - 4 8 246

9Auto switch OFF of Billet spraywater pump after teemingcomplition.

2008-09 189000 8.9 - - Nil Immediate 141.75

10Auto Partial closing of Bloomspray water pump delivery valveafter teeming complition.

2008-09 33220 1.56 - - Nil Immediate 24.91

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Page 4: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

11Auto stop of turret hydraulicpump motors after 15 minutes ofits start

2008-09 10072 4.5 - - Nil Immediate 7.55

12

Auto stop of steam exhaustmotor after completion of heateven in manual mode in Billetcaster

2008-09 29190 1.3 - - Nil Immediate 21.89

13

Auto stop of steam exhaustmotor after completion of heateven in manual mode in Bloomcaster

2008-09 45780 2.06 - - Nil Immediate 34.33

14

Extra bends has been reduced inBloom mould line to get 5Cu.Mtrs of extra water in all threestrands & to run only 2 mouldwater pumps in all grades.

2008-09 79200 3.72 - - 1 4 months 59.4

15 Installation of VFD drives forBillet RORT,RRT & DRT motors

2008-09 68640 3.2 - - 14 5 Years 5.15

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

16Utilization of waste heat fromtundish to preheat Sub EntryNozzle. (LPG saving)

2008-09 - - 41040 19.44 6 4 months 0.67

17 Wood gassifier for Tundishdrying system

2008-09 - - 68.83 28.22 3.8 1.6 270.26

18 5 m3 Bio gas plant in canteen 2008-09 - - 684 3.24 1.5 6 months 0.011

19 Bio mass stove in canteen 2008-09 - - 684 3.24 0.19 1 month 0.011

20

Running of One No. Machinecooling Pump during Millshutdown, Roll changing, (75kwcapacity) for cooling of watercooled compressor & PowerPack cooling.

2008-09 7200 0.3 - - Nil Nil 5.4

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savings achieved

Page 5: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

5

Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

21

Switching off of Descaler system(110kw motor x 3 Nos) during rollchanging time & blade changingtime (any major breakdown in themill)

2008-09 9887 0.4 - - Nil Nil 7.4

22Using of scale pit water thro'Dualmedia filter for descaling systeminstead of soft water

2008-09 1,12,320 4.49 - - Nil Nil 84.24

23Rerouting of furnace oil pipe line& two burners connected toheater to achieve 85oC at burner

2008-09 - - 138 31.74 1 15 days 338

24

Stoppage of existing 55 kw AirCompressor for power plant bytaking air supply from centralutility

2008-09 462000 20.79 60 34 months 346.5

25 Optimization of Argon in process& leakages arrested 2008-09 - -

0.20 Nm3/MT

29 Nil Immediate

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

26 Interlock for magnetic seperator 2009-10 3212 0.16 - - NIL NA 2.4

27 Impeller trimming of shell coolingpump (MBF 1 & 2) 2009-10 438000 21.9 - - NIL NA 328.5

28 Single GCP pump inplace of two 2009-10 336000 16.8 - - NIL NA 252

29 Stave water reduction 2009-10 96360 4.8 - - NIL NA 72.27

30 Conservation of Nitrogen in BLT 2009-10 42000 M3 1.26 - - 0.04 0.5

31 Gasfier for boiler water heatingsystem 2009-10 - - 135 40.50 6 2 330.9

32 Light tube (day lighting system inPPC & SMS meeting hall) 2009-10 2803 0.15 - - 0.4 31 2.1

33 1kwh Solar photo voltaic cell 2009-10 8760 0.48 - - 3.5 88 6.57

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Page 6: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Pay backPeriod

Kwh Rs.Lac KL Rs.Lac (Months)

34

Stopping continuous loading of TOT motors 2 x 45 kw . Modification is done in PLC logix.

2009-10 147633 6.6 - - Nil Nil 110.72

35

Stopping continuous loading of Grip tilter motor - 1 x 37 kw . Modification done in PLC logix.

2009-10 94907 4.3 - - Nil Nil 71.18

36Auto off operation for RT 1 to 5 Motors.Modification done in PLC Logix.

2009-10 38592 1.7 - - Nil Nil 28.94

37Auto OFF operation in RHF-2 Exit door roller table motors-9 Nos (2.2kw x 9 nos)

2009-10 3208 0.2 - - Nil Nil 2.40

38

Auto Switching Off booster pump(11kw) during hot saw cutting in HVMill.Running machine cooling pump pressure is suffiecent.

2009-10 29568 1.3 - - Nil Nil 22.17

Total Carbon Reduction in Tons ofCO2 annualy

ENERGY CONSERVATION PROJECTS

S.NO Title of Energy ConservationProject Implemented

Investment made(Rs.Lakh)

Year ofImplementation

Annual Energy Savingsachieved

Grand total of Carbon Reduction in 3 years – 3047 MT

Ø Formation of Energy Cell (2006-07) with a Commitment to reduce SE consumption.

ØPlant visits as a part of learning program.

Ø Internal trainings, to bring up the awareness.

Ø Encouraging the Innovative projects.

Ø Implementation through TPM/SIX SIGMA/Lean tools.

Ø Conducting Internal and External Energy/Water audits by CII, Godrej

Ø Taking Environment Management Program (EMP) in ISO 14001 system.

Ø Process audits and Improvements. ex: HM Temp. at EOF, Lime addition optimization etc.

Ø Utilizing waste heat from the systems.

Ø Actions to improve raw material condition at MBFs

Ø Regular review by top management (CEO)

Energy Conservation Efforts in last 3 Years

Page 7: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Benchmarking of SEC

Hospet Steels LimitedDRIVING INNOVATION Infinite resolve

Trend in SE Consumption

5.60

5.46

5.355.31

5.68

5.20

5.40

5.60

5.80

05-06' 06-07' 07-08' 08-09' 09-10'

G C

al/M

T

Benchmarking

5.35Year 2009-10

5.25Target for 10-11

5.38POSCO(World Best)

Gcal RateYear

Global recession

Coke quality HSL Target-5.25

Posco-5.38

Page 8: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

8

Road map to achieve Benchmark 5.25 G Cal/MTProcess Initiative:

1.4

92

7.28

653

As on08-09

0.0131.351.5Ltr/TOptimization of LDO consumption in caster

0.00178890Kwh/MT

Optimization of LRF power consumption

0.052

0.09

Reduction in Gcal/T

5.6

610

Target 10 - 11

6.00

622

As on 09-10

Lit/TReduction in FO Consumption by introduction of copper coil in boiler feed water heating through Gasifier system.

Kg/TOptimization of Coke Rate by enhancing MBP blowers efficiency of MBF 2

UOMActions

Road map to achieve Benchmark 5.25 G Cal/MTProject Initiative:

0.024

0.027

Benefit in SEC

0.000020

0.0001

Reduction in G Cal/T

Saving in PowerDay lighting system in Admin building

Saving in PowerReplacement of Electric Geyser with Biomass water heating system

BenefitActions

Total expected saving in G Cal – 0.154

Page 9: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Innovation Leads to Excellence

DRIVING INNOVATION Infinite resolve

Hospet Steels Limited

v Investment = Rs. 5 Lakhs v Savings in FO = 0.3 ltr/MTv Saving/Annum = Rs. 45 lakh/annum.v Payback period = 45 days

1.BIOMASS GASSIFIER SYSTEM

100 kg/hr Biomass gassifier

Water heating coil inserted in the chamber

• First time introduced steel industry for heating boiler feed water

• In house development

• Copper coil is being introduced in Aug’10 to improve water temperature

Page 10: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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2. DAY LIGHTING SYSTEM A NEW CONCEPT

v Investment = Rs. 4.7 Lakhs

v Savings in kwh = 9600 kwh/annumv Payback Period = 9 years

Light pipe collects the sun light from the roof and it transmitted to the room without any battery back up.

Before After

During rolling process the bloom size is gradually reduced to finish size by rolling in different passes & these passes have been reduced by increasing the draft from 30 mm to 45 mm.

No of passes before increase in draft = 11

No of passes after increase in draft = 9

Increase in productivity = 6 MT/hr

Savings in FO = 168 Kl p.a

Savings / annum = Rs.47 Lakhs

Payback Period = Immediate.

3. Reduction in Rolling time

Page 11: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

11

4. Reduction Hot Saw blade Changing timeBefore: Hot saw blade cover was being removed and put back by EOT crane. Blade locking Nut was being tightened manually by using hammer.

After: Hinges provided to Blade cover to open & close, EOT crane avoided. Pneumatic torque wrench introduced for tightening blade locking nut.

Hot saw blade change time before modification = 30 mins

Hot saw blade change time after modification = 20 minsNo of blade change = 2 nos/dayPower saving due to reduction in Mill idle time = 91000 unit p.aSavings in FO due to reduction in Mill idle time = 8050 lts p.a

Savings / annum (Power & FO) = Rs.27 Lakhs

Payback Period = Immediate.

Hinges

5. Reduction in Power Consumption of Hyd systemBefore: Two motors of 36 KW each were running in reheating pusher hyd. System

After: Two motors replaced with single motor of 45 KW. Modification done on hydraulic system. Dual pumps (one pump having high flow and low pressure, another pump having low flow and high pressure) connected to single motor.

Power consumption with two motors of 36 KW each = 302400 units p.a

Two motors replaced with Single motor of 45 KW = 189000 units p.a

Savings / annum = Rs.5.67 Lakhs

Payback period = 13 months

Page 12: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Environmental Projects

No of Tree Plantation to protect GHG

26550 27150 2832032575

2400016400

1000

11000

21000

31000

41000

2005-06 2006-07 2007-08 2008-09 2009-10 2010-11

Nos o

f tree

s

% of plantation area

10%20%

33%40% 45% 48%

0%

20%

40%

60%

2005-06 2006-07 2007-08 2008-09 2009-2010 2010-11

Year

%

Approx total power plant project cost503

Depends up on CER rate in the market

Estimated4204766969

Verification audit completed & under going registration.1st year2nd year

BF gas firing system in Boiler #2 of Power plant #2 (U/P)

2

Approx total power plant project investment 280

Depends up on CER rate in the market

69589681355040036854

2006200720082009

BF gas firing system in Boiler #1 of Power plant #1

1

Rs MillionRs Million

Tons of CO2

Invest. Made

Total Annual Savings

Total Carbon

Reduction

Year of Implementation

Title of project

implemented

Sl No

Carbon Emission Reduction initiatives (CDM/VER Projects)

Page 13: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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• Zero water discharge out side the plant premises ensured through 100% effluent treatment and recycling.

• Check dam of capacity increased from 50,000 m3 to 75000 m3 for Rain water harvesting. – 2009-10

• 3 Guard pond are constructed to 100% reuse of wastewater from the plant for various purposes.

• The wastewater generated in cooling of EOF, MBF’s is treated in Thickener & recycled.

• Secondary De-dusting system for controlling Fugitive Emissions at LRF & EOF..

• Canteen waste & House-hold garbage are utilized in bio-gas plant.• STP water is used for plantation through drip irrigation.• ETP treated water used for gardening.• STP cum ETP of capacity 50m3 / day is being installed at Contract

workers canteen. 2010-11• Reusing of MBF granulated slag making pavement bricks.• Environment lab established for continuous monitoring of stacks

and ambient air quality. 2009-10. • ETP & STP water quality lab established. 2009-10.

Major environmental improvements

Plant Specific Water Consumption

2.27

5.00

2.43 2.493.823.63

5.00

0.001.002.003.004.005.006.00

05-06' 06-07' 07-08' 08-09' 09-10'Year

M3/M

T of S

teel

M3/MT National Benchmark M3/MT by CPCB

Page 14: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

14

Encon Program Management Methodology

Encouragement for participation

Suggestions referred to EC Cell

Evaluation of the projects

Co-ordination for Management Approval

Implementation TPM /SIX SIGMA Tools

Review by Chief Executive

Not effective

Identification of Encon & Involvement of employees.

Completed in Sep 08

2.technician, 4.labors& 1.Manager

2008-09Utilization of waste heat from tundish to preheat Sub Entry Nozzle. (LPG saving)

3.

Completed in Feb 10

1technician 2.labors& 1.Electrical engineer.

2009-10Installation light pipe (daylight) in PPC & SMS meeting hall

2

Completed in Aug 09

2 Technicians 3.contract labors 2.Engineer.

2009-10Biomass grassfire system for heating boiler feed water

1

Progress of implementat

ion

Extent of man-power involved

***

Idea originated

in FY **

Source of ECON idea *SN

Page 15: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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AUDIT FINDINGS:

ISO 14001:2004Product Name :

1034314Re-CertificationJob Description/Code:

170.37KALYANI STEELS LTDCompany Name/Code

S.G. SahuContact(s) :

Team Member(s) :Operations - KalyaniSteels

Department :

G KarthikeyanTeam Leader :4.4.6 Operational controlClause :

GKA/01Number :17/03/2010Date(s) :

MinorType of findings :

Standard requirement : The organization shall identify and plan those operations that are associated with the identified significant environmental aspects consistentwith its environmental policy, objectives and targets, in order to ensure that they are carried out under specified conditions, by stipulating the operating criteria in the procedure(s).Non conformity : The operation control procedure OCP/work instruction EMS/WI/KSL/4.4/05 for the operation of furnace does not specify the operating criteria forthe air fuel oil ratio and the operation of recuperator to minimise the air pollution, which is required as per the environment Management system manual.

Non Conformity

Corrective Action Report (to be completed by the company) :

Mr.S.B.BurdeCompany Representative :

25.03.10Proposed Completion Date

CORRECTION: Exact Fuel Oil ratio is mentioned.ROOT CAUSE: Exact Fuel Oil ration was not mentioned (Lack of Documentation).CORRECTIVE ACTION: The documentation of the Work Instructions was carried out as per the requirements of Environmental Management System.

Final Clearance22.03.10Actual Completion date

18/08/10

AUDIT FINDINGS :

ISO 14001:2004Product Name :

1034086Re-CertificationJob Description/Code:

172.37MUKAND LIMITEDCompany Name/Code

Final Clearance22.03.10Actual Completion date

Correction: Aspects related with concerns of interested Parties are identified and documented in “List of Aspects and Impacts”.Root Cause: Lack of awareness.Corrective Action: Concerns of interested parties while documenting the “ List of Aspects and Impacts”Was carried out as per the requirements of EMS.

Corrective Action

Mr.S.B.BurdeCompany Representative :

25.03.10Proposed Completion Date

Corrective Action Report (to be completed by the company) :

Standard Requirement: The organization shall establish, implement and maintain a procedure(s)a) to identify the environmental aspects of its activities, products and services within the defined scope of the environmental management system that it can controland those that it can influence taking into account planned or new developments, or new or modified activities, products and services, andb) to determine those aspects that have or can have significant impact(s) on the environment (i.e. significant environmental aspects).The organization shall document this information and keep it up to date.The organization shall ensure that the significant environmental aspects are taken into account in establishing, implementing and maintaining its environmental management system.Observed Non-Conformity: There is no evidence of considering the aspects related concerns of interested parties in the identification of significant environmental aspects as required by the procedure No. HSL/EOHSMS/P/4.3.1/02, Revision 01, dated 15.03.2009.

Non Conformity

MinorType of findings :

B S SridharContact(s) :

Team Member(s) :UtilitiesDepartment :

Vineet M SarwadeTeam Leader :4.3.1 Environmental aspects

Clause :

VS0/01Number :20/03/2010Date(s) :

18/08/10

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Energy Conservation Project Reporting Format

PaybackDetailInvestment

One TimeaRecurring

Savings per year:

Implemented on:Team members:Care taker:

Project details:

Background

OPRUTLMechElecEnergy Saving at:Theme:

Completion Date

Start DateProject No.

Daily Prodn and Energy consumption ReportProdn Date:

Particulars UOM Target For the Day Till Date

MBF1 Production MT 550MBF2 Production MT 550MBF3 Production MT 800Total MT

MBF1 Coke rate MT/THM 0.600MBF2 Coke rate MT/THM 0.600MBF3 Coke rate MT/THM 0.600Average MT/THM 0.600

No.of HeatsAs Cast Production MTs

SMS-Power KWH/MT 183LRF-Power-LM KWH/LMT 80

Furnace oil - LRF Ltrs/MT 1.00Furnace oil - VD-LM Ltrs/LMT 4.60

L.D.O Ltrs/MT 1.25

Argon Sm3/MT 0.83

Oxygen Nm3/MT 70.00

Nitrogen Nm3/MT 20.52

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17

5.255.355.68Energy per Ton of Steel

0.0030.0040.0030.260.280.2612500KgLPG

0.0130.0140.0131.351.51.511840LtrsHSD

0.0520.0560.0685.66.07.289384LtrsFurnace Oil

0.0280.0280.036333342860KwhPower for O2

0.1550.1550.164180180191860KwhPower

SMS

0.0000.0000.0000.0020.000.00912500KgLPG

0.0020.0020.0070.210.210.8318820LtrsLDO

0.0030.0030.0010.260.260.1209783LtrsHSD for DG

0.1080.1080.148125125172860KwhPower

0.0060.0070.0127814860KwhPower for O2

4.884.9765.2256106226538000KgsCoke

MBF

G Cal/MTG Cal/MT

G Cal/MTSp.Conper MTper MTKcal/UOM

Target10-11ConsumnConsumnFactors Energy Items

10-1109-1008-09Target09-1008-09ConversionUOM

Master Sheet in G Cal

Solid waste management

Partly reused in the process, Sold to outside parties, partly used in the construction of internal Roads

9140083,4291,06,121TPASMS Slag8

Sold to outside parties1680615,88721,374TPAEOF Sludge7

Sold to the KSPCB Authorised Party.

--13,998LPAWaste Oil (Haz. Waste)

6

Reused in the EOF296810113TPAPig Iron Scrap

5

Reused in the EOF & used in the Construction of Roads

2616523,08024,810TPAMBF Slag4

Sold to the outside parties & Partly reused in the construction of internal roads.

1402871,14,91586,165TPAG Slag3

Sold to the outside parties1483051,36,4261,53,023TPAIron Ore Fines

2

Sold to the outside parties & used in EOF & LRF

4198937,03626,847TPACoke Fines1

2009-102008-092007-08

DisposalQuantityUnitType of Waste

SN

Page 18: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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v HSL has taken drive to reduce 3-5% of conventional energy in 3 - 5 years.

v Actions initiated so far are:

ü Use of Bio mass for process heating & canteen

ü Bio gas in canteen

ü Jatropha plantation in the plant area about 25 acres. Seeds are planted to produce bio diesel to use in company vehicles.

ü Light pipe (Day lighting system).

ü Solar water heating system.

Renewable Energy Drive

Turbo ventilators Translucent Sheets

Involving Associates in ENCON

• M/s.Kalyani Steels Ltd, Pune and M/s.Mukand Ltd, Kalwe are our promoters and pioneers in Alloy Steel Making, with whom we carryout our regular interaction for Encon.

• CII is auditing our plant for Energy and water since three years. Almost all the suggestions of CII are complied.

• M/s Nalco is our associate for water conservation as a part of Total Water Quality Program

• M/s Appropriate Rural and Renewable Energy Institute, Pune an NGO, M/s Phoenix Products Belgaum and Sky shade Daylight, Hyderabad are our associates for implementation of renewable energy projects at our plant.

Page 19: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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% Breakup of time currently spent (Average basis) by Senior Executives in various functions

v Strategic Planning - 20%

v Product Development - 5%

v Costing - 10%

v Training & Development - 10%

v Optimization of available resources - 10%

v Building Management Systems - 5%

v Improving Environmental effectiveness - 5%

v Corporate social responsibilities - 5 %

v Technology up gradation - 10%

v Safety Management - 10%

v Quality Management - 10%

Future Plans

v Coke Oven plant for better quality coke and to further reduction in coke rate.

v Sinter Plant to recycle the process wastes and improve BF productivity.

v New15 MW power plant by utilizing excess BF gas available

Page 20: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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HOSPET STEELS LTD

National Award for Excellence in Energy Management Received from CII

HOSPET STEELS LTD

National Award for Excellence in Water Management Received from CII

Page 21: Hospet Steels Limited - CIIGBC · 2010-09-07 · 3 Pay back Period Kwh Rs.Lac KL Rs.Lac (Months) 1 Reduction of LPG & O2 consumption in CCM by optimizing cutting torch speed & idle

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Hospet Steels Limited

Energy Conservation Award

THANK YOU

Hospet Steels LimitedDRIVING INNOVATION Infinite resolve


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