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8/10/2019 EOR-IOR
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E O R / I O R
CO2 foam has been used as an effective
mobility-reducing agent for CO2 flooding
in the oil-recovery process. Recent researchindicates that some CO2 foams can provide
selective mobility reduction (SMR). SMR in
foams reduces CO2 mobility by more in
higher- than in lower-permeability cores in
laboratory experiments. Unlike Darcy flowof ordinary fluids in rocks, where the
mobility is proportional to rock permeabil-ity, the mobility of foam with SMR is less
than proportional to core permeability and
foam flows through higher-permeabilityrocks at a lower rate than would be expect-
ed for the existing pressure gradient. This
allows foam to flow at the same velocity in
high- and low-permeability regions in thereservoir, preserving the uniformity of the
flood front while propagating through
rocks with nonuniform permeability. Use of
a CO2 foam with SMR delays CO2 break-
through and provides a high displacement
efficiency in heterogeneous reservoirs.
FOAM-DURABILITY TEST
For this study a high-pressure foam-dura-
bility test apparatus was constructed and
screening tests were conducted successfullyto select surfactants for field foam applica-
tion. The test determined the foaming abil-
ity of each surfactant, the stability of foam,
and surfactant properties, such as the inter-
facial tension (IFT) between a surfactantand dense CO2 and the critical micelle con-centration (CMC) of a surfactant. The
foam-durability apparatus comprises a CO2source tank, a visual cell made from a trans-parent sapphire tube, a buffer-solution
cylinder, and a pump. The major partof the
system, the CO2 tank and sapphire-tube
high-pressure cell, is contained in a tem-
perature-controlled water bath. The buffer-solution cylinder and the pump are
installed outside of the water bath, and
their temperatures are maintained at the
same temperature as the water bath by a
separate temperature-control system.During operation, the sapphire visual cell
is first filled with the solution to be tested.Once the system reaches the desired pres-
sure, the dense CO2 is introduced through a
needle at the lower end of the cell. The CO2is drawn upward inside the cell. The densi-
ty difference between dense CO2 and the
tested solution causes CO2 bubbles to form
and collect at the upper end of the cell.
These bubbles will either form a layer offoam-like dispersion at the top of the sap-
phire tube or coalesce into a clear layer of
dense CO2, depending on the effectiveness
of the surfactant. After 1.75 cm3 of CO2 has
been introduced into the sapphire tube, thepump is stopped and the length of time that
the formed foam persists is measured.
Surfactant solutions (1 wt% active compo-
nent) were prepared by dissolving the sur-
factant as received from the suppliers into abrine system consisting of 5.6 wt% NaCl
and 1.4 wt% CaCl2. Different concentra-
tions of the surfactant solution were pre-
pared by diluting the batch solution withthe 7 wt% brine. All screening tests were
conducted at 77F and 2,000 psig.
By measuring the time required to form a
bubble at the needle in the sapphire tube
and the number of bubbles formed within acertain time period, the average volume
and radius of each bubble is calculated.Once the average radius of dense CO2 is
known, the IFT between surfactant solu-tion and dense CO2 can be calculated.
Results and Discussion. The IFT decreas-
es with surfactant concentration and levels
off at a region where the IFT no longer
decreases as surfactant concentrationincreases. The concentration at which the
interfacial properties between surfactant
and CO2 show no significant change is the
CMC and can be graphically determined.
The IFT curves and CMC values vary withsurfactant formula. The CMC values for
Surfactants 1 through 5 are 0.04, 0.06, 0.07,
0.07, and 0.35 wt %, respectively.
The foaming ability of a surfactant is
defined as the ease with which a bubble isformed at the needle when the surfactant
CO2-FOAM FLOODS:
FOAM PROPERTIES AND
MOBILITY-REDUCTION EFFECTIVENESS
This article is a synopsis of paper SPE
37221, Assessment of Foam
Properties and Effectiveness in Mobility
Reduction for CO2-Foam Floods, by
Jyun-Syung Tsau, SPE, and Reid B.
Grigg, SPE, New Mexico Petroleum
Recovery Research Center, New
Mexico Inst. of Mining and Technology,
originally presented at the 1997 SPE
International Symposium on OilfieldChemistry, Houston, 1821 February.
Fig. 1Decay of CO2 foam with Surfactant 4.
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70 JANUARY 1998
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solution contacts the CO2. Durability is
defined as the persistence of foam bubbles
after a standard volume of CO2 has been
introduced. A cathetometer is used to mea-sure the foam height and the weight of the
CO2 to allow calculation of the percentage
of foam inside the sapphire tube and assess-
ment of the persistence of foam. Foam wasfound to form more easily as the surfactantconcentration increases. The foaming abili-
ty of surfactant increases as the IFT between
CO2 and the surfactant solution decreases.
The longest-lasting foams were not neces-
sarily found at the best foaming conditions.For Surfactant 4 (Fig. 1), there is an opti-
mum concentration (0.075 wt%) at which
the foam has the best stability or the longest
durability. The persistence of foam decreas-
es at concentrations either above or belowthis optimum concentration. This trend was
observed with Surfactant 1, with an opti-mum concentration of 0.05 wt%. In both
cases, the optimum concentration is close to
the surfactants CMC (i.e., 0.07 forSurfactant 4 and 0.04 for Surfactant 1). The
bubbles formed by Surfactants 5 and 2 coa-
lesced in less than 1 minute, whereas most
of the bubbles formed by Surfactant 3 lasted
longer than 90 minutes. The optimum con-centration for generating the longest-lasting
foams were not identified for Surfactants 5,
2, and 3. Surfactant 3 generates the most
stable foams, followed by Surfactants 4, 1, 2,and 5 (listed by decreasing level of stability).
FOAM-MOBILITY TEST
Core systems containing well-defined high-
and low-permeability regions were con-
structed to assess the flowing-foam proper-ties and verify the existence of SMR in het-
erogeneous porous media. This experiment
used two well-defined permeability regions
in capillary contact arranged in series. The
series assembly uses two 1/2-in.-diameter
cores approximately 3 in. long. The core-holder is fitted with five equally spaced
pressure taps so that the middle tap is near
the junction of the cores. The abutting endfaces of the cores are carefully cut perpen-dicular to their axes and ground flat before
mounting end to end. The space between
the two core faces is filled with fine sand.
Pressure differences between each pair of
pressure taps is recorded. The fluids flowinginto a foam generator and the composite
core are injected by two pumps, a positive-
displacement pump for the CO2 and a pis-
ton pump for brine or surfactant solution.
The pressure is maintained at an almost
constant level by leading the output fluids
into a backward-running piston pump.When the experimental conditions reach
steady state, pressure drops in each segment
of the core are recorded as functions of time.
The mobility of injected fluid, defined as theratio of Darcy or superficial velocity of the
fluid to the average pressure gradient along
each segment of core, is calculated and com-
pared for different injection conditions.
The foam generator and core sample arepreflushed with synthetic brine for at least 40
pore volumes (PV) before the brine perme-
ability measurements are begun. The hetero-
geneity of the series composite core was
determined by measuring the brine perme-abilities for four different sections along the
core. Following the permeability measure-
ments, dense CO2 and brine were injected
simultaneously into the core sample. The
mobility of the two-phase mixture was mea-
sured for each core section and used as a ref-erence for later comparison. After establish-
ing the baseline, a sequence of foam experi-ments was performed. To satisfy the adsorp-
tion requirement, 50 PV of surfactant solu-
tion was displaced. Then CO2 and surfactantsolution were injected into the core until
steady-state conditions were reached. Foam
mobility was measured. The ratio of volu-
metric flow rate of CO2 to aqueous phase was
maintained at four to one. The total injectionrate was varied from 5.0 to 15.0 cm3/hr cor-
responding to velocities of 3.1 to 9.4 ft/D.
The two composite cores had permeabilities
ranging from 525 to 128 md for Core 1 and
819 to 106 md for Core 2. Surfactant con-centrations of 0.1 wt% were used in Core 1
experiments, while 0.05 wt% surfactant solu-
tions were used in Core 2 experiments.
Results and Discussion. Comparison of themobility data in the first three core sections
indicates that the mobility of CO2/brine is
reduced by the addition of surfactant. Foam
mobilities are significantly lower than the total
mobility of CO2/brine. This mobility reduc-
tion varies with surfactant, surfactant concen-tration, and flow condition. In general, foam
mobility is lower when foam is generated at
higher surfactant concentrations or whenfoam is displaced at a lower injection rate.
When mobility dependence on rock per-
meability is examined, SMR is also found to
depend on the surfactant type, concentra-
tion, and flow rate. When the mobility of
CO2/brine or CO2/foam is plotted vs. the
sectional permeability, the slope of the lineindicates the degree to which the the mobil-
ity of fluid depends on the permeability of
porous media. A slope of one indicates that
the mobility of the fluid is proportional tothe rock permeability as described by
Darcys law. A value of less than one shows afavorable dependence of SMR that will lead
to a more uniform displacement front when
the fluid is flowing through heterogeneous
porous media. In general, the value of theslope decreases when surfactant is added to
the brine as a foaming agent. This suggests
that foam is useful in correcting the nonuni-
form flow of CO2 and brine in a porous sys-
tem containing differing permeabilities. Atlower velocities, the value of the slopedecreases, indicating a more favorable SMR
occurs at a lower displacement rate.
When results from the foam-durability
tests are compared with the mobility tests,
the stability of foam in the bulk phase canbe correlated with the effectiveness of
mobility reduction of flowing foam in the
porous media. The mobility reduction is
enhanced as foam stability increases. Themobility-reduction factor (MRF), defined as
the ratio of total mobility of CO2/brine to
foam mobility, increases with the foam life.When foams become more stable, more
resistance to flow results in a higher mobili-
ty reduction. On the basis of these observa-tions, the capability of surfactant in stabiliz-
ing the bubble file or lamellae in the porous
media is believed to be the most likely rea-
son for the effectiveness of foam in reducing
the mobility of CO2.Use of a proper CO2 foam could minimize
the mobility contrast between high- and low-
permeability zones in reservoir flow, increas-
ing the efficiency of oil displacement.
Experimental research indicates that the SMRproperty of CO2 foam is real. It is observed in
parallel- and series-core tests with capillary
contact and can be presumed to function
similarly in actual field situations.
CONCLUSIONS
1. The stability of foam in the bulk phase
can be correlated with the performance of
foam flowing in porous media. When com-
paring different surfactants, greater foamstability gives more mobility reduction in
foam displacement.
2. The MRF increases as the reduction
factor of the IFT between CO2 and theaqueous phase increases.
3. An optimum concentration exists atwhich the most stable foam in the bulk phase
is formed. This optimum concentration is
close to the CMC of each surfactant solution.
4. Factors that favor reducing the mobili-ty of CO2/brine also lead to a more favorableSMR when foam flows in a composite core
consisting of differing permeabilities.
Please read the full-length paper for addi-
tional detail, illustrations, and references.
The paper from which the synopsis hasbeen taken has not been peer reviewed.
8/10/2019 EOR-IOR
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JANUARY 1998 71
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After the 1973 oil embargo, the U.S. gov-
ernment funded several initiatives to pro-
vide additional worldwide resources as a
means of lowering oil prices. One of these
initiatives was Project Deep Steam. Thisproject evolved on the theory that signifi-
cant reserves of heavy oil, worldwide,
were beyond the reach of surface-generat-
ed steam because of heat losses in the tub-ing. Two approaches were taken to achieve
the goal of steam delivery to deep forma-
tions. One was to improve or develop newinjection strings to minimize heat loss,
and the second was to design and demon-strate the operation of a device that would
generate steam in the wellbore at the
depth of the formation. Sandia Natl.
Laboratory was given a U.S. $23 million
budget for a 4-year program beginning in1976. Sandia initiated an in-house effort
for steam-generator development. Both
the insulated-injection-tubing develop-
ment and testing were carried out by
external contract.The outside diameter (OD) of the down-
hole steam generator could not exceed 4.5
in. This OD would fit inside 7-in. casing. To
achieve large-magnitude firing rates, thecombustion process would have to occur at
high pressure. Steam would be generated in
either of two ways. One was by a tradition-
al heat-exchanger surface that separated the
hot flue gases from the water. Adequate sur-face for efficient heat transfer was obtained
by heat-exchanger lengths of up to 100 ft.
The cooled flue gases were exhausted up
the annulus. Combustion did not have to
occur at pressures as high as those required
for injection. In the second method, com-bustion occurred at high pressure and
water was injected directly into the hot flue
gases. Then, both steam and flue gases were
injected into the formation. Injection of theflue gases proved to be either a benefit or a
problem; one benefit was that it was helpfulin the air-quality permitting process.
Operation of both downhole steam genera-
tors could be carried out on the surface,
with injection tubing transporting the
steam downhole. The Sandia developmentand one of the outside contracts were based
on a direct-contact steam generator. The
other outside contract was for an indirect-
contact steam generator.
FIELD OPERATIONSKern River Field. The equipment for this
test was sized for a delivery of 5 million
Btu/hr at a maximum pressure of 400 psi.Along with the steam, nitrogen and carbon
dioxide were generated. The combustion
was carried out with minimum excess air.
Because this was the first operation of a
direct-contact steam generator of Sandiadesign, the generator was operated on the
surface rather than downhole. The OD of
the steam generator was 4.5 in., and liquid
propane was the fuel. The Kern River field
had been steamflooded for a number ofyears before this test, and the injector well
communicated quickly with surrounding
production wells because of this previous
steaming. No particular increase in produc-tion was noted because this was a rather
mature steamflooded field.
Wilmington Field. For this operation two
different generators and support systems
were demonstrated simultaneously. Thefirst was operated downhole, and the sec-
ond was operated on the surface. Both were
fired with air as the oxidizer and diesel as
the fuel.Downhole Air/Fuel Generator. The out-
put for this system was sized for 5 million
Btu/hr at a pressure rating of 1,400 psi.
Installation of the generator was a rather
complex task. The connectors from the
generator to the surface consisted of twojointed tubulars and four continuous tub-
ing lines. The air line was 23/8-in. jointed
tubing and was the load-bearing element
for the installation. Water was conducted
down 1.66-in. jointed tubing that had to be
made up by hand tools after the larger tub-
ing had been made up with power tools.The other lines were continuous coiled tub-
ing that had to be pulled out of the way by
hand to make up the jointed tubulars.
These four lines were attached to the 23/8-
in. tubing by a custom-made cast-alu-
minum clamp. Because diesel contains sul-fur that produces acids when burned, caus-
tic was injected through a 1/4-in. line to
neutralize the generator effluent. Two
additional tubing strings were installed to
verify operation. One was a continuous,fully sheathed, 1/8-in. thermocouple line
and the other a1
/4-in. sample return line.The final line was a 3/8-in. fuel line. A
thermal packer with a short stinger hung
below the generator. A cap on the end ofthe stinger was used to keep annulus flu-
ids isolated from the generator assembly
before operation.
When the installation was complete,
the operation was begun by blowing theplug off the end of the stinger. Then, a
volume of air was injected through the
generator to create a compressible cush-
ion before ignition. Next, water injection
began. Ignition was achieved by use of aslug of pyrophoric fluid that was injected
into the diesel line that had first been
flushed with water. When ignition was
achieved, pressure transients wereobserved at the surface monitoring point.
Usually 1 to 2 minutes were required for
flows to quasistabilize. An increasing
pressure was usually observed for a signif-
icant period of time following initiation.Several problems occurred in the down-
hole equipment. The lines for the fuel, air,
and water had filters and check valves just
above the steam generator to ensure that
critical ports were not plugged and thatfluids from the formation could not flow
back through the generator during shut-
downs. In spite of corrosion inhibitors in
the water supply, large quantities of corro-sion debris sloughed from the water line
and began plugging that filter. The gener-
ator had to be pulled, and the mesh size
and accumulation volume increased.
Improved production was observedduring this test because of the injected
flue gases and their communication with
surrounding production wells. The flue
gases reduced the caloric value of the pro-duced market gas, but the blended pro-
REFLECTIONS ON A DOWNHOLE
STEAM GENERATOR
This article is a synopsis of paper SPE
38276, Reflections on a Downhole
Steam-Generator Program, by A.B.
Donaldson, SPE, New Mexico
Highlands U., originally presented at
the 1997 SPE Western Regional
Meeting, Long Beach, California, 2527June.
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E O R / I O R
duction from the rest of the field kept the
value within specifications.
Surface Oxygen/Fuel Generator.
Oxygen was used in one trial to eliminatethe large amount of noncondensable
nitrogen and increase the partial pressure
of carbon dioxide. This also eliminated
compression equipment. While the exper-iment with oxygen did not have the sameoperational problems as the downhole
unit, it had its share of difficulties. The
major problem was survival time of the
combustor can that isolated the combus-tion process from the injected water until
combustion was complete. None of the
conventional stainless steels used had suf-
ficient strength to survive the very high
thermal stresses caused by an oxygen/hydrocarbon flame.
At the end of operations in the Long
Beach,California, area, the apparent scarci-ty of oil disappeared and government fund-
ing was reduced. A number of the projectteam members elected to leave Sandia and
obtain nongovernment funding to attempt
commercialization of the technology.
Enhanced Energy Systems, Inc. (EESI). A
number of deficiencies in the Sandia equip-
ment were obvious after the field experi-
ences. Manpower requirements and sophis-
tication were excessive for oilfield applica-tions. The equipment was redesigned for
commercial applications, with the goal ofone-person operation and the use of field
gas or crude oil for generator fuel. The con-
cept of steamdrive was replaced by huff n
puff operation. Installation of the units
downhole was difficult, and many of thelater operations were conducted with the
generator on the surface.
Hondo, Texas. The formation is shallow
chalk with poor permeability and the pay
is thin (from 7 to 40 ft). A major oil com-pany had attempted steaming in a shallow
sand zone in the area, but the return was
insufficient to continue the effort. Seven
wells were stimulated. The casings hadsmall diameters, and the steam generatorwas installed at the surface with effluent
conducted to the wells. Neither insulated
injection string nor packer was used. Flue
gases were injected into the formation with
the steam. Because of poor injectivity, theequipment was operated at the lowest out-
put, 2 million Btu/hr, at the maximum
pressure, 1000 psi. The fuel used for the
steam generator was site crude, and the
location water had a high hardness.Production was improved from primary
production but was not sufficient for fur-ther operation in this field.
Hospah, New Mexico. The formation is
a consolidated sand, approximately 1,100
ft deep, with a thickness from 10 to 20 ft.
The wells were not thermally insulated,and a downhole packer was not used. Fuel
for the generator was old diesel. The injec-
tivity of the wells was good, and some flue-
gas production was observed at wells alongthe path of least resistance. The oil pro-
duced was in the form of an emulsion.
Various chemicals were used in an attempt
to break the emulsion, but none was suc-
cessful. Production increases were attrib-uted to creation of a high-pressure pocket
of gas that blocked the cold-water seepage
into the formation.
Long Beach. This customer was the first
to purchase a full line of equipment.
Because of the complexity of equipmentand procedures, EESI personnel were
retained to operate the equipment. Becausefield gas was available at this location, both
the generator and compressors were fueled
by site gas. Expansion cooling of the fuelgas led to icing conditions inside the con-
trol valve, and the flow could not be
bypassed. A desiccant was used to dry the
gas. A major problem was controlling deliv-ery of fuel, air, and water 2,000 ft down-
hole. A thermal packer was used to isolate
the annulus from the reservoir, but filters
and check valves were used sparingly. The
equipment was designed to operate atapproximately 8 million Btu/hr at pressures
up to 1,850 psi. Two wells were steamed
with downhole units. One well was lost in
this operation because of parted casing at
400 ft.As operating experience was gained,
many of the urgent operational bugs were
found and corrected, and some reasonable
periods of steam injection were experi-
enced. The generator had to be pulled onone or two occasions because of deteriora-
tion of the combustion-chamber wall. At
this time, operation of the steam generator
was returned to the surface and no further
installations were made downhole.Two other nearby wells were cyclicly
steamed from this surface location.
Insulated surface-injection piping was used
to transport the steam to the wells. Some ofthe most reliable operations occurred dur-
ing this time. Peak production immediately
after bringing the well back into production
sometimes exceeded 500 BOPD, compared
with a prestimulation production of 20 to40 BOPD. The customer calculated total
production costs of approximately U.S.
$12/bbl, which was the lowest of any of
their production. Although conventionalsteam would probably have been economi-
cally viable at this location, compliance
with air-quality regulations was difficult.
THE COMPLETION
While conventional steam-generation tech-
nology has the advantage of being the
accepted technology for shallow reservoirs
with good injectivity, there are some areaswhere improvements can be made. In insu-lated injection tubing currently available,
heat losses at bare collars, expansion joints,
packers, and subs almost negate the bene-
fits of insulation unless the annulus is com-pletely dry. This conclusion is based on a
water-reflux mechanism that occurs even
when the annulus fluids are initially
expelled. Residual water film or leaks into
the annulus can generally be expected.
CONCLUSIONS
In general, no advantage was evident inplacing the generator downhole, particu-
larly when injectivity of gases was a prob-
lem. It was evident that injection of thecombustion gases was desirable in some
cases and, in one case, necessary.
Formations with poor injectivity are a
major resource awaiting a viable recovery
mechanism. Placement of a direct-contactsteam generator downhole is not a solution
to this problem.
RECOMMENDATIONS
These recommendation focus on whatmodifications can be made to the downhole
steam generator for successful stimulation
of tight formations.
New Concepts. A downhole steam genera-tor that does not produce nitrogen gas
appears to offer potential for low-injectivity
applications. There have been field trials of
radio-frequency heating devices as well as
one that uses electricity for energy. It isuncertain whether any of these have under-
gone extensive field tests. One other possi-
bility is to transpose submerged combus-
tion technology developed for toxic-wastedisposal to oilfield applications. Anotheridea is to use the heat of mixing two fluid
components that can be separated by distil-
lation at the surface. A downhole heat
exchanger would be used to heat feed water
to steam, and the mixture of the two com-ponents would be returned to the surface
for processing.
Please read the full-length paper for
additional detail, illustrations, and ref-
erences. The paper from which the syn-
opsis has been taken has not been peerreviewed.
8/10/2019 EOR-IOR
5/217 4 JANUARY 1998
E O R / I O R
Foam has the potential to relieve several
common problems by better areal sweep,
better vertical sweep, less viscous fingering,
and lower handling costs when compared
with gas-injection improved oil recovery(IOR). Foam may be introduced by contin-
uous coinjection of gas and surfactant solu-
tion or by injection of a slug of surfactant
solution followed by injection of a gas slug,known as a surfactant-alternating-gas
(SAG) process. SAG injection has certain
advantages over continuous foam injectionin foam IOR processes. SAG injection min-
imizes contact between gas and water in theinjection facilities, reducing corrosion, and
can achieve high injectivity and low mobil-
ity at the displacement front. High injectiv-
ity results as foam near the well dries out,
weakens, and collapses, while stronger,wetter foam farther from the well maintains
mobility control. Recent simulation results
show that SAG processes can overcome
gravity override with less increase in injec-
tion-well pressure than is possible withcontinuous foam injection.
SCALEUP OF LABORATORY RESULTS
There are a number of published coreflood
studies where gas is injected into core sam-
ples presaturated with surfactant solution.Some show foam persistence for many pore
volumes (PVs) of gas injection. However,
extrapolating these results directly to field
scale is dangerous. Because of dispersive
effects, the mobility within the shock frontmay exert influence in the length scale of a
coreflood that does not occur in the field.
Processes such as foam generation may
occur slowly on the time scale of a core-flood but be virtually instantaneous on thetime scale of a field project. Unsteady-state
displacements in a coreflood may not be
directly proportional to field scale, and
foam behavior in a reservoir may not be
directly proportional to unsteady-state dis-
placements in a coreflood. Capillary endeffects in a coreflood study may prevent
water transport out of the core, prolonging
foam life beyond that observed in a larger
system without this effect. A more reliable
procedure is to derive the fractional-flowcurve from the coreflood and then scale to
reservoir size with fractional-flow methods.
APPARATUS AND MATERIALS
An unfired Berea core with a permeability of
720 md and porosity of 0.22 was used in theexperiments. It was cut into a 9.5-in.-long
right-circular cylinder. An N2 gas phase
with a 1.0-wt% NaCl/0.01-wt% CaCl2/1.0-
wt% surfactant aqueous phase was used.
The coreholder, positioned downstream ofthe foam generator, held the core in a verti-
cal position. The coreholder was designed
to be lightweight so that the weight of the
core could be measured effectively during
the flood to determine water saturation, Sw.
Flow lines were flexible, transparent nylon,
and baffles were installed to restrict air flow
around the apparatus and minimize exter-
nal forces on the coreholder. Ports divided
the length of the core into three sections of2.6, 2.75, and 4.15 in., respectively, from
inlet to outlet. The weight of the system,
with Sw in the core equal to one and zero,
was measured before the tests, allowing
determination of Sw during the test.
One goal of these tests was to measurecap-illary pressure, Pc. A probe was designed that
used a differential-pressure transducer to
measure the pressure in the gas phase on oneside and pressure in the water phase on theother side of the transducer. A backpressure
regulator maintained a steady backpressure of
147 psi on the entire system during the two-
phase flow. Differential-pressure transducers
measured pressure drop, p, across each ofthe three sections of the core. All transducershad a range of 0 to 80 psi, and were calibrat-
ed before the test. Data were recorded by a
computerized data-acquisition system.
EXPERIMENTAL STRATEGY
Tests were performed at room temperature.The core was vacuum saturated with brine,
then hundreds of PVs of brine were injected
as backpressure was changed between 0 and
100 psi to eliminate gas from the core.
Backpressure was set at 147 psi at the end of
the extended brine injection and held con-stant. Dozens of PVs of surfactant solution
were then injected. Gas was then introduced
with the surfactant solution at a water volu-
metric fraction, fw, of 0.2. fw was incremen-
tally reduced as pressure responses stabi-lized. When a minimum value of fw=0.002
was reached, water injection ceased and anextended period of gas injection began.
EXPERIMENTAL RESULTS
Gas/Water Coinjection. The value of Sw was
derived from measured weight. Two methods
of estimating the amount of water in the dead
volume were used. The first assumes that the
imposed fw equals the water volume fractionin the endcap. The second is based on endcap
weight that changes in a shorttime compared
with changes that occur across the core. Both
methods give qualitatively similar results.
Water relative permeability,krw
, values werecomputed from measured p with a form of
Darcys law and with the assumption of a
water viscosity of 1.0 cp. The measured p in
Section 2 was used in all calculations to avoid
end effects. Pc andp were measured, and Pcof the Berea computed from Sw values, by useof capillary pressure curves for unfired Berea
during primary drainage, at values of N2/
aqueous interfacial tension (33 dynes/cm),
measured at room temperature. The Berea Pcwas computed to compare measured Pc withand without foam under the same conditions.
Foam strength is characterized by its
resistance factor (RF), the ratio of mobilitywithout foam to that with foam at the sameSw. An RF value of 1 indicates no foam,while an RF value of 100 means that the
presence of foam has reduced gas mobility
100 times more than gas mobility without
foam at the same Sw. Computation of RF
requires knowledge of gas relative perme-ability, krg, without foam. Because krg is
high, and changed very little with the low
values of Sw used in these tests, the value of
krg was assumed to be 1.0.
Results.When gas and water are injectedtogether, the foam is strong (RF2,000)
COREFLOOD STUDY OF SURFACTANT-
ALTERNATING-GAS FOAM PROCESSES
This article is a synopsis of paper SPE
38318,Coreflood Study of Surfactant-
Alternating-Gas Foam Processes:
Implications for Field Design, byK.R.
Kibodeaux, SPE (now with Texaco E&P
Technology), and W.R. Rossen, SPE, U.
of Texas, originally presented at the
1997 SPE Western Regional Meeting,Long Beach, California, 2527 June.
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beforefw=0.008, then there is catastrophic
weakening of the foam between fw=0.02
andfw=0.008, followed by a gradual weak-ening asfw decreases. Foam strength is still
appreciable (RF=25) after breakage, and
foam collapse is not complete. When the
foam breaks, fluid is absorbed and swellingresults (imbibition), accompanied by adecrease in Pc. As Sw increases, krw also
increases as Pc drops. Measured values of Pcwere high, compared with those expected
without foam.
DISCUSSION
In these tests, Pc was measured during foam
flow in consolidated porous media for the
first time. Foam is strong asPc increases to
some limiting value. There is a critical Pcabove which foam lamellae rupture, and a
limiting Pc value is expected to exist inporous media at which a strong foam weak-
ens drastically. In these tests, the value of the
critical Pc was approximately 12 psi. Otherinvestigators have reported a foam film sur-
viving at Pc>17 psi. The Pc measurements,
although unexpectedly high, were valid
indications of the actual values in the core.
One goal of this work was to apply frac-
tional-flow methods and a coreflood-derived
fw curve to scale up laboratory coreflood
results. A time/distance diagram for an SAGprocess was generated from the fractional-
flow curve. Mobility is high at the initial con-
ditions behind the shock front. At the shock
front, mobility is low, with spreading waves ofgently increasing mobility behind it. A foamof very low mobility exists in a thin, moving
front composing the shock. Within this zone,
foam forms, strengthens, exceeds critical Pc,
and weakens. Fractional-flow theory states
that all the points between initial conditionsand the shock on the fractional-flow curve,
including the strong foam near fw=0.02, lie
inside the the shock. This extremely strong
foam within the narrow shock front improves
the mobility ratio of the displacement with noadverse effect on injectivity.
CONCLUSIONS
1. Pc was measured during foam flow in
consolidated porous media for the firsttime. Unexpectedly high Pc were measured
in the presence of strong foam.
2. Sw declined and Pc increased as injec-
tion fw was reduced in steps to a point
where foam abruptly weakened. This point
is defined as the limiting Pc. The shape of
the fractional-flow curve was similar to
those proposed previously.3. When the foam weakened, imbibition
occurred, with a increase in Sw and a
decrease in Pc. This imbibition event, as
well as multiple steady states of foam and amultivalued fractional-flow function, maycomplicate the use of fractional-flow meth-
ods for foam-performance prediction.
4. Coreflood results cannot be scaled direct-
ly to field performance because both evapora-
tion and capillary end effects alter water trans-port late in the flood. Using laboratory core-
floods to derive fw as a function of Sw, then
scaling up with fractional-flow methods or
computer simulation, provides more reliable
scaleup from the laboratory to the field.5. Results suggest moderate mobility
reduction in a broad region behind theshock front, while weakened foam near the
well allows good injectivity.
Please read the full-length paper for addi-
tional detail, illustrations, and references.
The paper from which the synopsis has
been taken has not been peer reviewed.
JANUARY 1998 7 7
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78 JANUARY 1998
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On 17 May 1996, Total Minatome Corp.
initiated an enhanced-oil-recovery (EOR)
high-pressure air-injection project at the
Horse Creek field in North Dakota. This
project is the third high-pressure air-injec-tion program completed in the Ordovician
Red River formation in the Williston basin.
The Horse Creek field is 7 miles east of the
Cedar Creek anticline, in the south centralportion of the Williston basin. The field was
discovered in 1972 and comprised 15 pro-
ducing oil wells. In 1993, geological, labo-ratory, and reservoir-modeling studies were
conducted to evaluate the EOR potential ofthe field. On the basis of the results from
these studies, an EOR unit for this field was
formed in 1995. There are currently 11 pro-
ducing wells, three air-injection wells, one
monitor well, and one water-disposal wellwithin the unit area. Air is being injected
into the reservoir at a rate of approximately
8,500 Mscf/D at 4,700 psi discharge pres-
sure. Nine months after injection began,
the reservoir pressure continues to rise andproduction has increased from 293 to 400
BOPD.
RESERVOIR CHARACTERIZATION
Geology. The Horse Creek field is a strati-
graphic oil accumulation within theOrdovician Red River formation. The Red
River formation in this portion of the
Williston basin is subdivided into four
porosity zones. These porosity zones are
referred to as Zones A through D (Fig. 1).Air injection and production in the Horse
Creek field has been limited to Zone D.
The upper portion of the Red River for-
mation consists of a series of briningupward, cyclic carbonates deposited in asubtidal to supratidal environment on a
restricted shelf during the Red River marine
transgression. Rock types include lime-
stones, dolomites, and anhydrites.
Lithology varies from laminated mudstones
to heavily bioturbated packstones, wacke-
stones, and mudstones. Dolomitization of
the heavily bioturbated units has resultedin a secondary porosity within Zone D,
from which the Horse Creek field produces.
Stratigraphic cross sections, core data, and
petrophysical-facies maps indicate that
Zone D comprises two separate lobes thatare discontinuous across the field. The
HORSE CREEK AIR-INJECTION
PROJECT: AN OVERVIEW
This article is a synopsis of paper SPE
38359, The Horse Creek Air-Injection
Project: An Overview, by B.C. Watts,
T.F. Hall, SPE, and D.J. Petri, SPE,
Total Minatome Corp., originally pre-
sented at the 1997 SPE Rocky
Mountain Regional Meeting, Casper,Wyoming, 1821 May.
Fig. 1Horse Creek field type log.
MASSIVEANHYDRITE
GAMMA RAY
8900
9000
9100
9100
GAMMA RAY
DENSITY @
CORE 2
CORE 1
C ZONE
D ZONE
A ZONE
TOP RED RIVER
B ZONE
North Dakota
DENSITY POROSITY30 10
LITHOLOGY
CORE DESCRIPTION
DEPOSITIONALENVIRONMENT
LAMINATEDMEMBER
BURROWEDMEMBER
SUPRATIDAL
SUPRATIDAL
TO
UPPER
INTERTIDAL
(RESTRICTED
FAUNA)
LAMINATED
DOLOMITIC
MUDSTONE
HEAVILYBURROWED
PACKST/WAKESTDOLOMITE
HEAVILYBURROWEDDOLOMITICMUDSTONE
TIGHTLY BURROWED
LIME MUDSTONE
SUBTIDAL(NORMALMARINE)
SUBTIDAL TOLOWER INTERTIDAL
(NORMALMARINE)
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lower unit of Zone D is one continuous
unit that occurs across the entire field area.
Porosity and Permeability. Porosity andpermeability in Red River Zone D are
related to several stages of dolomitization.
The highly burrowed subtidal to lower-
intertidal lime muds in Zone D, whichcontain mainly macroporous pore throats(2 to 20 m), contain most of the reser-
voir-quality porosity and permeability.
Burrowing appears to have prepared these
rocks for dolomitization and porosity
development as compared with the sur-rounding nonburrowed, laminated
supratidal to upper-intertidal lime muds,
which, although porous, contain mainly
microporous (0.2 to 0.5 m) pore throatsand are nonproductive. On the basis ofcore data, thin-section descriptions, and
log analysis, reservoir-quality porosity isintercrystalline and ranges from 8 to 20%
and averages 16%. Reservoir thickness
ranges from 0 to 45 ft and averages 20 ft.Permeability ranges from 1 to 97 m, aver-
aging 10 to 20 md.
Net Pay. Net-pay thickness for Zone D was
determined by log analysis. The log datawere calibrated with core data, and petro-
physical values were calculated for all wells
from digital data. Net-pay cutoffs deter-
mined by porosity, permeability, produc-
tion, and relative oil/water permeabilitydata were established at 12% porosity and
water saturation < 50% for the primary
(moveable) oil reserves.
Original Oil in Place(OOIP).Well controlwithin the field is adequate to give a reliable
estimation of effective OOIP. A porosity
cutoff of 12%, average water saturation of
35%, and a formation volume factor of
1.205 yield an effective OOIP of 45.7 mil-lion bbl.
PRODUCTION PERFORMANCE
AND EOR POTENTIAL
The primary producing mechanism for
Zone D is liquid and rock expansion. A200- to 300-ft oil column has developed
within the macroporous petrofacies.
Production has included a water cut of
approximately 60%, which has remainedconstant since the initial field production.
The constant water cut and steady decline
in reservoir pressure indicate that the trap-
ping mechanism is stratigraphic and sug-
gest that there is no active aquifer. Remain-ing primary reserves of 1.25 million bbl
were calculated by decline-curve analysis.
The primary recovery factor for the field is
estimated to be 9.9% of OOIP.
EOR Potential. Several different EOR
methods were considered for the Horse
Creek field. Waterflooding was ruled out
because of oil and water relative permeabil-
ity differences which, coupled with the cur-rent water saturation, impeded the ability ofthe oil to form a bank, reducing recovery.
Gas (N2 and CO2) injection was eliminated
because of excessively high costs.
The process finally selected was high-
pressure air injection. This method provid-ed all the benefits of waterflooding and gas
injection. Technical parameters contribut-
ing to this decision include the following.
1. Reservoir temperature of 220F, indi-
cating that in-situ oxidation would occurspontaneously without downhole igniters.
2. Oil with a gravity of 32 API and agood affinity for oxidation.
3. An in-situ oxidation process with ahigh oxygen-utilization rate that indicated
good oil recovery.
4. Rapid field repressurization that
would restore reservoir pressure and
enhance early oil recovery.The decision to use the air-injection
method was influenced by the favorable
comparison of reservoir and fluid parame-
ters from the Horse Creek field with the
successful air-injection programs at twoother units in the same field.
RESERVOIR AND
LABORATORY STUDIES
A series of reservoir models, simulations,
and laboratory studies was conducted toevaluate the EOR potential and to ensure
that the most efficient and economical
recovery process was used.
Pressure/Volume/Temperature (PVT)
Analysis.A PVT analysis of the oil was per-
formed and included differential liberation
and N2 swelling tests.
Waterflood Study. A waterflood studyindicated that the field was not a good
waterflood candidate because of unfavor-
able water/oil relative permeabilities and a
low incremental-recovery factor. On the
basis of this study, waterflooding was ruledout as a possible EOR process.
Black-Oil Models. The first phase of the
reservoir modeling consisted of a black-oil
model of the southern portion of the field.
The objective of this model was to confirm
the volumetric assumption in this portionof the field and to estimate the incremental
recovery from gas injection. Results from
this model were encouraging and led to the
decision to construct a full-field model.The objectives of the full-field black-oil
model were (1) to acquire a full-field his-
tory match and confirm the volumetric
OOIP, (2) to verify the lack of water influx
into the reservoir, (3) to examine the reser-voir response to gas injection, and (4) to
provide a reservoir model for subsequent
simulations. Several different production
scenarios were tested with various injec-
tion rates and injection-well locations.Model results indicated that the best pro-
duction scenario included three injection
wells with an initial injection rate of 10
MMscf/D. The model estimated incremen-tal oil recovery of 7.6 million bbl. Fast and
reliable results from the black-oil model
enabled an initial economic projection to
be made for the project.
Accelerating Rate Calorimeter (ARC)
Tests. ARC tests were conducted to assessthe oil oxidation kinetic parameters under
quasiadiabatic conditions. Results from
these tests are qualitative but help to deter-
mine the range of conditions under which
the oil will react with air. Two main oxida-tion reactions were detected by the ARC
tests. The first reaction began at 279 to
315F and was described as a low-tempera-
ture oxidation (LTO) reaction that pro-
duced polar compounds. The second reac-tion, which began at 404 to 441F, is the
reaction that would produce significant
quantities of CO and CO2. Results from the
ARC test indicated that the oil would react
under low-temperature conditions.
Combustion-Tube Burns. Two combus-
tion-tube burns were performed at the U.
of Calgary to quantify the combustion
characteristics of the rock, oil, and brine.Both burns were conducted in a 6-ft-long
vessel with a 4-in.-diameter core from the
Horse Creek field. The experiments used
different air-flux rates and ignition tem-peratures to assess the displacementprocess. The results indicated that a pro-
gressing temperature front is established at
approximately 600F. This temperature
range is indicative of LTO. The steady
thermal-front displacement, low airrequirement, low fuel load, and high per-
centage of oil recovered indicated an effi-
cient recovery process.
Thermal Model. To obtain parameters to
describe the oil oxidation kinetics, a ther-
mal simulation of the combustion-tube-burn experiments was performed. A match
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80 JANUARY 1998
E O R / I O R
of the combustion-tube results was
obtained by use of a simple, complete oxy-
gen combustion with no coke formation.
Air-Injection Radial Model. An air-injec-
tion radial model was built with a thermal
simulator to study the conditions around
an air-injection well. This was importantbecause air-injection startup is the mostcritical phase of project operations. The
radial model used the reservoir properties
from the full-field black-oil model and the
kinetic parameters from thermal modelingof the combustion-tube experiments. The
following are some important results from
the thermal model.
1. Temperature Profile. The temperature
of the oxidation front was from 500 to700F. Following 15 years of injection, the
heated zone was estimated to be a cylinder
with a diameter of approximately 900 ft.2. Oxygen Behavior in the Reservoir.
Oxygen was consumed in a rapid and sta-ble reaction. After 15 years of injection,
oxygen did not move beyond a radius of
500 ft from the injection well. The model
predicted that no oxygen would reach a fic-
titious producer located 3,500 ft from theinjection well.
3. Hetrogeneities. Sensitivity cases with
vertical permeabilities from 1 to 300 md
showed no oxygen breakthrough and indi-cated that the oxygen did not go beyond a
radius of 700 ft from the injection well.
Full-Field Thermal Simulation. The final
phase of reservoir study included a full-field model with a thermal simulator. The
model used the reservoir properties fromthe full-field black-oil model along with a
compositional description of the oil and
introduction of chemical reactions that
enable oil oxidation and CO2 formation.
Predictive-model runs were performed for a20-year period, with air-injection rates
averaging 10 MMscf/D. Several different
injection scenarios were examined to deter-
mine the optimum location and number ofair-injection wells. The main results fromthe thermal simulation follow.
1. Incremental oil recovery was estimat-
ed at 7.2 to 7.9 million bbl.
2. The oxidization front did not go
beyond 3,500 ft from the injection well.3. Oxygen breakthrough did not occur in
the producing wells.
4. The incremental recovery with air
injection was approximately 10% more
than with nitrogen injection.5. Gas sweeping and reservoir repressur-
ization are the main mechanisms influenc-ing incremental recovery in this light-oil
reservoir. Viscosity reduction is not a sig-
nificant factor.The results of the full-field thermal sim-
ulation confirmed the economic feasibility
of the project. Data from thermal simula-
tion helped to define a field production-
monitoring program that was implemented
in the field.
PRODUCTION FACILITIES
Engineering for the project facilities began
in March 1995. Detailed design of the com-
pressors was completed and contracts for
their construction were awarded in April1995. Detailed engineering for all other
phases of the compression facility were
completed, and construction on the plant
foundations and installation of the 13-mile
fuel-gas pipeline were initiated. The com-pressors were delivered in December 1995,
and construction of the remaining facilities,including piping, instrumentation, well
conversions, and installation of high-pres-sure air lines, was completed during the
first quarter of 1996.
The injection plant for the Horse Creek
project was designed (1) to build safety
and redundancy into all systems, (2) toprovide computer control and call-out
warning systems, and (3) to meter and
control rate and pressure accurately to
each injection well.
Compressors for the project were select-ed on the basis of field-proven perfor-
mance and ability to supply the project
requirement of 10 MMscf/D at 5,000 psi.
Two Integral 8 throw, seven-stage conpres-sors, driven by two V-16 turbo-charged
natural gas engines, are used to compress
the air.
Before air injection could begin, two pro-
ducing wells had to be converted to air-injection wells and one new injection well
had to be drilled and completed. All injec-
tion wells were fitted with high-pressure
wellheads and permanent air-injection
packers with 23/8-in. tubing with premium
two-step connections, and 20,000 ft of 23/8-in. 5,000-psi air-injection lines was
installed from the compression facility tothe injection wells. All production wells in
the unit are equipped with 23/8-in.
anchored tubing and have beam pumps.
Each producing well has its own produc-
tion facility.
Safety and Environment Factors. Special
precautions must be implemented to pre-
vent explosions of hydrocarbons when
using high-pressure air injection. To reduce
this risk, the following equipment, materi-als, and processes were employed.
1. Special packers, two-step tubing con-
nections, and innovative pressure testing to
minimize the potential for downhole leaks.2. Special high-temperature lubricants
for the compressors, wellheads, and tubing
to minimize the danger of explosion.
3. Passivation of all tubulars to reduce
internal rust, corrosion, and scale.4. Wellhead controls at the injection wells
to prevent backflow and overpresssuring.
5. Dual compressors to add redundancy
and maintain constant injection to the
reservoir.6. A nitrogen-deployment system to
ensure continuous positive pressure to the
reservoir in the event that both compres-
sors malfunctioned at the same time.7. An emergency generator to provide
automatic electrical backup in the event of
a power failure.
PROJECT PERFORMANCE
The average gas/oil ratio has decreased
with repressurization of the reservior. Theaverage bottomhole pressure has increased
approximately 550 psi. Average daily pro-
duction rate has increased from 293 BOPD
to approximately 400 BOPD. All these
changes were predicted by the reservoir-simulation studies. On the basis of the lim-
ited production history, the production
goal of 1,100 to 1,300 BOPD probably will
be met.
CONCLUSIONS
1. The EOR potential of the Horse Creek
field was determined by an integrated team
of geologists and engineers.
2. A black-oil model provided fast andreliable predictions of incremental recovery
and production required to make initial
economic projections and business deci-
sions for the project.
3. ARC and combustion-tube experi-ments provided the kinetic parameters for
thermal modeling and indicated that air
injection would be an efficient recovery
process.4. Thermal simulation of the project pro-
vided the ability to examine different pro-
duction scenarios to test injector locations
and production results.
5. Production results to date indicatethat the project is proceeding as predicted
by the reservoir models and simulation
studies.
Please read the full-length paper for addi-
tional detail, illustrations, and references.
The paper from which the synopsis hasbeen taken has not been peer reviewed.
8/10/2019 EOR-IOR
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JANUARY 1998 81
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Polymer flooding is an enhanced-oil-
recovery method with great potential in
the Daqing oil field. Many new problems
will be encountered producing crude oil
mixed with polymer solution. During thewaterflood development phase, the
oil/water mixture is treated as a
Newtonian fluid. Analysis of oilfield fluids
indicates that fluids produced by polymerflooding are non-Newtonian and that con-
ventional methods of calculating inflow-
performance-relationship (IPR) curvescannot be used. This paper considers the
variation of rheological properties of fluidproduced from polymer-flooded reservoirs
on the basis of core-displacement and rhe-
ological-property experiments.
RHEOLOGICAL PROPERTIES
OF IN-SITU FLUID
The in-situ fluid in polymer-flooded reser-
voirs is a mixture of aqueous polymer
solution and crude oil. Many studies have
been conducted to determine the rheolog-
ical properties of polymer solutions, butno studies have been published on their
rheological-property variation in the direc-
tion of flow. Rheological properties of
polymer solutions change continuously
along the flow direction as a result ofadsorption, retention, and shear degrada-
tion of the solution. In laboratory dis-
placement tests, the viscosity of a polymer
solution was measured at different outlet
points in an artificial column core.Apparent viscosity decreases in the direc-
tion of flow. Assuming a power-law fluid,
the consistency coefficient, k, decreases
sharply near the inlet of the core and con-tinues to decrease slowly in the directionof flow, and the power-law exponent, n,
increases in the direction of flow. This
indicates that larger molecules of the poly-
mer are degraded and the non-Newtonian
behavior of the polymer solution is
reduced in the direction of flow.
FLOW BEHAVIOR OF POLYMER-
SOLUTION/OIL MIXTURE
Core-displacement experiments were per-
formed in the laboratory to compare thebehavior of polymer-solution/oil mixtures
with different volume ratios with that ofsingle-phase polymer solution. When pres-
sure drop is plotted vs. equivalent shear
rate on a log-log graph, the polymer-solu-tion/oil mixture plots are identical to that
for polymer alone at shear rates greater
than 10 seconds-1. This indicates that a sin-
gle-phase fluid model can be used to calcu-
late the pressure drop of polymer-solu-tion/oil mixtures.When flow rate and pres-
sure drop through a core are plotted, the
pressure drop varies linearly with the nth
power of the flow rate. The relationship of
pressure drop and flow rate exhibits thebehavior of a non-Newtonian power-law
fluid in the porous media. At high flow
rates, the pressure drop increases, deviating
from the power-law model, indicating that
the rheological properties of the polymersolution in porous media are not the same
as in a capillary tube.
IPR CURVES FOR OIL WELLS
The apparent viscosity of polymer solution
varies greatly during the time the solutionis mixed at the surface, injected, and finally
produced with the oil. In the Daqing oil
field, the apparent viscosity decreasesapproximately 30% from the time it ismixed to the time it reaches the injection
wells. Apparent viscosity decreases 60%
when it reaches an observation well 30 m
from the injection well and 70% at a pro-
duction well 106 m away. This indicatesthat the loss of apparent viscosity is large
near injection wells. Severe shear degrada-
tion of large polymer clumps usually occurs
near the bottom of injection wells, decreas-
ing the non-Newtonian behavior of thepolymer solution. When the shear rate is
greater than the critical shear rate, the fluidexhibits viscoelastic behavior in the vicini-
ty of the wellbore and power-law fluid
behavior in the formation. The full-length
paper contains a differential equation forinflow performance. This equation com-
bines equations of continuity, motion, and
state. Boundary conditions are defined.
Calculations. An IPR curve was calculatedwith the derived equation. When calculat-
ed flowing bottomhole pressures were com-pared with measured values, the maximum
absolute error was 230 kPa and the maxi-mum relative error was 5.82%. The close
agreement of measured and predicted val-
ues indicates that variable rheological para-meters must be used to predict IPRs for oil
wells in polymer-flooded reservoirs.
Analysis of IPR curves of oil wells shows
that, when the rheological parameters offluid vary in injection and production
wells, the pressure drop in the formation
increases as the k of the produced fluid
increases and n decreases. Pressure drops
decrease ask decreases and n increases.
Case History and Influence Factors.
Polymer-solution rheological parameters
were measured for an oil well in a poly-
mer-flooded reservoir in the Daqing oil
field with a permeability of 475 md, and aporosity of 0.267. The concentration of
the injected polymer solution was 1000
mg/L, k = 0.0809 Pas, and n = 0.5637.The value of k for the fluid produced from
an oil well in this field was 0.0145 Pasand n was 0.809.
CONCLUSIONS
1. Rheological properties of formationfluids in polymer-flooded reservoirs change
in the direction of flow.2. Calculations of IPR curves for oil wells
in polymer-flooded reservoirs need to
include variations of rheological properties as
the fluids flow through the reservoir.
Please read the full-length paper for
additional detail, illustrations, and ref-
erences. The paper from which the syn-
opsis has been taken has not been peerreviewed.
CALCULATION OF IPR CURVES FOR OIL
WELLS IN POLYMER-FLOOD RESERVOIRS
This article is a synopsis of paper SPE
38936, Calculation of IPR Curves of
Oil Wells for Polymer-Flooding Reser-
voirs, by Yue XiangAn, SPE, Xia
Huifen, Yunxiang Zhang, and Li
Jingyuan, Daqing Petroleum Inst., orig-
inal ly presented at the 1997 SPE
Annual Technical Conference and
Exhibition, San Antonio, Texas, 58October.
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Field testing has confirmed that a newly
discovered, modified hot-lime process
(MHLP) is a significant improvement overexisting precipitation-softening options. A
Permian Basin produced oilfield water
containing 2,000 ppm hardness, 500 ppm
sulfides, 10,000 total dissolved solids
(TDS), and 200 ppm oil is being convert-ed successfully to steam-generator-quality
feedwater. Alkali consumption and sludgeproduction have been reduced by 50%
compared with the conventional process.In addition, alkali consumption by
entrained CO2 is eliminated. Many hot-
lime softeners (HLSs) currently in service
can be inexpensively converted to this
more efficient process.
The lack of economical water treatmentis one of the most critical obstacles to
achieving a successful steam-injection pro-
ject. Because of strict environmental regula-
tions and lack of available fresh water, pro-
duced oilfield water is typically used assource water for steam generation. For
most steamfloods, quality of the produced
water is fair and sufficient treating can be
accomplished with typical oil-removal andsoftening techniques. In many west Texas
oil fields, however, produced-water quality
is much worse than that currently used for
steam generation. Hardness and sulfide lev-
els are 10 times the average for Californiasteamflood source waters.
Identification of the significant reserves
and economic potential of a thermal project
in a large west Texas oil field led Marathon
Oil Co. to embark on an operational steamfield test in 1995. The test consisted of
installation of a 5,000-BWPD oilfield
water purification facility and three sin-
gle-pass waste-heat steam generators and
drilling of one steam-injection well.
WATER QUALITY
Steam for most oilfield steamflooding is
produced in conventional steam genera-tors. These generators are fired with nat-
ural gas or waste heat and use a single-
pass tube arrangement to produce 80-
quality steam. Saturated steam (including
the 20% liquid phase) is injected into theoil formation with steam-injection wells.
Many impurities in the steam-generatorfeedwater can be tolerated because the
20% liquid phase provides a place forthem to concentrate and still remain solu-
ble. However, according to typical steam-
generator-manufacturer guidelines, all oil,
sulfides, hardness, and suspended solids
must be removed to prevent damage tosteam-generator tubes. Oil in the feedwa-
ter contributes to film formation and cok-
ing in the generator tubes, resulting in
their eventual failure. Sulfides are
believed to be corrosive. Hardness deposi-tion creates steam-generator scaling,
eventually leading to hot spots and tube
failures. Suspended solids must be
removed because they contribute to for-
mation of steam-generator sludge. Typicalsteamflood source waters contain 200 ppm
hardness and essentially no sulfides. The
extremely high amounts of hardness and
sulfides in the source water in this westTexas field made their removal the major
challenge for a successful project.
OVERALL PROCESS FLOW
Produced oilfield water first enters a hydro-
cyclone for rough-cut oil and water separa-tion. Oil content is reduced from 200 to 40ppm. Next, single-media filters are used to
reduce oil content further to 10 to 20 ppm.
Water then enters a packed column, where
nitrogen at 4 scf/gal is used to reduce sul-
fide levels from 500 to< 200 ppm. An oxy-gen scavenger is added to reduce oxygen
content from 20 to approximately 0 ppb.
Water is then pumped to the modified hot-
lime softener (MHLS), where heat, lime,
and caustic are added. Hardness is reducedfrom 2000 to 4 ppm here. Anthracite filters
are used next to remove any suspended cal-cium carbonate (CaCO3) and magnesium
hydroxide [Mg(OH)2] precipitates. Weak
acid cation vessels are then used to polish
hardness to
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water and collected in the lower cone or
solid/liquid separation chamber. Here, pre-
cipitated material is separated from the soft-
ened water in the form of sludge. Periodic
blowdown is performed to remove thismaterial from the vessel.
MHLP. After additional laboratory and field
testing, a new, more efficient method was
discovered and commercially demonstrated.The process is a variation of the standard
HLP. Fig. 2 shows a schematic of the modi-
fied vessel. Instead of adding heat, lime
and/or caustic simultaneously to precipitatehardness, as in the existing HLP, the MHLP
precipitates hardness in two separate steps.In the first step, cold, hard water enters the
vessel and is sprayed into a steam atmos-
phere and heated to near boiling, just as in
the standard HLP. Soda ash can be added atthis point to supply the necessary bicarbon-
ate ion for hardness precipitation if the ion
is not present in sufficient quantities natu-
rally. However, instead of adding lime or
caustic soda at this point, the MHLP allowsretention time for precipitation reactions
resulting from only the addition of heat totake place. Laboratory and field testing has
shown that 10 to 20 minutes is required for
completion of thermal softening reactions at
vessel operating temperatures. If less reten-tion time is allotted (as with the HLP), ther-
mal reactions will not take place. Instead,
the preference for reactions with lime and
caustic overrides thermal reactions. The
amount of thermal softening that takesplace can be significant. In the field test,
produced oilfield water was softened from
2,000 to < 1,000 ppm in this step, with-
out any chemical addition.The second step of the MHLP consists of
adding lime and/or caustic soda to precipi-tate hardness not removed during thermal
softening in the first step. Chemical reac-
tions that take place are identical to those in
the HLP. Resulting reactions from the addi-
tion of heat and chemicals form CaCO3 andMg(OH)2 precipitates. The amount of pre-
cipitates generated by the MHLP is signifi-cantly less than that of the HLP. Only 1
mole of CaCO3 is created per mole of hard-
ness during Step 1 (thermal softening)compared with 2 moles /mole of hardness
generated in Step 2 (lime softening). This
translates to a significant reduction in the
amount of precipitated solids. Typically
these solids are hauled to a landfill, whichcan prove costly. The MHLP has several
additional benefits.
1. Improved Removal of H2S. H2S is diffi-
cult to remove from water at elevated pH.
Because the typical HLP quickly elevateswater pH by introducing lime early, gaseous
H2S is converted to ionic sulfide, which
cannot be removed. The MHLP does not
elevate pH significantly for several minutes,
so H2S is removed by steam deaerationmuch more effectively.
2. Elimination of Lime Consumption by
CO2. The standard HLP introduces lime
into the vessel in the steam/vapor space
where CO2 can exist. CO2 dissolved in the
produced water will react with added limeand create CaCO3. Therefore, the presence
of CO2 increases alkali demand and
increases the amount of precipitated solids,both of which are unfavorable. The MHLPeliminates these problems because the alka-
li is introduced below the water level in the
vessel. CO2 does not exist in water at HLP
temperatures (it is driven off by Step 1 heat-
ing) and therefore cannot consume lime.
Existing HLS can be inexpensively con-verted to this more efficient process. Most
vessel designs currently in service afford
necessary retention time for thermal reac-
tions to occur in the reaction chamber ofthe vessel. The primary modification
required for conversion is lowering thealkali feed point from the top of the reac-
tion chamber to the top of the reaction
chamber downcomer.
USE OF TWO ALKALIS TO
IMPROVE PERFORMANCE OF THE
PRECIPITATION PROCESS
When lime alone is used, pH must be main-
tained in the very tight pH range of 9.3 to9.6 to achieve acceptable effluent hardnesslevels. If the pH levels fall outside this
range, hardness levels climb quickly. To
overcome this chemistry problem, both
lime and caustic are fed to precipitate
hardness in the HLS. After thermal soft-ening takes place in the upper portion of
the reaction chamber, hydrated lime is
added to boost the pH to near 9.0.
Hardness is reduced to approximately 100ppm. The result is precipitation of large
amounts of hardness with cheap lime. A
relatively small amount of caustic soda isthen added to precipitate the majority of
remaining hardness. Because caustic sodais free of calcium ions, hardness does not
increase when overfed. While caustic
could be used exclusively and accomplish
the same result, the relatively high cost of
the chemical makes this economicallyunattractive for high-hardness waters.
Fig. 1HLS vessel.
Solid/Liquid
SeparationChamber
Fig. 2MHLS vessel.
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In addition to producing CaCO3 and
Mg(OH)2, sodium carbonate (Na2CO3) or
soda ash is also formed by caustic reactions.
Presence of these excess carbonates allowsthe process to achieve extremely low hard-
ness levels. Effluent hardness levels less
than 4 ppm have been routinely achieved in
the precipitation softener.
TEST PROJECT OPERATING
CHALLENGES
Plugging. The MHLS has been in service
for more than 1 year. After design refine-
ments were complete, operating efficiencyand operability have surpassed expecta-
tions in many respects. However, the
major operational challenge still facing
the vessel is periodic plugging of the reac-
tion chamber and downcomer with pre-cipitated hardness. Field testing estab-
lished that standard HLSs require signifi-cant modification to accommodate the
solids generated from precipitation soft-ening of west Texas produced oilfield
water. With the standard design HLS,
operation would be halted after 2 weeks
because of a plugged reaction-chamber
downcomer. Through a series of improve-ments, periods of run time for the MHLS
extended significantly. Those modifica-
tions include the following.
1. Enlargement of the reaction-chamber
downcomer. Typically, reaction-chamberdowncomers are sized to achieve a down-
ward water velocity of 1 ft/sec. Field expe-
rience indicates that a more appropriate
design criterion for extremely hard waters
is 0.5 ft/sec.2. Modification of the downcomer
splashplate to a witchs hat design.
Standard HLSs use a flat plate at the bottom
of the reaction-chamber downcomer to pre-vent disturbance of the sludge below. Field
testing operations suggested that the stan-
dard splashplate design allowed precipitat-
ed solids to stack, eventually plugging the
downcomer. The current witchs hat design
allows solids to slough off much moreeffectively.
3. Creation of a high-rate cyclonic
motion in the 10-ft-diameter reaction
chamber with tangential nozzles. To keepprecipitated solids in suspension as water
moves down the downcomer, 600 gal/min
of water (from the reaction chamber) is
recirculated.4. Use of a steeper-sloped reaction-cham-
ber cone. Standard HLS design calls for a
45 from horizontal cone in the reaction
chamber, even though the sludge repose
angle is greater than 50. Future vesseldesigns will use a 60 from horizontal cone
in an attempt to alleviate the plugging ten-
dencies further.
Sulfide Removal. Sulfide removal from the
source water was the second significant
technical challenge for project engineers.
Removal of an extremely large amount of
sulfides (500 ppm) in steam-generatorfeedwater is very unusual. Use of conven-tional methods to accomplish this would
adversely affect water-treating costs.
Initially, complete sulfide removal, as
recommended by steam-generator-manu-facturers guidelines, was thought to be
necessary. Experience from other steam-
flood operators, however, indicated that
this was not necessarily true. Steamflood
operators in California have operated foryears with source waters containing 40
ppm sulfides and have reported no signif-
icant problems. With this information, atwo-pronged strategy to the sulfide issue
was adopted. First, an uncommon sulfide-removal technique would be engineered
and installed that would reduce sulfide
levels to less than 40 ppm. Second, field-
testing facilities would be used to deter-mine whether higher sulfide levels were
tolerable. For example, if the upper sul-
fide level limit could be extended to 200
ppm, water-treating costs would be
reduced, thereby improving project eco-nomics. Also, field experience found that
sulfide levels below 200 ppm prevented
interference with hardness reactions in
the MHLS. Sulfides under certain condi-
tions were found to tie up available car-bonate alkalinity needed for the process,
thereby creating permanent hardness in
the water.
After more than 1 year of steam injection,
no significant corrosion is evident in thewater plant or steam system with boiler
feedwater containing 200 ppm sulfides.
Therefore, 200 ppm sulfides will be the
newly established upper sulfide target forfuture water-plant designs. Nitrogen with-
out any sort of pH adjustment will be usedto accomplish this level of reduction.
Conventional Sulfide Removal. Sulfides
exist in both ionic and gaseous forms at pHlevels of typical oilfield waters. To remove
all sulfides, water pH must be lowered to
below 5 to convert ionic sulfide to H2S.
Hydrochloric acid is the agent used typical-ly for pH reduction. H2S can then be
removed effectively with conventional
stripping techniques. The problem with
using conventional methods before a pre-
cipitation process is that added acid signifi-
cantly reduces the amount of alkalinityneeded for hardness precipitation. Lost
alkalinity must therefore be replaced in the
form of Na2CO3. This approach of elimi-
nating alkalinity with acid to remove sul-
fides, then replenishing that lost alkalinitywith an additional chemical, is expensive
and unnecessary.
Uncommon Sulfide Removal Method.
The original sulfide removal techniqueused CO2 as both the stripping gas andagent for pH reduction. CO2 forms carbon-
ic acid, bicarbonate, and carbonate when
dissolved in water. The free hydrogen-ions
released by dissociation of carbonic acid
reduce the pH of the water. Laboratory andfield testing indicate the water pH can be
reduced to less than 5 by dissolved CO2.
Because the reactions are reversible, no
adverse effect on alkalinity occurs.
Nitrogen is not as effective as CO2 becausethe water pH actually increases as a result of
stripping of entrained CO2 with the sul-fides. Blending even small amounts of CO2into the nitrogen stream significantly
improves packed-column performance.Adding only 10% CO2 to the nitrogen strip-
ping gas stream removes an additional 90
ppm of sulfides. Any CO2 dissolved in the
water is effectively removed by heating in
the downstream HLS.
CONCLUSIONS
1. A new process for converting hard oil-
field water to boiler-quality feedwater has
been developed and commercially demon-strated. Alkali consumption and sludge
production have been reduced by 50%,
compared with the standard HLP.
2. The addition of small amounts of caus-
tic soda to the MHLP enhances the stabilityand efficiency of softening in high-hardness
west Texas source waters.
3. CO2 is effective at removing sulfides
from water without adversely affecting
water chemistry in regard to softening.However, piping and vessels exposed to
dissolved CO2 must be protected to pre-
vent corrosion caused by carbonic acid.
4. Sulfide levels up to 200 ppm in steam-generator feedwater have resulted in no sig-nificant corrosion to steam generation and
distribution equipment after 1 year of oper-
ation. At a typical produced-water pH, this
level of reduction can be accomplished
with nitrogen.
Please read the full-length paper for
additional detail, illustrations, and ref-
erences. The paper from which the syn-
opsis has been taken has not been peerreviewed.
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JANUARY 1998 85
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The Simonette Beaverhill Lake A and B
pools were discovered in September 1993.
Enhanced recovery (EOR) by water-alter-
nating-gas (WAG) miscible flooding was
initiated in May 1995. This short, 20-
month cycle time was achieved through
careful planning, multifunctional team
work, and close cooperation between the
partners in all critical decisions. The chal-
lenges to develop Simonette, including uni-
tizing, well spacing and scheduling, con-
serving gas, and selecting the type of floodwere identified in a development plan cre-
ated before discovery. Keys to economic
success were also identified in the planning
stage. When the discovery was made, a
multidisciplinary development team was
formed. Much effort was spent on under-
standing and meeting the needs of all inter-
ested parties, including partners and regu-
latory agencies.
GEOLOGY
Oil is trapped in the Simonette Beaverhill
Lake A and B pools in the updip culmina-tion of a Swan Hills reef, a part of the
Beaverhill Lake group. The Beaverhill Lake
group comprises the Swan Hills formation,
consisting of reefal carbonates, and the
Waterways formation, composed of basin-
filling marlstones and carbonate mud-
stones. The A pool is separated from the B
pool by a normal fault with approximately
30 m of throw. The reefs were deposited in
a series of eight reef stages that grew in
response to rising sea levels. Development
and management of the reservoir is driven
by the properties and relationships of thesestages. Stage porosities within a well range
from 7 to 12%, and permeabilities can
range from 1 to 400 md.
PLANNING
Exploration Economics. The Simonette
exploration prospect was characterized as
having a geologic risk of one in five and
recoverable oil from 795 to 5500103 m3.
The area ranged from 24 to 40106 m2.
Net pay was expected to be from 7.5 to
12.0 m. The original development plan
called for a waterflood with 65-ha spac-ing, the same as most Beaverhill Lake
reservoirs in Alberta, and a nominal five-
spot pattern. With the estimated
exploratory risk of one in five, the
prospect was considered uneconomical.
The performance of other Beaverhill
Lake reservoirs showed that 80% of the
recovery was obtained from 20% of the
wells. Flood-front mapping of other
waterfloods showed that water injectors
could sweep oil as much as 4.83 km. The
performance of these reservoirs caused
the development plan to be revised to use
130-ha spacing.
Improved Oil Recovery (IOR). Implicit in
the economic evaluation was the need for
EOR. Expected primary recovery factors
were 10 to 20%, which would not support
the well investment and facilities cost.
Waterflooding was considered the mini-
mum depletion mechanism. In addition,
the Alberta Energy and Utilities Board
(AEUB) limits production from a reservoir
by a maximum rate limitation (MRL) that istypically 9000 m3 per month/1106 m3 of
recoverable oil.
Development Plan Goals. A Gantt Chart
for the development plan was presented
to management. If this extremely aggres-
sive timeline could be met and the pool
developed on 130-ha spacing, the explo-
ration economics were very attractive.
The following were major challenges in
the timeline.
Designing and selecting a flood with
only three to four wells out of an ulti-mate pool development of 19 wells.
Obtaining AEUB approval in 3 months
with limited data when 6 to 12 months
is typical.
Unitizing the pool within 2 years, withthe same data limitations.
After management was assured that the
timeline would be met, approval was
given for drilling the discovery well in
June 1993. After discovery, water injec-tion was achieved 6 months ahead of plan
and gas injection began 4 months ahead
of the injection target date.
LABORATORY STUDIES
Reservoir fluid studies and laboratorycorefloods are critical sources of data for
designing and selecting a flood scheme for
a reservoir. Representative samples from
the dominant flow facies were selected for
waterflood tests, relative permeabilitydetermination, and (combined with fluid
studies) miscible flooding potential. A set
of capillary pressure curves, covering a
range of porosities and permeabilities, was
determined. These data were gathered tocreate a permeability transform to popu-
late a reservoir-simulation model. The
composition analysis revealed that solu-
tion gas from Simonette could be used as amiscible solvent for the oil. This finding
was instrumental in the decision to use a
miscible flood.
REGULATORY ENGAGEMENT
The AEUB must approve all recovery
schemes as part of their mandate to con-serve the energy resources of Alberta. AEUB
approval can take up to 1 year if they iden-
tify issues with a proposed scheme thatrequire additional laboratory or simulationstudies. Because approval was required
within 3 months of application with little
data, a meeting was held to explain the
nature of the reservoir, development plans,
and the need for a short cycle time. Thestaff of the AEUB raised several questions.
The objectives of the simulation studies
were set to address these. The AEUB staff
was kept informed of the findings and con-
clusions of various studies. The final appli-cation was submitted in October 1994 with
data from only three wells. The applicationwas updated with information from an
A MODERN EXAMPLE OF SHORT-CYCLE-
TIME DEVELOPMENT
This article is a synopsis of paper SPE
38824, Simonette Beaverhil l Lake
A&B Pools: A Modern Example of
Short-Cycle-Time Development, by
T.J. Moynihan, SPE, Chevron Canada
Resources; J.C. Fryters, Chevron
Petroleum Technology Co.; and P.
Chernik, SPE, Shell Canada Ltd. origi-
nal ly presented at the 1997 SPE
Annual Technical Conference and
Exhibition, San Antonio, Texas, 58October.
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additional five wells in January 1995, and
approval of miscible flood for the Simonette
A pool was obtained in March 1995.
EARLY PERFORMANCE
MONITORING
As each well was drilled, a temporary bat-
tery was installed at the wellsite. T