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  • 8/10/2019 EOR-IOR

    1/21 JANUARY 1998 69

    E O R / I O R

    CO2 foam has been used as an effective

    mobility-reducing agent for CO2 flooding

    in the oil-recovery process. Recent researchindicates that some CO2 foams can provide

    selective mobility reduction (SMR). SMR in

    foams reduces CO2 mobility by more in

    higher- than in lower-permeability cores in

    laboratory experiments. Unlike Darcy flowof ordinary fluids in rocks, where the

    mobility is proportional to rock permeabil-ity, the mobility of foam with SMR is less

    than proportional to core permeability and

    foam flows through higher-permeabilityrocks at a lower rate than would be expect-

    ed for the existing pressure gradient. This

    allows foam to flow at the same velocity in

    high- and low-permeability regions in thereservoir, preserving the uniformity of the

    flood front while propagating through

    rocks with nonuniform permeability. Use of

    a CO2 foam with SMR delays CO2 break-

    through and provides a high displacement

    efficiency in heterogeneous reservoirs.

    FOAM-DURABILITY TEST

    For this study a high-pressure foam-dura-

    bility test apparatus was constructed and

    screening tests were conducted successfullyto select surfactants for field foam applica-

    tion. The test determined the foaming abil-

    ity of each surfactant, the stability of foam,

    and surfactant properties, such as the inter-

    facial tension (IFT) between a surfactantand dense CO2 and the critical micelle con-centration (CMC) of a surfactant. The

    foam-durability apparatus comprises a CO2source tank, a visual cell made from a trans-parent sapphire tube, a buffer-solution

    cylinder, and a pump. The major partof the

    system, the CO2 tank and sapphire-tube

    high-pressure cell, is contained in a tem-

    perature-controlled water bath. The buffer-solution cylinder and the pump are

    installed outside of the water bath, and

    their temperatures are maintained at the

    same temperature as the water bath by a

    separate temperature-control system.During operation, the sapphire visual cell

    is first filled with the solution to be tested.Once the system reaches the desired pres-

    sure, the dense CO2 is introduced through a

    needle at the lower end of the cell. The CO2is drawn upward inside the cell. The densi-

    ty difference between dense CO2 and the

    tested solution causes CO2 bubbles to form

    and collect at the upper end of the cell.

    These bubbles will either form a layer offoam-like dispersion at the top of the sap-

    phire tube or coalesce into a clear layer of

    dense CO2, depending on the effectiveness

    of the surfactant. After 1.75 cm3 of CO2 has

    been introduced into the sapphire tube, thepump is stopped and the length of time that

    the formed foam persists is measured.

    Surfactant solutions (1 wt% active compo-

    nent) were prepared by dissolving the sur-

    factant as received from the suppliers into abrine system consisting of 5.6 wt% NaCl

    and 1.4 wt% CaCl2. Different concentra-

    tions of the surfactant solution were pre-

    pared by diluting the batch solution withthe 7 wt% brine. All screening tests were

    conducted at 77F and 2,000 psig.

    By measuring the time required to form a

    bubble at the needle in the sapphire tube

    and the number of bubbles formed within acertain time period, the average volume

    and radius of each bubble is calculated.Once the average radius of dense CO2 is

    known, the IFT between surfactant solu-tion and dense CO2 can be calculated.

    Results and Discussion. The IFT decreas-

    es with surfactant concentration and levels

    off at a region where the IFT no longer

    decreases as surfactant concentrationincreases. The concentration at which the

    interfacial properties between surfactant

    and CO2 show no significant change is the

    CMC and can be graphically determined.

    The IFT curves and CMC values vary withsurfactant formula. The CMC values for

    Surfactants 1 through 5 are 0.04, 0.06, 0.07,

    0.07, and 0.35 wt %, respectively.

    The foaming ability of a surfactant is

    defined as the ease with which a bubble isformed at the needle when the surfactant

    CO2-FOAM FLOODS:

    FOAM PROPERTIES AND

    MOBILITY-REDUCTION EFFECTIVENESS

    This article is a synopsis of paper SPE

    37221, Assessment of Foam

    Properties and Effectiveness in Mobility

    Reduction for CO2-Foam Floods, by

    Jyun-Syung Tsau, SPE, and Reid B.

    Grigg, SPE, New Mexico Petroleum

    Recovery Research Center, New

    Mexico Inst. of Mining and Technology,

    originally presented at the 1997 SPE

    International Symposium on OilfieldChemistry, Houston, 1821 February.

    Fig. 1Decay of CO2 foam with Surfactant 4.

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    70 JANUARY 1998

    E O R / I O R

    solution contacts the CO2. Durability is

    defined as the persistence of foam bubbles

    after a standard volume of CO2 has been

    introduced. A cathetometer is used to mea-sure the foam height and the weight of the

    CO2 to allow calculation of the percentage

    of foam inside the sapphire tube and assess-

    ment of the persistence of foam. Foam wasfound to form more easily as the surfactantconcentration increases. The foaming abili-

    ty of surfactant increases as the IFT between

    CO2 and the surfactant solution decreases.

    The longest-lasting foams were not neces-

    sarily found at the best foaming conditions.For Surfactant 4 (Fig. 1), there is an opti-

    mum concentration (0.075 wt%) at which

    the foam has the best stability or the longest

    durability. The persistence of foam decreas-

    es at concentrations either above or belowthis optimum concentration. This trend was

    observed with Surfactant 1, with an opti-mum concentration of 0.05 wt%. In both

    cases, the optimum concentration is close to

    the surfactants CMC (i.e., 0.07 forSurfactant 4 and 0.04 for Surfactant 1). The

    bubbles formed by Surfactants 5 and 2 coa-

    lesced in less than 1 minute, whereas most

    of the bubbles formed by Surfactant 3 lasted

    longer than 90 minutes. The optimum con-centration for generating the longest-lasting

    foams were not identified for Surfactants 5,

    2, and 3. Surfactant 3 generates the most

    stable foams, followed by Surfactants 4, 1, 2,and 5 (listed by decreasing level of stability).

    FOAM-MOBILITY TEST

    Core systems containing well-defined high-

    and low-permeability regions were con-

    structed to assess the flowing-foam proper-ties and verify the existence of SMR in het-

    erogeneous porous media. This experiment

    used two well-defined permeability regions

    in capillary contact arranged in series. The

    series assembly uses two 1/2-in.-diameter

    cores approximately 3 in. long. The core-holder is fitted with five equally spaced

    pressure taps so that the middle tap is near

    the junction of the cores. The abutting endfaces of the cores are carefully cut perpen-dicular to their axes and ground flat before

    mounting end to end. The space between

    the two core faces is filled with fine sand.

    Pressure differences between each pair of

    pressure taps is recorded. The fluids flowinginto a foam generator and the composite

    core are injected by two pumps, a positive-

    displacement pump for the CO2 and a pis-

    ton pump for brine or surfactant solution.

    The pressure is maintained at an almost

    constant level by leading the output fluids

    into a backward-running piston pump.When the experimental conditions reach

    steady state, pressure drops in each segment

    of the core are recorded as functions of time.

    The mobility of injected fluid, defined as theratio of Darcy or superficial velocity of the

    fluid to the average pressure gradient along

    each segment of core, is calculated and com-

    pared for different injection conditions.

    The foam generator and core sample arepreflushed with synthetic brine for at least 40

    pore volumes (PV) before the brine perme-

    ability measurements are begun. The hetero-

    geneity of the series composite core was

    determined by measuring the brine perme-abilities for four different sections along the

    core. Following the permeability measure-

    ments, dense CO2 and brine were injected

    simultaneously into the core sample. The

    mobility of the two-phase mixture was mea-

    sured for each core section and used as a ref-erence for later comparison. After establish-

    ing the baseline, a sequence of foam experi-ments was performed. To satisfy the adsorp-

    tion requirement, 50 PV of surfactant solu-

    tion was displaced. Then CO2 and surfactantsolution were injected into the core until

    steady-state conditions were reached. Foam

    mobility was measured. The ratio of volu-

    metric flow rate of CO2 to aqueous phase was

    maintained at four to one. The total injectionrate was varied from 5.0 to 15.0 cm3/hr cor-

    responding to velocities of 3.1 to 9.4 ft/D.

    The two composite cores had permeabilities

    ranging from 525 to 128 md for Core 1 and

    819 to 106 md for Core 2. Surfactant con-centrations of 0.1 wt% were used in Core 1

    experiments, while 0.05 wt% surfactant solu-

    tions were used in Core 2 experiments.

    Results and Discussion. Comparison of themobility data in the first three core sections

    indicates that the mobility of CO2/brine is

    reduced by the addition of surfactant. Foam

    mobilities are significantly lower than the total

    mobility of CO2/brine. This mobility reduc-

    tion varies with surfactant, surfactant concen-tration, and flow condition. In general, foam

    mobility is lower when foam is generated at

    higher surfactant concentrations or whenfoam is displaced at a lower injection rate.

    When mobility dependence on rock per-

    meability is examined, SMR is also found to

    depend on the surfactant type, concentra-

    tion, and flow rate. When the mobility of

    CO2/brine or CO2/foam is plotted vs. the

    sectional permeability, the slope of the lineindicates the degree to which the the mobil-

    ity of fluid depends on the permeability of

    porous media. A slope of one indicates that

    the mobility of the fluid is proportional tothe rock permeability as described by

    Darcys law. A value of less than one shows afavorable dependence of SMR that will lead

    to a more uniform displacement front when

    the fluid is flowing through heterogeneous

    porous media. In general, the value of theslope decreases when surfactant is added to

    the brine as a foaming agent. This suggests

    that foam is useful in correcting the nonuni-

    form flow of CO2 and brine in a porous sys-

    tem containing differing permeabilities. Atlower velocities, the value of the slopedecreases, indicating a more favorable SMR

    occurs at a lower displacement rate.

    When results from the foam-durability

    tests are compared with the mobility tests,

    the stability of foam in the bulk phase canbe correlated with the effectiveness of

    mobility reduction of flowing foam in the

    porous media. The mobility reduction is

    enhanced as foam stability increases. Themobility-reduction factor (MRF), defined as

    the ratio of total mobility of CO2/brine to

    foam mobility, increases with the foam life.When foams become more stable, more

    resistance to flow results in a higher mobili-

    ty reduction. On the basis of these observa-tions, the capability of surfactant in stabiliz-

    ing the bubble file or lamellae in the porous

    media is believed to be the most likely rea-

    son for the effectiveness of foam in reducing

    the mobility of CO2.Use of a proper CO2 foam could minimize

    the mobility contrast between high- and low-

    permeability zones in reservoir flow, increas-

    ing the efficiency of oil displacement.

    Experimental research indicates that the SMRproperty of CO2 foam is real. It is observed in

    parallel- and series-core tests with capillary

    contact and can be presumed to function

    similarly in actual field situations.

    CONCLUSIONS

    1. The stability of foam in the bulk phase

    can be correlated with the performance of

    foam flowing in porous media. When com-

    paring different surfactants, greater foamstability gives more mobility reduction in

    foam displacement.

    2. The MRF increases as the reduction

    factor of the IFT between CO2 and theaqueous phase increases.

    3. An optimum concentration exists atwhich the most stable foam in the bulk phase

    is formed. This optimum concentration is

    close to the CMC of each surfactant solution.

    4. Factors that favor reducing the mobili-ty of CO2/brine also lead to a more favorableSMR when foam flows in a composite core

    consisting of differing permeabilities.

    Please read the full-length paper for addi-

    tional detail, illustrations, and references.

    The paper from which the synopsis hasbeen taken has not been peer reviewed.

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    JANUARY 1998 71

    E O R / I O R

    After the 1973 oil embargo, the U.S. gov-

    ernment funded several initiatives to pro-

    vide additional worldwide resources as a

    means of lowering oil prices. One of these

    initiatives was Project Deep Steam. Thisproject evolved on the theory that signifi-

    cant reserves of heavy oil, worldwide,

    were beyond the reach of surface-generat-

    ed steam because of heat losses in the tub-ing. Two approaches were taken to achieve

    the goal of steam delivery to deep forma-

    tions. One was to improve or develop newinjection strings to minimize heat loss,

    and the second was to design and demon-strate the operation of a device that would

    generate steam in the wellbore at the

    depth of the formation. Sandia Natl.

    Laboratory was given a U.S. $23 million

    budget for a 4-year program beginning in1976. Sandia initiated an in-house effort

    for steam-generator development. Both

    the insulated-injection-tubing develop-

    ment and testing were carried out by

    external contract.The outside diameter (OD) of the down-

    hole steam generator could not exceed 4.5

    in. This OD would fit inside 7-in. casing. To

    achieve large-magnitude firing rates, thecombustion process would have to occur at

    high pressure. Steam would be generated in

    either of two ways. One was by a tradition-

    al heat-exchanger surface that separated the

    hot flue gases from the water. Adequate sur-face for efficient heat transfer was obtained

    by heat-exchanger lengths of up to 100 ft.

    The cooled flue gases were exhausted up

    the annulus. Combustion did not have to

    occur at pressures as high as those required

    for injection. In the second method, com-bustion occurred at high pressure and

    water was injected directly into the hot flue

    gases. Then, both steam and flue gases were

    injected into the formation. Injection of theflue gases proved to be either a benefit or a

    problem; one benefit was that it was helpfulin the air-quality permitting process.

    Operation of both downhole steam genera-

    tors could be carried out on the surface,

    with injection tubing transporting the

    steam downhole. The Sandia developmentand one of the outside contracts were based

    on a direct-contact steam generator. The

    other outside contract was for an indirect-

    contact steam generator.

    FIELD OPERATIONSKern River Field. The equipment for this

    test was sized for a delivery of 5 million

    Btu/hr at a maximum pressure of 400 psi.Along with the steam, nitrogen and carbon

    dioxide were generated. The combustion

    was carried out with minimum excess air.

    Because this was the first operation of a

    direct-contact steam generator of Sandiadesign, the generator was operated on the

    surface rather than downhole. The OD of

    the steam generator was 4.5 in., and liquid

    propane was the fuel. The Kern River field

    had been steamflooded for a number ofyears before this test, and the injector well

    communicated quickly with surrounding

    production wells because of this previous

    steaming. No particular increase in produc-tion was noted because this was a rather

    mature steamflooded field.

    Wilmington Field. For this operation two

    different generators and support systems

    were demonstrated simultaneously. Thefirst was operated downhole, and the sec-

    ond was operated on the surface. Both were

    fired with air as the oxidizer and diesel as

    the fuel.Downhole Air/Fuel Generator. The out-

    put for this system was sized for 5 million

    Btu/hr at a pressure rating of 1,400 psi.

    Installation of the generator was a rather

    complex task. The connectors from the

    generator to the surface consisted of twojointed tubulars and four continuous tub-

    ing lines. The air line was 23/8-in. jointed

    tubing and was the load-bearing element

    for the installation. Water was conducted

    down 1.66-in. jointed tubing that had to be

    made up by hand tools after the larger tub-

    ing had been made up with power tools.The other lines were continuous coiled tub-

    ing that had to be pulled out of the way by

    hand to make up the jointed tubulars.

    These four lines were attached to the 23/8-

    in. tubing by a custom-made cast-alu-

    minum clamp. Because diesel contains sul-fur that produces acids when burned, caus-

    tic was injected through a 1/4-in. line to

    neutralize the generator effluent. Two

    additional tubing strings were installed to

    verify operation. One was a continuous,fully sheathed, 1/8-in. thermocouple line

    and the other a1

    /4-in. sample return line.The final line was a 3/8-in. fuel line. A

    thermal packer with a short stinger hung

    below the generator. A cap on the end ofthe stinger was used to keep annulus flu-

    ids isolated from the generator assembly

    before operation.

    When the installation was complete,

    the operation was begun by blowing theplug off the end of the stinger. Then, a

    volume of air was injected through the

    generator to create a compressible cush-

    ion before ignition. Next, water injection

    began. Ignition was achieved by use of aslug of pyrophoric fluid that was injected

    into the diesel line that had first been

    flushed with water. When ignition was

    achieved, pressure transients wereobserved at the surface monitoring point.

    Usually 1 to 2 minutes were required for

    flows to quasistabilize. An increasing

    pressure was usually observed for a signif-

    icant period of time following initiation.Several problems occurred in the down-

    hole equipment. The lines for the fuel, air,

    and water had filters and check valves just

    above the steam generator to ensure that

    critical ports were not plugged and thatfluids from the formation could not flow

    back through the generator during shut-

    downs. In spite of corrosion inhibitors in

    the water supply, large quantities of corro-sion debris sloughed from the water line

    and began plugging that filter. The gener-

    ator had to be pulled, and the mesh size

    and accumulation volume increased.

    Improved production was observedduring this test because of the injected

    flue gases and their communication with

    surrounding production wells. The flue

    gases reduced the caloric value of the pro-duced market gas, but the blended pro-

    REFLECTIONS ON A DOWNHOLE

    STEAM GENERATOR

    This article is a synopsis of paper SPE

    38276, Reflections on a Downhole

    Steam-Generator Program, by A.B.

    Donaldson, SPE, New Mexico

    Highlands U., originally presented at

    the 1997 SPE Western Regional

    Meeting, Long Beach, California, 2527June.

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    72 JANUARY 1998

    E O R / I O R

    duction from the rest of the field kept the

    value within specifications.

    Surface Oxygen/Fuel Generator.

    Oxygen was used in one trial to eliminatethe large amount of noncondensable

    nitrogen and increase the partial pressure

    of carbon dioxide. This also eliminated

    compression equipment. While the exper-iment with oxygen did not have the sameoperational problems as the downhole

    unit, it had its share of difficulties. The

    major problem was survival time of the

    combustor can that isolated the combus-tion process from the injected water until

    combustion was complete. None of the

    conventional stainless steels used had suf-

    ficient strength to survive the very high

    thermal stresses caused by an oxygen/hydrocarbon flame.

    At the end of operations in the Long

    Beach,California, area, the apparent scarci-ty of oil disappeared and government fund-

    ing was reduced. A number of the projectteam members elected to leave Sandia and

    obtain nongovernment funding to attempt

    commercialization of the technology.

    Enhanced Energy Systems, Inc. (EESI). A

    number of deficiencies in the Sandia equip-

    ment were obvious after the field experi-

    ences. Manpower requirements and sophis-

    tication were excessive for oilfield applica-tions. The equipment was redesigned for

    commercial applications, with the goal ofone-person operation and the use of field

    gas or crude oil for generator fuel. The con-

    cept of steamdrive was replaced by huff n

    puff operation. Installation of the units

    downhole was difficult, and many of thelater operations were conducted with the

    generator on the surface.

    Hondo, Texas. The formation is shallow

    chalk with poor permeability and the pay

    is thin (from 7 to 40 ft). A major oil com-pany had attempted steaming in a shallow

    sand zone in the area, but the return was

    insufficient to continue the effort. Seven

    wells were stimulated. The casings hadsmall diameters, and the steam generatorwas installed at the surface with effluent

    conducted to the wells. Neither insulated

    injection string nor packer was used. Flue

    gases were injected into the formation with

    the steam. Because of poor injectivity, theequipment was operated at the lowest out-

    put, 2 million Btu/hr, at the maximum

    pressure, 1000 psi. The fuel used for the

    steam generator was site crude, and the

    location water had a high hardness.Production was improved from primary

    production but was not sufficient for fur-ther operation in this field.

    Hospah, New Mexico. The formation is

    a consolidated sand, approximately 1,100

    ft deep, with a thickness from 10 to 20 ft.

    The wells were not thermally insulated,and a downhole packer was not used. Fuel

    for the generator was old diesel. The injec-

    tivity of the wells was good, and some flue-

    gas production was observed at wells alongthe path of least resistance. The oil pro-

    duced was in the form of an emulsion.

    Various chemicals were used in an attempt

    to break the emulsion, but none was suc-

    cessful. Production increases were attrib-uted to creation of a high-pressure pocket

    of gas that blocked the cold-water seepage

    into the formation.

    Long Beach. This customer was the first

    to purchase a full line of equipment.

    Because of the complexity of equipmentand procedures, EESI personnel were

    retained to operate the equipment. Becausefield gas was available at this location, both

    the generator and compressors were fueled

    by site gas. Expansion cooling of the fuelgas led to icing conditions inside the con-

    trol valve, and the flow could not be

    bypassed. A desiccant was used to dry the

    gas. A major problem was controlling deliv-ery of fuel, air, and water 2,000 ft down-

    hole. A thermal packer was used to isolate

    the annulus from the reservoir, but filters

    and check valves were used sparingly. The

    equipment was designed to operate atapproximately 8 million Btu/hr at pressures

    up to 1,850 psi. Two wells were steamed

    with downhole units. One well was lost in

    this operation because of parted casing at

    400 ft.As operating experience was gained,

    many of the urgent operational bugs were

    found and corrected, and some reasonable

    periods of steam injection were experi-

    enced. The generator had to be pulled onone or two occasions because of deteriora-

    tion of the combustion-chamber wall. At

    this time, operation of the steam generator

    was returned to the surface and no further

    installations were made downhole.Two other nearby wells were cyclicly

    steamed from this surface location.

    Insulated surface-injection piping was used

    to transport the steam to the wells. Some ofthe most reliable operations occurred dur-

    ing this time. Peak production immediately

    after bringing the well back into production

    sometimes exceeded 500 BOPD, compared

    with a prestimulation production of 20 to40 BOPD. The customer calculated total

    production costs of approximately U.S.

    $12/bbl, which was the lowest of any of

    their production. Although conventionalsteam would probably have been economi-

    cally viable at this location, compliance

    with air-quality regulations was difficult.

    THE COMPLETION

    While conventional steam-generation tech-

    nology has the advantage of being the

    accepted technology for shallow reservoirs

    with good injectivity, there are some areaswhere improvements can be made. In insu-lated injection tubing currently available,

    heat losses at bare collars, expansion joints,

    packers, and subs almost negate the bene-

    fits of insulation unless the annulus is com-pletely dry. This conclusion is based on a

    water-reflux mechanism that occurs even

    when the annulus fluids are initially

    expelled. Residual water film or leaks into

    the annulus can generally be expected.

    CONCLUSIONS

    In general, no advantage was evident inplacing the generator downhole, particu-

    larly when injectivity of gases was a prob-

    lem. It was evident that injection of thecombustion gases was desirable in some

    cases and, in one case, necessary.

    Formations with poor injectivity are a

    major resource awaiting a viable recovery

    mechanism. Placement of a direct-contactsteam generator downhole is not a solution

    to this problem.

    RECOMMENDATIONS

    These recommendation focus on whatmodifications can be made to the downhole

    steam generator for successful stimulation

    of tight formations.

    New Concepts. A downhole steam genera-tor that does not produce nitrogen gas

    appears to offer potential for low-injectivity

    applications. There have been field trials of

    radio-frequency heating devices as well as

    one that uses electricity for energy. It isuncertain whether any of these have under-

    gone extensive field tests. One other possi-

    bility is to transpose submerged combus-

    tion technology developed for toxic-wastedisposal to oilfield applications. Anotheridea is to use the heat of mixing two fluid

    components that can be separated by distil-

    lation at the surface. A downhole heat

    exchanger would be used to heat feed water

    to steam, and the mixture of the two com-ponents would be returned to the surface

    for processing.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the syn-

    opsis has been taken has not been peerreviewed.

  • 8/10/2019 EOR-IOR

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    E O R / I O R

    Foam has the potential to relieve several

    common problems by better areal sweep,

    better vertical sweep, less viscous fingering,

    and lower handling costs when compared

    with gas-injection improved oil recovery(IOR). Foam may be introduced by contin-

    uous coinjection of gas and surfactant solu-

    tion or by injection of a slug of surfactant

    solution followed by injection of a gas slug,known as a surfactant-alternating-gas

    (SAG) process. SAG injection has certain

    advantages over continuous foam injectionin foam IOR processes. SAG injection min-

    imizes contact between gas and water in theinjection facilities, reducing corrosion, and

    can achieve high injectivity and low mobil-

    ity at the displacement front. High injectiv-

    ity results as foam near the well dries out,

    weakens, and collapses, while stronger,wetter foam farther from the well maintains

    mobility control. Recent simulation results

    show that SAG processes can overcome

    gravity override with less increase in injec-

    tion-well pressure than is possible withcontinuous foam injection.

    SCALEUP OF LABORATORY RESULTS

    There are a number of published coreflood

    studies where gas is injected into core sam-

    ples presaturated with surfactant solution.Some show foam persistence for many pore

    volumes (PVs) of gas injection. However,

    extrapolating these results directly to field

    scale is dangerous. Because of dispersive

    effects, the mobility within the shock frontmay exert influence in the length scale of a

    coreflood that does not occur in the field.

    Processes such as foam generation may

    occur slowly on the time scale of a core-flood but be virtually instantaneous on thetime scale of a field project. Unsteady-state

    displacements in a coreflood may not be

    directly proportional to field scale, and

    foam behavior in a reservoir may not be

    directly proportional to unsteady-state dis-

    placements in a coreflood. Capillary endeffects in a coreflood study may prevent

    water transport out of the core, prolonging

    foam life beyond that observed in a larger

    system without this effect. A more reliable

    procedure is to derive the fractional-flowcurve from the coreflood and then scale to

    reservoir size with fractional-flow methods.

    APPARATUS AND MATERIALS

    An unfired Berea core with a permeability of

    720 md and porosity of 0.22 was used in theexperiments. It was cut into a 9.5-in.-long

    right-circular cylinder. An N2 gas phase

    with a 1.0-wt% NaCl/0.01-wt% CaCl2/1.0-

    wt% surfactant aqueous phase was used.

    The coreholder, positioned downstream ofthe foam generator, held the core in a verti-

    cal position. The coreholder was designed

    to be lightweight so that the weight of the

    core could be measured effectively during

    the flood to determine water saturation, Sw.

    Flow lines were flexible, transparent nylon,

    and baffles were installed to restrict air flow

    around the apparatus and minimize exter-

    nal forces on the coreholder. Ports divided

    the length of the core into three sections of2.6, 2.75, and 4.15 in., respectively, from

    inlet to outlet. The weight of the system,

    with Sw in the core equal to one and zero,

    was measured before the tests, allowing

    determination of Sw during the test.

    One goal of these tests was to measurecap-illary pressure, Pc. A probe was designed that

    used a differential-pressure transducer to

    measure the pressure in the gas phase on oneside and pressure in the water phase on theother side of the transducer. A backpressure

    regulator maintained a steady backpressure of

    147 psi on the entire system during the two-

    phase flow. Differential-pressure transducers

    measured pressure drop, p, across each ofthe three sections of the core. All transducershad a range of 0 to 80 psi, and were calibrat-

    ed before the test. Data were recorded by a

    computerized data-acquisition system.

    EXPERIMENTAL STRATEGY

    Tests were performed at room temperature.The core was vacuum saturated with brine,

    then hundreds of PVs of brine were injected

    as backpressure was changed between 0 and

    100 psi to eliminate gas from the core.

    Backpressure was set at 147 psi at the end of

    the extended brine injection and held con-stant. Dozens of PVs of surfactant solution

    were then injected. Gas was then introduced

    with the surfactant solution at a water volu-

    metric fraction, fw, of 0.2. fw was incremen-

    tally reduced as pressure responses stabi-lized. When a minimum value of fw=0.002

    was reached, water injection ceased and anextended period of gas injection began.

    EXPERIMENTAL RESULTS

    Gas/Water Coinjection. The value of Sw was

    derived from measured weight. Two methods

    of estimating the amount of water in the dead

    volume were used. The first assumes that the

    imposed fw equals the water volume fractionin the endcap. The second is based on endcap

    weight that changes in a shorttime compared

    with changes that occur across the core. Both

    methods give qualitatively similar results.

    Water relative permeability,krw

    , values werecomputed from measured p with a form of

    Darcys law and with the assumption of a

    water viscosity of 1.0 cp. The measured p in

    Section 2 was used in all calculations to avoid

    end effects. Pc andp were measured, and Pcof the Berea computed from Sw values, by useof capillary pressure curves for unfired Berea

    during primary drainage, at values of N2/

    aqueous interfacial tension (33 dynes/cm),

    measured at room temperature. The Berea Pcwas computed to compare measured Pc withand without foam under the same conditions.

    Foam strength is characterized by its

    resistance factor (RF), the ratio of mobilitywithout foam to that with foam at the sameSw. An RF value of 1 indicates no foam,while an RF value of 100 means that the

    presence of foam has reduced gas mobility

    100 times more than gas mobility without

    foam at the same Sw. Computation of RF

    requires knowledge of gas relative perme-ability, krg, without foam. Because krg is

    high, and changed very little with the low

    values of Sw used in these tests, the value of

    krg was assumed to be 1.0.

    Results.When gas and water are injectedtogether, the foam is strong (RF2,000)

    COREFLOOD STUDY OF SURFACTANT-

    ALTERNATING-GAS FOAM PROCESSES

    This article is a synopsis of paper SPE

    38318,Coreflood Study of Surfactant-

    Alternating-Gas Foam Processes:

    Implications for Field Design, byK.R.

    Kibodeaux, SPE (now with Texaco E&P

    Technology), and W.R. Rossen, SPE, U.

    of Texas, originally presented at the

    1997 SPE Western Regional Meeting,Long Beach, California, 2527 June.

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    beforefw=0.008, then there is catastrophic

    weakening of the foam between fw=0.02

    andfw=0.008, followed by a gradual weak-ening asfw decreases. Foam strength is still

    appreciable (RF=25) after breakage, and

    foam collapse is not complete. When the

    foam breaks, fluid is absorbed and swellingresults (imbibition), accompanied by adecrease in Pc. As Sw increases, krw also

    increases as Pc drops. Measured values of Pcwere high, compared with those expected

    without foam.

    DISCUSSION

    In these tests, Pc was measured during foam

    flow in consolidated porous media for the

    first time. Foam is strong asPc increases to

    some limiting value. There is a critical Pcabove which foam lamellae rupture, and a

    limiting Pc value is expected to exist inporous media at which a strong foam weak-

    ens drastically. In these tests, the value of the

    critical Pc was approximately 12 psi. Otherinvestigators have reported a foam film sur-

    viving at Pc>17 psi. The Pc measurements,

    although unexpectedly high, were valid

    indications of the actual values in the core.

    One goal of this work was to apply frac-

    tional-flow methods and a coreflood-derived

    fw curve to scale up laboratory coreflood

    results. A time/distance diagram for an SAGprocess was generated from the fractional-

    flow curve. Mobility is high at the initial con-

    ditions behind the shock front. At the shock

    front, mobility is low, with spreading waves ofgently increasing mobility behind it. A foamof very low mobility exists in a thin, moving

    front composing the shock. Within this zone,

    foam forms, strengthens, exceeds critical Pc,

    and weakens. Fractional-flow theory states

    that all the points between initial conditionsand the shock on the fractional-flow curve,

    including the strong foam near fw=0.02, lie

    inside the the shock. This extremely strong

    foam within the narrow shock front improves

    the mobility ratio of the displacement with noadverse effect on injectivity.

    CONCLUSIONS

    1. Pc was measured during foam flow in

    consolidated porous media for the firsttime. Unexpectedly high Pc were measured

    in the presence of strong foam.

    2. Sw declined and Pc increased as injec-

    tion fw was reduced in steps to a point

    where foam abruptly weakened. This point

    is defined as the limiting Pc. The shape of

    the fractional-flow curve was similar to

    those proposed previously.3. When the foam weakened, imbibition

    occurred, with a increase in Sw and a

    decrease in Pc. This imbibition event, as

    well as multiple steady states of foam and amultivalued fractional-flow function, maycomplicate the use of fractional-flow meth-

    ods for foam-performance prediction.

    4. Coreflood results cannot be scaled direct-

    ly to field performance because both evapora-

    tion and capillary end effects alter water trans-port late in the flood. Using laboratory core-

    floods to derive fw as a function of Sw, then

    scaling up with fractional-flow methods or

    computer simulation, provides more reliable

    scaleup from the laboratory to the field.5. Results suggest moderate mobility

    reduction in a broad region behind theshock front, while weakened foam near the

    well allows good injectivity.

    Please read the full-length paper for addi-

    tional detail, illustrations, and references.

    The paper from which the synopsis has

    been taken has not been peer reviewed.

    JANUARY 1998 7 7

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    78 JANUARY 1998

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    On 17 May 1996, Total Minatome Corp.

    initiated an enhanced-oil-recovery (EOR)

    high-pressure air-injection project at the

    Horse Creek field in North Dakota. This

    project is the third high-pressure air-injec-tion program completed in the Ordovician

    Red River formation in the Williston basin.

    The Horse Creek field is 7 miles east of the

    Cedar Creek anticline, in the south centralportion of the Williston basin. The field was

    discovered in 1972 and comprised 15 pro-

    ducing oil wells. In 1993, geological, labo-ratory, and reservoir-modeling studies were

    conducted to evaluate the EOR potential ofthe field. On the basis of the results from

    these studies, an EOR unit for this field was

    formed in 1995. There are currently 11 pro-

    ducing wells, three air-injection wells, one

    monitor well, and one water-disposal wellwithin the unit area. Air is being injected

    into the reservoir at a rate of approximately

    8,500 Mscf/D at 4,700 psi discharge pres-

    sure. Nine months after injection began,

    the reservoir pressure continues to rise andproduction has increased from 293 to 400

    BOPD.

    RESERVOIR CHARACTERIZATION

    Geology. The Horse Creek field is a strati-

    graphic oil accumulation within theOrdovician Red River formation. The Red

    River formation in this portion of the

    Williston basin is subdivided into four

    porosity zones. These porosity zones are

    referred to as Zones A through D (Fig. 1).Air injection and production in the Horse

    Creek field has been limited to Zone D.

    The upper portion of the Red River for-

    mation consists of a series of briningupward, cyclic carbonates deposited in asubtidal to supratidal environment on a

    restricted shelf during the Red River marine

    transgression. Rock types include lime-

    stones, dolomites, and anhydrites.

    Lithology varies from laminated mudstones

    to heavily bioturbated packstones, wacke-

    stones, and mudstones. Dolomitization of

    the heavily bioturbated units has resultedin a secondary porosity within Zone D,

    from which the Horse Creek field produces.

    Stratigraphic cross sections, core data, and

    petrophysical-facies maps indicate that

    Zone D comprises two separate lobes thatare discontinuous across the field. The

    HORSE CREEK AIR-INJECTION

    PROJECT: AN OVERVIEW

    This article is a synopsis of paper SPE

    38359, The Horse Creek Air-Injection

    Project: An Overview, by B.C. Watts,

    T.F. Hall, SPE, and D.J. Petri, SPE,

    Total Minatome Corp., originally pre-

    sented at the 1997 SPE Rocky

    Mountain Regional Meeting, Casper,Wyoming, 1821 May.

    Fig. 1Horse Creek field type log.

    MASSIVEANHYDRITE

    GAMMA RAY

    8900

    9000

    9100

    9100

    GAMMA RAY

    DENSITY @

    CORE 2

    CORE 1

    C ZONE

    D ZONE

    A ZONE

    TOP RED RIVER

    B ZONE

    North Dakota

    DENSITY POROSITY30 10

    LITHOLOGY

    CORE DESCRIPTION

    DEPOSITIONALENVIRONMENT

    LAMINATEDMEMBER

    BURROWEDMEMBER

    SUPRATIDAL

    SUPRATIDAL

    TO

    UPPER

    INTERTIDAL

    (RESTRICTED

    FAUNA)

    LAMINATED

    DOLOMITIC

    MUDSTONE

    HEAVILYBURROWED

    PACKST/WAKESTDOLOMITE

    HEAVILYBURROWEDDOLOMITICMUDSTONE

    TIGHTLY BURROWED

    LIME MUDSTONE

    SUBTIDAL(NORMALMARINE)

    SUBTIDAL TOLOWER INTERTIDAL

    (NORMALMARINE)

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    lower unit of Zone D is one continuous

    unit that occurs across the entire field area.

    Porosity and Permeability. Porosity andpermeability in Red River Zone D are

    related to several stages of dolomitization.

    The highly burrowed subtidal to lower-

    intertidal lime muds in Zone D, whichcontain mainly macroporous pore throats(2 to 20 m), contain most of the reser-

    voir-quality porosity and permeability.

    Burrowing appears to have prepared these

    rocks for dolomitization and porosity

    development as compared with the sur-rounding nonburrowed, laminated

    supratidal to upper-intertidal lime muds,

    which, although porous, contain mainly

    microporous (0.2 to 0.5 m) pore throatsand are nonproductive. On the basis ofcore data, thin-section descriptions, and

    log analysis, reservoir-quality porosity isintercrystalline and ranges from 8 to 20%

    and averages 16%. Reservoir thickness

    ranges from 0 to 45 ft and averages 20 ft.Permeability ranges from 1 to 97 m, aver-

    aging 10 to 20 md.

    Net Pay. Net-pay thickness for Zone D was

    determined by log analysis. The log datawere calibrated with core data, and petro-

    physical values were calculated for all wells

    from digital data. Net-pay cutoffs deter-

    mined by porosity, permeability, produc-

    tion, and relative oil/water permeabilitydata were established at 12% porosity and

    water saturation < 50% for the primary

    (moveable) oil reserves.

    Original Oil in Place(OOIP).Well controlwithin the field is adequate to give a reliable

    estimation of effective OOIP. A porosity

    cutoff of 12%, average water saturation of

    35%, and a formation volume factor of

    1.205 yield an effective OOIP of 45.7 mil-lion bbl.

    PRODUCTION PERFORMANCE

    AND EOR POTENTIAL

    The primary producing mechanism for

    Zone D is liquid and rock expansion. A200- to 300-ft oil column has developed

    within the macroporous petrofacies.

    Production has included a water cut of

    approximately 60%, which has remainedconstant since the initial field production.

    The constant water cut and steady decline

    in reservoir pressure indicate that the trap-

    ping mechanism is stratigraphic and sug-

    gest that there is no active aquifer. Remain-ing primary reserves of 1.25 million bbl

    were calculated by decline-curve analysis.

    The primary recovery factor for the field is

    estimated to be 9.9% of OOIP.

    EOR Potential. Several different EOR

    methods were considered for the Horse

    Creek field. Waterflooding was ruled out

    because of oil and water relative permeabil-

    ity differences which, coupled with the cur-rent water saturation, impeded the ability ofthe oil to form a bank, reducing recovery.

    Gas (N2 and CO2) injection was eliminated

    because of excessively high costs.

    The process finally selected was high-

    pressure air injection. This method provid-ed all the benefits of waterflooding and gas

    injection. Technical parameters contribut-

    ing to this decision include the following.

    1. Reservoir temperature of 220F, indi-

    cating that in-situ oxidation would occurspontaneously without downhole igniters.

    2. Oil with a gravity of 32 API and agood affinity for oxidation.

    3. An in-situ oxidation process with ahigh oxygen-utilization rate that indicated

    good oil recovery.

    4. Rapid field repressurization that

    would restore reservoir pressure and

    enhance early oil recovery.The decision to use the air-injection

    method was influenced by the favorable

    comparison of reservoir and fluid parame-

    ters from the Horse Creek field with the

    successful air-injection programs at twoother units in the same field.

    RESERVOIR AND

    LABORATORY STUDIES

    A series of reservoir models, simulations,

    and laboratory studies was conducted toevaluate the EOR potential and to ensure

    that the most efficient and economical

    recovery process was used.

    Pressure/Volume/Temperature (PVT)

    Analysis.A PVT analysis of the oil was per-

    formed and included differential liberation

    and N2 swelling tests.

    Waterflood Study. A waterflood studyindicated that the field was not a good

    waterflood candidate because of unfavor-

    able water/oil relative permeabilities and a

    low incremental-recovery factor. On the

    basis of this study, waterflooding was ruledout as a possible EOR process.

    Black-Oil Models. The first phase of the

    reservoir modeling consisted of a black-oil

    model of the southern portion of the field.

    The objective of this model was to confirm

    the volumetric assumption in this portionof the field and to estimate the incremental

    recovery from gas injection. Results from

    this model were encouraging and led to the

    decision to construct a full-field model.The objectives of the full-field black-oil

    model were (1) to acquire a full-field his-

    tory match and confirm the volumetric

    OOIP, (2) to verify the lack of water influx

    into the reservoir, (3) to examine the reser-voir response to gas injection, and (4) to

    provide a reservoir model for subsequent

    simulations. Several different production

    scenarios were tested with various injec-

    tion rates and injection-well locations.Model results indicated that the best pro-

    duction scenario included three injection

    wells with an initial injection rate of 10

    MMscf/D. The model estimated incremen-tal oil recovery of 7.6 million bbl. Fast and

    reliable results from the black-oil model

    enabled an initial economic projection to

    be made for the project.

    Accelerating Rate Calorimeter (ARC)

    Tests. ARC tests were conducted to assessthe oil oxidation kinetic parameters under

    quasiadiabatic conditions. Results from

    these tests are qualitative but help to deter-

    mine the range of conditions under which

    the oil will react with air. Two main oxida-tion reactions were detected by the ARC

    tests. The first reaction began at 279 to

    315F and was described as a low-tempera-

    ture oxidation (LTO) reaction that pro-

    duced polar compounds. The second reac-tion, which began at 404 to 441F, is the

    reaction that would produce significant

    quantities of CO and CO2. Results from the

    ARC test indicated that the oil would react

    under low-temperature conditions.

    Combustion-Tube Burns. Two combus-

    tion-tube burns were performed at the U.

    of Calgary to quantify the combustion

    characteristics of the rock, oil, and brine.Both burns were conducted in a 6-ft-long

    vessel with a 4-in.-diameter core from the

    Horse Creek field. The experiments used

    different air-flux rates and ignition tem-peratures to assess the displacementprocess. The results indicated that a pro-

    gressing temperature front is established at

    approximately 600F. This temperature

    range is indicative of LTO. The steady

    thermal-front displacement, low airrequirement, low fuel load, and high per-

    centage of oil recovered indicated an effi-

    cient recovery process.

    Thermal Model. To obtain parameters to

    describe the oil oxidation kinetics, a ther-

    mal simulation of the combustion-tube-burn experiments was performed. A match

    JANUARY 1998 79

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    of the combustion-tube results was

    obtained by use of a simple, complete oxy-

    gen combustion with no coke formation.

    Air-Injection Radial Model. An air-injec-

    tion radial model was built with a thermal

    simulator to study the conditions around

    an air-injection well. This was importantbecause air-injection startup is the mostcritical phase of project operations. The

    radial model used the reservoir properties

    from the full-field black-oil model and the

    kinetic parameters from thermal modelingof the combustion-tube experiments. The

    following are some important results from

    the thermal model.

    1. Temperature Profile. The temperature

    of the oxidation front was from 500 to700F. Following 15 years of injection, the

    heated zone was estimated to be a cylinder

    with a diameter of approximately 900 ft.2. Oxygen Behavior in the Reservoir.

    Oxygen was consumed in a rapid and sta-ble reaction. After 15 years of injection,

    oxygen did not move beyond a radius of

    500 ft from the injection well. The model

    predicted that no oxygen would reach a fic-

    titious producer located 3,500 ft from theinjection well.

    3. Hetrogeneities. Sensitivity cases with

    vertical permeabilities from 1 to 300 md

    showed no oxygen breakthrough and indi-cated that the oxygen did not go beyond a

    radius of 700 ft from the injection well.

    Full-Field Thermal Simulation. The final

    phase of reservoir study included a full-field model with a thermal simulator. The

    model used the reservoir properties fromthe full-field black-oil model along with a

    compositional description of the oil and

    introduction of chemical reactions that

    enable oil oxidation and CO2 formation.

    Predictive-model runs were performed for a20-year period, with air-injection rates

    averaging 10 MMscf/D. Several different

    injection scenarios were examined to deter-

    mine the optimum location and number ofair-injection wells. The main results fromthe thermal simulation follow.

    1. Incremental oil recovery was estimat-

    ed at 7.2 to 7.9 million bbl.

    2. The oxidization front did not go

    beyond 3,500 ft from the injection well.3. Oxygen breakthrough did not occur in

    the producing wells.

    4. The incremental recovery with air

    injection was approximately 10% more

    than with nitrogen injection.5. Gas sweeping and reservoir repressur-

    ization are the main mechanisms influenc-ing incremental recovery in this light-oil

    reservoir. Viscosity reduction is not a sig-

    nificant factor.The results of the full-field thermal sim-

    ulation confirmed the economic feasibility

    of the project. Data from thermal simula-

    tion helped to define a field production-

    monitoring program that was implemented

    in the field.

    PRODUCTION FACILITIES

    Engineering for the project facilities began

    in March 1995. Detailed design of the com-

    pressors was completed and contracts for

    their construction were awarded in April1995. Detailed engineering for all other

    phases of the compression facility were

    completed, and construction on the plant

    foundations and installation of the 13-mile

    fuel-gas pipeline were initiated. The com-pressors were delivered in December 1995,

    and construction of the remaining facilities,including piping, instrumentation, well

    conversions, and installation of high-pres-sure air lines, was completed during the

    first quarter of 1996.

    The injection plant for the Horse Creek

    project was designed (1) to build safety

    and redundancy into all systems, (2) toprovide computer control and call-out

    warning systems, and (3) to meter and

    control rate and pressure accurately to

    each injection well.

    Compressors for the project were select-ed on the basis of field-proven perfor-

    mance and ability to supply the project

    requirement of 10 MMscf/D at 5,000 psi.

    Two Integral 8 throw, seven-stage conpres-sors, driven by two V-16 turbo-charged

    natural gas engines, are used to compress

    the air.

    Before air injection could begin, two pro-

    ducing wells had to be converted to air-injection wells and one new injection well

    had to be drilled and completed. All injec-

    tion wells were fitted with high-pressure

    wellheads and permanent air-injection

    packers with 23/8-in. tubing with premium

    two-step connections, and 20,000 ft of 23/8-in. 5,000-psi air-injection lines was

    installed from the compression facility tothe injection wells. All production wells in

    the unit are equipped with 23/8-in.

    anchored tubing and have beam pumps.

    Each producing well has its own produc-

    tion facility.

    Safety and Environment Factors. Special

    precautions must be implemented to pre-

    vent explosions of hydrocarbons when

    using high-pressure air injection. To reduce

    this risk, the following equipment, materi-als, and processes were employed.

    1. Special packers, two-step tubing con-

    nections, and innovative pressure testing to

    minimize the potential for downhole leaks.2. Special high-temperature lubricants

    for the compressors, wellheads, and tubing

    to minimize the danger of explosion.

    3. Passivation of all tubulars to reduce

    internal rust, corrosion, and scale.4. Wellhead controls at the injection wells

    to prevent backflow and overpresssuring.

    5. Dual compressors to add redundancy

    and maintain constant injection to the

    reservoir.6. A nitrogen-deployment system to

    ensure continuous positive pressure to the

    reservoir in the event that both compres-

    sors malfunctioned at the same time.7. An emergency generator to provide

    automatic electrical backup in the event of

    a power failure.

    PROJECT PERFORMANCE

    The average gas/oil ratio has decreased

    with repressurization of the reservior. Theaverage bottomhole pressure has increased

    approximately 550 psi. Average daily pro-

    duction rate has increased from 293 BOPD

    to approximately 400 BOPD. All these

    changes were predicted by the reservoir-simulation studies. On the basis of the lim-

    ited production history, the production

    goal of 1,100 to 1,300 BOPD probably will

    be met.

    CONCLUSIONS

    1. The EOR potential of the Horse Creek

    field was determined by an integrated team

    of geologists and engineers.

    2. A black-oil model provided fast andreliable predictions of incremental recovery

    and production required to make initial

    economic projections and business deci-

    sions for the project.

    3. ARC and combustion-tube experi-ments provided the kinetic parameters for

    thermal modeling and indicated that air

    injection would be an efficient recovery

    process.4. Thermal simulation of the project pro-

    vided the ability to examine different pro-

    duction scenarios to test injector locations

    and production results.

    5. Production results to date indicatethat the project is proceeding as predicted

    by the reservoir models and simulation

    studies.

    Please read the full-length paper for addi-

    tional detail, illustrations, and references.

    The paper from which the synopsis hasbeen taken has not been peer reviewed.

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    JANUARY 1998 81

    E O R / I O R

    Polymer flooding is an enhanced-oil-

    recovery method with great potential in

    the Daqing oil field. Many new problems

    will be encountered producing crude oil

    mixed with polymer solution. During thewaterflood development phase, the

    oil/water mixture is treated as a

    Newtonian fluid. Analysis of oilfield fluids

    indicates that fluids produced by polymerflooding are non-Newtonian and that con-

    ventional methods of calculating inflow-

    performance-relationship (IPR) curvescannot be used. This paper considers the

    variation of rheological properties of fluidproduced from polymer-flooded reservoirs

    on the basis of core-displacement and rhe-

    ological-property experiments.

    RHEOLOGICAL PROPERTIES

    OF IN-SITU FLUID

    The in-situ fluid in polymer-flooded reser-

    voirs is a mixture of aqueous polymer

    solution and crude oil. Many studies have

    been conducted to determine the rheolog-

    ical properties of polymer solutions, butno studies have been published on their

    rheological-property variation in the direc-

    tion of flow. Rheological properties of

    polymer solutions change continuously

    along the flow direction as a result ofadsorption, retention, and shear degrada-

    tion of the solution. In laboratory dis-

    placement tests, the viscosity of a polymer

    solution was measured at different outlet

    points in an artificial column core.Apparent viscosity decreases in the direc-

    tion of flow. Assuming a power-law fluid,

    the consistency coefficient, k, decreases

    sharply near the inlet of the core and con-tinues to decrease slowly in the directionof flow, and the power-law exponent, n,

    increases in the direction of flow. This

    indicates that larger molecules of the poly-

    mer are degraded and the non-Newtonian

    behavior of the polymer solution is

    reduced in the direction of flow.

    FLOW BEHAVIOR OF POLYMER-

    SOLUTION/OIL MIXTURE

    Core-displacement experiments were per-

    formed in the laboratory to compare thebehavior of polymer-solution/oil mixtures

    with different volume ratios with that ofsingle-phase polymer solution. When pres-

    sure drop is plotted vs. equivalent shear

    rate on a log-log graph, the polymer-solu-tion/oil mixture plots are identical to that

    for polymer alone at shear rates greater

    than 10 seconds-1. This indicates that a sin-

    gle-phase fluid model can be used to calcu-

    late the pressure drop of polymer-solu-tion/oil mixtures.When flow rate and pres-

    sure drop through a core are plotted, the

    pressure drop varies linearly with the nth

    power of the flow rate. The relationship of

    pressure drop and flow rate exhibits thebehavior of a non-Newtonian power-law

    fluid in the porous media. At high flow

    rates, the pressure drop increases, deviating

    from the power-law model, indicating that

    the rheological properties of the polymersolution in porous media are not the same

    as in a capillary tube.

    IPR CURVES FOR OIL WELLS

    The apparent viscosity of polymer solution

    varies greatly during the time the solutionis mixed at the surface, injected, and finally

    produced with the oil. In the Daqing oil

    field, the apparent viscosity decreasesapproximately 30% from the time it ismixed to the time it reaches the injection

    wells. Apparent viscosity decreases 60%

    when it reaches an observation well 30 m

    from the injection well and 70% at a pro-

    duction well 106 m away. This indicatesthat the loss of apparent viscosity is large

    near injection wells. Severe shear degrada-

    tion of large polymer clumps usually occurs

    near the bottom of injection wells, decreas-

    ing the non-Newtonian behavior of thepolymer solution. When the shear rate is

    greater than the critical shear rate, the fluidexhibits viscoelastic behavior in the vicini-

    ty of the wellbore and power-law fluid

    behavior in the formation. The full-length

    paper contains a differential equation forinflow performance. This equation com-

    bines equations of continuity, motion, and

    state. Boundary conditions are defined.

    Calculations. An IPR curve was calculatedwith the derived equation. When calculat-

    ed flowing bottomhole pressures were com-pared with measured values, the maximum

    absolute error was 230 kPa and the maxi-mum relative error was 5.82%. The close

    agreement of measured and predicted val-

    ues indicates that variable rheological para-meters must be used to predict IPRs for oil

    wells in polymer-flooded reservoirs.

    Analysis of IPR curves of oil wells shows

    that, when the rheological parameters offluid vary in injection and production

    wells, the pressure drop in the formation

    increases as the k of the produced fluid

    increases and n decreases. Pressure drops

    decrease ask decreases and n increases.

    Case History and Influence Factors.

    Polymer-solution rheological parameters

    were measured for an oil well in a poly-

    mer-flooded reservoir in the Daqing oil

    field with a permeability of 475 md, and aporosity of 0.267. The concentration of

    the injected polymer solution was 1000

    mg/L, k = 0.0809 Pas, and n = 0.5637.The value of k for the fluid produced from

    an oil well in this field was 0.0145 Pasand n was 0.809.

    CONCLUSIONS

    1. Rheological properties of formationfluids in polymer-flooded reservoirs change

    in the direction of flow.2. Calculations of IPR curves for oil wells

    in polymer-flooded reservoirs need to

    include variations of rheological properties as

    the fluids flow through the reservoir.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the syn-

    opsis has been taken has not been peerreviewed.

    CALCULATION OF IPR CURVES FOR OIL

    WELLS IN POLYMER-FLOOD RESERVOIRS

    This article is a synopsis of paper SPE

    38936, Calculation of IPR Curves of

    Oil Wells for Polymer-Flooding Reser-

    voirs, by Yue XiangAn, SPE, Xia

    Huifen, Yunxiang Zhang, and Li

    Jingyuan, Daqing Petroleum Inst., orig-

    inal ly presented at the 1997 SPE

    Annual Technical Conference and

    Exhibition, San Antonio, Texas, 58October.

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    Field testing has confirmed that a newly

    discovered, modified hot-lime process

    (MHLP) is a significant improvement overexisting precipitation-softening options. A

    Permian Basin produced oilfield water

    containing 2,000 ppm hardness, 500 ppm

    sulfides, 10,000 total dissolved solids

    (TDS), and 200 ppm oil is being convert-ed successfully to steam-generator-quality

    feedwater. Alkali consumption and sludgeproduction have been reduced by 50%

    compared with the conventional process.In addition, alkali consumption by

    entrained CO2 is eliminated. Many hot-

    lime softeners (HLSs) currently in service

    can be inexpensively converted to this

    more efficient process.

    The lack of economical water treatmentis one of the most critical obstacles to

    achieving a successful steam-injection pro-

    ject. Because of strict environmental regula-

    tions and lack of available fresh water, pro-

    duced oilfield water is typically used assource water for steam generation. For

    most steamfloods, quality of the produced

    water is fair and sufficient treating can be

    accomplished with typical oil-removal andsoftening techniques. In many west Texas

    oil fields, however, produced-water quality

    is much worse than that currently used for

    steam generation. Hardness and sulfide lev-

    els are 10 times the average for Californiasteamflood source waters.

    Identification of the significant reserves

    and economic potential of a thermal project

    in a large west Texas oil field led Marathon

    Oil Co. to embark on an operational steamfield test in 1995. The test consisted of

    installation of a 5,000-BWPD oilfield

    water purification facility and three sin-

    gle-pass waste-heat steam generators and

    drilling of one steam-injection well.

    WATER QUALITY

    Steam for most oilfield steamflooding is

    produced in conventional steam genera-tors. These generators are fired with nat-

    ural gas or waste heat and use a single-

    pass tube arrangement to produce 80-

    quality steam. Saturated steam (including

    the 20% liquid phase) is injected into theoil formation with steam-injection wells.

    Many impurities in the steam-generatorfeedwater can be tolerated because the

    20% liquid phase provides a place forthem to concentrate and still remain solu-

    ble. However, according to typical steam-

    generator-manufacturer guidelines, all oil,

    sulfides, hardness, and suspended solids

    must be removed to prevent damage tosteam-generator tubes. Oil in the feedwa-

    ter contributes to film formation and cok-

    ing in the generator tubes, resulting in

    their eventual failure. Sulfides are

    believed to be corrosive. Hardness deposi-tion creates steam-generator scaling,

    eventually leading to hot spots and tube

    failures. Suspended solids must be

    removed because they contribute to for-

    mation of steam-generator sludge. Typicalsteamflood source waters contain 200 ppm

    hardness and essentially no sulfides. The

    extremely high amounts of hardness and

    sulfides in the source water in this westTexas field made their removal the major

    challenge for a successful project.

    OVERALL PROCESS FLOW

    Produced oilfield water first enters a hydro-

    cyclone for rough-cut oil and water separa-tion. Oil content is reduced from 200 to 40ppm. Next, single-media filters are used to

    reduce oil content further to 10 to 20 ppm.

    Water then enters a packed column, where

    nitrogen at 4 scf/gal is used to reduce sul-

    fide levels from 500 to< 200 ppm. An oxy-gen scavenger is added to reduce oxygen

    content from 20 to approximately 0 ppb.

    Water is then pumped to the modified hot-

    lime softener (MHLS), where heat, lime,

    and caustic are added. Hardness is reducedfrom 2000 to 4 ppm here. Anthracite filters

    are used next to remove any suspended cal-cium carbonate (CaCO3) and magnesium

    hydroxide [Mg(OH)2] precipitates. Weak

    acid cation vessels are then used to polish

    hardness to

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    E O R / I O R

    water and collected in the lower cone or

    solid/liquid separation chamber. Here, pre-

    cipitated material is separated from the soft-

    ened water in the form of sludge. Periodic

    blowdown is performed to remove thismaterial from the vessel.

    MHLP. After additional laboratory and field

    testing, a new, more efficient method was

    discovered and commercially demonstrated.The process is a variation of the standard

    HLP. Fig. 2 shows a schematic of the modi-

    fied vessel. Instead of adding heat, lime

    and/or caustic simultaneously to precipitatehardness, as in the existing HLP, the MHLP

    precipitates hardness in two separate steps.In the first step, cold, hard water enters the

    vessel and is sprayed into a steam atmos-

    phere and heated to near boiling, just as in

    the standard HLP. Soda ash can be added atthis point to supply the necessary bicarbon-

    ate ion for hardness precipitation if the ion

    is not present in sufficient quantities natu-

    rally. However, instead of adding lime or

    caustic soda at this point, the MHLP allowsretention time for precipitation reactions

    resulting from only the addition of heat totake place. Laboratory and field testing has

    shown that 10 to 20 minutes is required for

    completion of thermal softening reactions at

    vessel operating temperatures. If less reten-tion time is allotted (as with the HLP), ther-

    mal reactions will not take place. Instead,

    the preference for reactions with lime and

    caustic overrides thermal reactions. The

    amount of thermal softening that takesplace can be significant. In the field test,

    produced oilfield water was softened from

    2,000 to < 1,000 ppm in this step, with-

    out any chemical addition.The second step of the MHLP consists of

    adding lime and/or caustic soda to precipi-tate hardness not removed during thermal

    softening in the first step. Chemical reac-

    tions that take place are identical to those in

    the HLP. Resulting reactions from the addi-

    tion of heat and chemicals form CaCO3 andMg(OH)2 precipitates. The amount of pre-

    cipitates generated by the MHLP is signifi-cantly less than that of the HLP. Only 1

    mole of CaCO3 is created per mole of hard-

    ness during Step 1 (thermal softening)compared with 2 moles /mole of hardness

    generated in Step 2 (lime softening). This

    translates to a significant reduction in the

    amount of precipitated solids. Typically

    these solids are hauled to a landfill, whichcan prove costly. The MHLP has several

    additional benefits.

    1. Improved Removal of H2S. H2S is diffi-

    cult to remove from water at elevated pH.

    Because the typical HLP quickly elevateswater pH by introducing lime early, gaseous

    H2S is converted to ionic sulfide, which

    cannot be removed. The MHLP does not

    elevate pH significantly for several minutes,

    so H2S is removed by steam deaerationmuch more effectively.

    2. Elimination of Lime Consumption by

    CO2. The standard HLP introduces lime

    into the vessel in the steam/vapor space

    where CO2 can exist. CO2 dissolved in the

    produced water will react with added limeand create CaCO3. Therefore, the presence

    of CO2 increases alkali demand and

    increases the amount of precipitated solids,both of which are unfavorable. The MHLPeliminates these problems because the alka-

    li is introduced below the water level in the

    vessel. CO2 does not exist in water at HLP

    temperatures (it is driven off by Step 1 heat-

    ing) and therefore cannot consume lime.

    Existing HLS can be inexpensively con-verted to this more efficient process. Most

    vessel designs currently in service afford

    necessary retention time for thermal reac-

    tions to occur in the reaction chamber ofthe vessel. The primary modification

    required for conversion is lowering thealkali feed point from the top of the reac-

    tion chamber to the top of the reaction

    chamber downcomer.

    USE OF TWO ALKALIS TO

    IMPROVE PERFORMANCE OF THE

    PRECIPITATION PROCESS

    When lime alone is used, pH must be main-

    tained in the very tight pH range of 9.3 to9.6 to achieve acceptable effluent hardnesslevels. If the pH levels fall outside this

    range, hardness levels climb quickly. To

    overcome this chemistry problem, both

    lime and caustic are fed to precipitate

    hardness in the HLS. After thermal soft-ening takes place in the upper portion of

    the reaction chamber, hydrated lime is

    added to boost the pH to near 9.0.

    Hardness is reduced to approximately 100ppm. The result is precipitation of large

    amounts of hardness with cheap lime. A

    relatively small amount of caustic soda isthen added to precipitate the majority of

    remaining hardness. Because caustic sodais free of calcium ions, hardness does not

    increase when overfed. While caustic

    could be used exclusively and accomplish

    the same result, the relatively high cost of

    the chemical makes this economicallyunattractive for high-hardness waters.

    Fig. 1HLS vessel.

    Solid/Liquid

    SeparationChamber

    Fig. 2MHLS vessel.

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    In addition to producing CaCO3 and

    Mg(OH)2, sodium carbonate (Na2CO3) or

    soda ash is also formed by caustic reactions.

    Presence of these excess carbonates allowsthe process to achieve extremely low hard-

    ness levels. Effluent hardness levels less

    than 4 ppm have been routinely achieved in

    the precipitation softener.

    TEST PROJECT OPERATING

    CHALLENGES

    Plugging. The MHLS has been in service

    for more than 1 year. After design refine-

    ments were complete, operating efficiencyand operability have surpassed expecta-

    tions in many respects. However, the

    major operational challenge still facing

    the vessel is periodic plugging of the reac-

    tion chamber and downcomer with pre-cipitated hardness. Field testing estab-

    lished that standard HLSs require signifi-cant modification to accommodate the

    solids generated from precipitation soft-ening of west Texas produced oilfield

    water. With the standard design HLS,

    operation would be halted after 2 weeks

    because of a plugged reaction-chamber

    downcomer. Through a series of improve-ments, periods of run time for the MHLS

    extended significantly. Those modifica-

    tions include the following.

    1. Enlargement of the reaction-chamber

    downcomer. Typically, reaction-chamberdowncomers are sized to achieve a down-

    ward water velocity of 1 ft/sec. Field expe-

    rience indicates that a more appropriate

    design criterion for extremely hard waters

    is 0.5 ft/sec.2. Modification of the downcomer

    splashplate to a witchs hat design.

    Standard HLSs use a flat plate at the bottom

    of the reaction-chamber downcomer to pre-vent disturbance of the sludge below. Field

    testing operations suggested that the stan-

    dard splashplate design allowed precipitat-

    ed solids to stack, eventually plugging the

    downcomer. The current witchs hat design

    allows solids to slough off much moreeffectively.

    3. Creation of a high-rate cyclonic

    motion in the 10-ft-diameter reaction

    chamber with tangential nozzles. To keepprecipitated solids in suspension as water

    moves down the downcomer, 600 gal/min

    of water (from the reaction chamber) is

    recirculated.4. Use of a steeper-sloped reaction-cham-

    ber cone. Standard HLS design calls for a

    45 from horizontal cone in the reaction

    chamber, even though the sludge repose

    angle is greater than 50. Future vesseldesigns will use a 60 from horizontal cone

    in an attempt to alleviate the plugging ten-

    dencies further.

    Sulfide Removal. Sulfide removal from the

    source water was the second significant

    technical challenge for project engineers.

    Removal of an extremely large amount of

    sulfides (500 ppm) in steam-generatorfeedwater is very unusual. Use of conven-tional methods to accomplish this would

    adversely affect water-treating costs.

    Initially, complete sulfide removal, as

    recommended by steam-generator-manu-facturers guidelines, was thought to be

    necessary. Experience from other steam-

    flood operators, however, indicated that

    this was not necessarily true. Steamflood

    operators in California have operated foryears with source waters containing 40

    ppm sulfides and have reported no signif-

    icant problems. With this information, atwo-pronged strategy to the sulfide issue

    was adopted. First, an uncommon sulfide-removal technique would be engineered

    and installed that would reduce sulfide

    levels to less than 40 ppm. Second, field-

    testing facilities would be used to deter-mine whether higher sulfide levels were

    tolerable. For example, if the upper sul-

    fide level limit could be extended to 200

    ppm, water-treating costs would be

    reduced, thereby improving project eco-nomics. Also, field experience found that

    sulfide levels below 200 ppm prevented

    interference with hardness reactions in

    the MHLS. Sulfides under certain condi-

    tions were found to tie up available car-bonate alkalinity needed for the process,

    thereby creating permanent hardness in

    the water.

    After more than 1 year of steam injection,

    no significant corrosion is evident in thewater plant or steam system with boiler

    feedwater containing 200 ppm sulfides.

    Therefore, 200 ppm sulfides will be the

    newly established upper sulfide target forfuture water-plant designs. Nitrogen with-

    out any sort of pH adjustment will be usedto accomplish this level of reduction.

    Conventional Sulfide Removal. Sulfides

    exist in both ionic and gaseous forms at pHlevels of typical oilfield waters. To remove

    all sulfides, water pH must be lowered to

    below 5 to convert ionic sulfide to H2S.

    Hydrochloric acid is the agent used typical-ly for pH reduction. H2S can then be

    removed effectively with conventional

    stripping techniques. The problem with

    using conventional methods before a pre-

    cipitation process is that added acid signifi-

    cantly reduces the amount of alkalinityneeded for hardness precipitation. Lost

    alkalinity must therefore be replaced in the

    form of Na2CO3. This approach of elimi-

    nating alkalinity with acid to remove sul-

    fides, then replenishing that lost alkalinitywith an additional chemical, is expensive

    and unnecessary.

    Uncommon Sulfide Removal Method.

    The original sulfide removal techniqueused CO2 as both the stripping gas andagent for pH reduction. CO2 forms carbon-

    ic acid, bicarbonate, and carbonate when

    dissolved in water. The free hydrogen-ions

    released by dissociation of carbonic acid

    reduce the pH of the water. Laboratory andfield testing indicate the water pH can be

    reduced to less than 5 by dissolved CO2.

    Because the reactions are reversible, no

    adverse effect on alkalinity occurs.

    Nitrogen is not as effective as CO2 becausethe water pH actually increases as a result of

    stripping of entrained CO2 with the sul-fides. Blending even small amounts of CO2into the nitrogen stream significantly

    improves packed-column performance.Adding only 10% CO2 to the nitrogen strip-

    ping gas stream removes an additional 90

    ppm of sulfides. Any CO2 dissolved in the

    water is effectively removed by heating in

    the downstream HLS.

    CONCLUSIONS

    1. A new process for converting hard oil-

    field water to boiler-quality feedwater has

    been developed and commercially demon-strated. Alkali consumption and sludge

    production have been reduced by 50%,

    compared with the standard HLP.

    2. The addition of small amounts of caus-

    tic soda to the MHLP enhances the stabilityand efficiency of softening in high-hardness

    west Texas source waters.

    3. CO2 is effective at removing sulfides

    from water without adversely affecting

    water chemistry in regard to softening.However, piping and vessels exposed to

    dissolved CO2 must be protected to pre-

    vent corrosion caused by carbonic acid.

    4. Sulfide levels up to 200 ppm in steam-generator feedwater have resulted in no sig-nificant corrosion to steam generation and

    distribution equipment after 1 year of oper-

    ation. At a typical produced-water pH, this

    level of reduction can be accomplished

    with nitrogen.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the syn-

    opsis has been taken has not been peerreviewed.

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    E O R / I O R

    The Simonette Beaverhill Lake A and B

    pools were discovered in September 1993.

    Enhanced recovery (EOR) by water-alter-

    nating-gas (WAG) miscible flooding was

    initiated in May 1995. This short, 20-

    month cycle time was achieved through

    careful planning, multifunctional team

    work, and close cooperation between the

    partners in all critical decisions. The chal-

    lenges to develop Simonette, including uni-

    tizing, well spacing and scheduling, con-

    serving gas, and selecting the type of floodwere identified in a development plan cre-

    ated before discovery. Keys to economic

    success were also identified in the planning

    stage. When the discovery was made, a

    multidisciplinary development team was

    formed. Much effort was spent on under-

    standing and meeting the needs of all inter-

    ested parties, including partners and regu-

    latory agencies.

    GEOLOGY

    Oil is trapped in the Simonette Beaverhill

    Lake A and B pools in the updip culmina-tion of a Swan Hills reef, a part of the

    Beaverhill Lake group. The Beaverhill Lake

    group comprises the Swan Hills formation,

    consisting of reefal carbonates, and the

    Waterways formation, composed of basin-

    filling marlstones and carbonate mud-

    stones. The A pool is separated from the B

    pool by a normal fault with approximately

    30 m of throw. The reefs were deposited in

    a series of eight reef stages that grew in

    response to rising sea levels. Development

    and management of the reservoir is driven

    by the properties and relationships of thesestages. Stage porosities within a well range

    from 7 to 12%, and permeabilities can

    range from 1 to 400 md.

    PLANNING

    Exploration Economics. The Simonette

    exploration prospect was characterized as

    having a geologic risk of one in five and

    recoverable oil from 795 to 5500103 m3.

    The area ranged from 24 to 40106 m2.

    Net pay was expected to be from 7.5 to

    12.0 m. The original development plan

    called for a waterflood with 65-ha spac-ing, the same as most Beaverhill Lake

    reservoirs in Alberta, and a nominal five-

    spot pattern. With the estimated

    exploratory risk of one in five, the

    prospect was considered uneconomical.

    The performance of other Beaverhill

    Lake reservoirs showed that 80% of the

    recovery was obtained from 20% of the

    wells. Flood-front mapping of other

    waterfloods showed that water injectors

    could sweep oil as much as 4.83 km. The

    performance of these reservoirs caused

    the development plan to be revised to use

    130-ha spacing.

    Improved Oil Recovery (IOR). Implicit in

    the economic evaluation was the need for

    EOR. Expected primary recovery factors

    were 10 to 20%, which would not support

    the well investment and facilities cost.

    Waterflooding was considered the mini-

    mum depletion mechanism. In addition,

    the Alberta Energy and Utilities Board

    (AEUB) limits production from a reservoir

    by a maximum rate limitation (MRL) that istypically 9000 m3 per month/1106 m3 of

    recoverable oil.

    Development Plan Goals. A Gantt Chart

    for the development plan was presented

    to management. If this extremely aggres-

    sive timeline could be met and the pool

    developed on 130-ha spacing, the explo-

    ration economics were very attractive.

    The following were major challenges in

    the timeline.

    Designing and selecting a flood with

    only three to four wells out of an ulti-mate pool development of 19 wells.

    Obtaining AEUB approval in 3 months

    with limited data when 6 to 12 months

    is typical.

    Unitizing the pool within 2 years, withthe same data limitations.

    After management was assured that the

    timeline would be met, approval was

    given for drilling the discovery well in

    June 1993. After discovery, water injec-tion was achieved 6 months ahead of plan

    and gas injection began 4 months ahead

    of the injection target date.

    LABORATORY STUDIES

    Reservoir fluid studies and laboratorycorefloods are critical sources of data for

    designing and selecting a flood scheme for

    a reservoir. Representative samples from

    the dominant flow facies were selected for

    waterflood tests, relative permeabilitydetermination, and (combined with fluid

    studies) miscible flooding potential. A set

    of capillary pressure curves, covering a

    range of porosities and permeabilities, was

    determined. These data were gathered tocreate a permeability transform to popu-

    late a reservoir-simulation model. The

    composition analysis revealed that solu-

    tion gas from Simonette could be used as amiscible solvent for the oil. This finding

    was instrumental in the decision to use a

    miscible flood.

    REGULATORY ENGAGEMENT

    The AEUB must approve all recovery

    schemes as part of their mandate to con-serve the energy resources of Alberta. AEUB

    approval can take up to 1 year if they iden-

    tify issues with a proposed scheme thatrequire additional laboratory or simulationstudies. Because approval was required

    within 3 months of application with little

    data, a meeting was held to explain the

    nature of the reservoir, development plans,

    and the need for a short cycle time. Thestaff of the AEUB raised several questions.

    The objectives of the simulation studies

    were set to address these. The AEUB staff

    was kept informed of the findings and con-

    clusions of various studies. The final appli-cation was submitted in October 1994 with

    data from only three wells. The applicationwas updated with information from an

    A MODERN EXAMPLE OF SHORT-CYCLE-

    TIME DEVELOPMENT

    This article is a synopsis of paper SPE

    38824, Simonette Beaverhil l Lake

    A&B Pools: A Modern Example of

    Short-Cycle-Time Development, by

    T.J. Moynihan, SPE, Chevron Canada

    Resources; J.C. Fryters, Chevron

    Petroleum Technology Co.; and P.

    Chernik, SPE, Shell Canada Ltd. origi-

    nal ly presented at the 1997 SPE

    Annual Technical Conference and

    Exhibition, San Antonio, Texas, 58October.

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    additional five wells in January 1995, and

    approval of miscible flood for the Simonette

    A pool was obtained in March 1995.

    EARLY PERFORMANCE

    MONITORING

    As each well was drilled, a temporary bat-

    tery was installed at the wellsite. T


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