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u#6 Overhaul

Date post: 05-Apr-2018
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    U # 6 OH Exception

    15/05/2006

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    U # 6 OH Exception

    Steam erosion due to W/W soot blowers nearcorner 2 & 6

    Probable causes of steam erosion :

    Improper draining of S/B header before start ofsoot blowing

    Problem in S/B rotary motion mechanism

    Steam kept charged in case of S/B gets stuck-up inside furnace

    S/B alignment problem due to missing furnace

    cap

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    U # 6 OH Exception

    Steam erosion was observed in radiant S/Hinlet header (L4) : no of bend tubes got eroded,

    complete set is required to be replaced.

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    Radiant S/H I/L header (L4)

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    Radiant S/H I/L header (L4)

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    Radiant S/H I/L header (L4)

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    U # 6 OH Exception

    Reheater final stage tubes connecting to outletheader (in the pent house) are having blackish

    layer.

    This is due to long term overheating (byconduction)

    Hardness has not changed much.

    Reason : Probable cause is secondary combustiondue to air ingress through pent house.

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    U # 6 OH Exception

    1

    9

    16

    24

    31

    39

    46

    5461

    69

    76

    84

    Going to 2

    nd

    pass

    Blakish

    layer inmiddle

    coils

    42,43,44

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    U # 6 OH Exception

    1

    3

    5

    7

    9

    11

    13

    1517

    19

    21

    23

    Going to

    Platen II

    Platen-IMiddle

    Platen-I

    Final

    I/LO/L I/L O/L

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    U # 6 OH Exception

    1

    3

    5

    7

    9

    11

    13

    1517

    19

    21

    23

    Going to

    R/H panel

    Platen-IIMiddle

    Platen-II

    Final

    I/LO/L I/L O/L

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    CW Outlet duct

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    CW Outlet duct

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    CW Outlet duct

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    CW Outlet duct

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    CW Outlet duct

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    U # 6 OH Exception

    CBA of CW inlet duct painting CW flow data (FY 2005-06)

    U# Pre O/H Post O/H Gain

    #5 20130 23255 3125(where Black bituminous painting was done)

    Additional gain in CW flow = 3125 9150 = 1175

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    U # 6 OH Exception

    CBA of CW inlet duct paintingWith increase of 1000 M3/Hr CW flow there

    will be gain in CW temp rise equivalent to 0.3

    deg C & corresponding gain in Condenser

    vacuum and Heat rate will be 0.00175 Ksc (1.3

    mmHg) and 2.1 Kcal/Kwhr

    daily monetary gain (For 100% PLF) will be

    ~Rs. 3175/=

    Cost of painting is 100000/-

    Hence, payback period is 31 days

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    U # 6 OH Observations

    Reheater 3rd

    Stage Notch observed in panel no. 83 at first bent.

    02 nos. steam cooled wall infront of top binder of panel

    no. 84 rubbing the steam-cooled wall. The binder is to be

    cut.

    The spacers provided at front side is rubbing with the

    coil, to be cut and provided below the coil where shield

    is available with the tube

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    U # 6 OH Observations

    Reheater 2nd

    Stage Out of side panel no. 83 centre bent has been notched.

    Steam cooled wall front side tube no. 2,3,4,5,6,7&8

    (from RHS) are to be replaced at eco top.

    Eco top steam cooled wall tube no. 6 to 10 are to be

    replaced

    Steam cooled wall above economiser at rear wall tube

    no. 6,7,8,9&10 are to be replaced.

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    U # 6 OH Observations

    Reheater 2nd

    Stage LHS steam cooled wall above economiser tube no. 6 to 1

    notches observed.

    Front steam cooled wall above economiser tube 4,5&6

    notched observed.

    Rear side steam cooled wall above economiser tube no.

    3,4,5,6,7,8&9 notches observed

    In RHS steam cooled wall 4th tube from rear side notchesobserved.

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    U # 6 OH Observations

    Hanger Tubes Row no. 6 hanger no. 1 notches observed.

    Row no. 5 hanger no. 72 notches observed.

    Row no. 6 hanger no. 72 notches observed.

    Row no. 3 hanger no. 4 to be replaced.

    Row no. 6 hanger no. 29 to 31 fitting observed.

    83 tubes have been identified for rectification

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    U # 6 OH Observations

    Radiant Super heater Soot blower is rubbing with radiant super heater tubes.

    In radiant super heater bents rubbing the tube in some

    locations.

    Radiant super heater hooks are tapping water wall tube

    that has to be protected at few locations, the supports are

    radiant super heater damaged.

    Superheater panel no. 11 near the top binder erosionobserved.

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    U # 6 OH Observations

    Burner area Top oil burner plate in each panel block got damaged. To

    be rectified.

    Oil burner air guide pipe badly damaged at the top most

    of corner and partially damaged at bottom blocks.

    Oil gun guide pipe at the furnace side is melted.

    Refractory is to be provided for panel side tubes.

    05 nos. of tubes are identified for replacement.


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