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L-MT-14-075 ENCLOSURE 5 WESTINGHOUSE LETTER REPORT, LTR-BWR-ENG-14-034-NP NON-PROPRIETARY INVESTIGATION INTO THE CAUSE OF EXCEEDING THE LEVEL 1 (L1) AND LEVEL 2 (L2) LIMIT CURVES GENERATED BASED ON 2011 MONTICELLO MAIN STEAM LINE STRAIN GAUGE DATA 51 pages follow
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Page 1: LTR-BWR-ENG-14-034-NP, 'Investigation into the Cause of … · 2014-10-14 · LTR-BWR-ENG-14-034-NP, Revision 1 1 Background In early 2014, during power ascension activities (at 1864

L-MT-14-075

ENCLOSURE 5

WESTINGHOUSE LETTER REPORT, LTR-BWR-ENG-14-034-NPNON-PROPRIETARY

INVESTIGATION INTO THE CAUSE OF EXCEEDINGTHE LEVEL 1 (L1) AND LEVEL 2 (L2) LIMIT CURVES GENERATED

BASED ON 2011 MONTICELLO MAIN STEAM LINE STRAIN GAUGE DATA

51 pages follow

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Westinghouse Non-Proprietary Class 3

LTR-BWR-ENG- 14-034-NP

Investigation into the Cause of Exceeding the

Level 1 (LI) and Level 2 (L2) Limit Curves

Generated Based on 2011 Monticello Main

Steam Line Strain Gauge Data

September 5, 2014

Westinghouse Electric Company LLC1000 Westinghouse Drive

Cranberry Township, PA 16066 USA

© 2014 Westinghouse Electric Company LLCAll Rights Reserved

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Westinghouse Non-Proprietary Class 3 LTR-BWR-ENG-14-034-NP, Revision 1

1

 

Background In early 2014, during power ascension activities (at 1864 MWt) for the extended power uprate (EPU) license amendment, the United States Nuclear Regulatory Commission (U.S. NRC) questioned the accuracy of certain steam dryer data that had been provided as information by Monticello Nuclear Generating Plant (MNGP). After investigation, Northern States Power Minnesota (NSPM) discovered that data errors existed in the replacement steam dryer (RSD) analyses. The errors consisted of 1) a strain gauge (SG) adjustment factor in the data acquisition system (DAS) that was set to a value that reduced the amplitude of the data acquired by a constant factor and; 2) an inadvertent reversal of main steam line (MSL) strain gauge signals, on MSL C, [ ]a,c In Reference 1, the NRC requested additional information (RAIs) related to this issue. NSPM/Westinghouse Electric Company reanalyzed the steam dryer performance using corrected information without changing the benchmark methodology and provided this analysis in response to the RAI request (Reference 2). The minimum alternating stress ratio (MASR) for operation at 2004 MWt that was used to derive the benchmark limit curves in References 2 and 3 [ ]a,c These limit curves were generated based on the 2011 MSL pressure power spectral densities (PSDs) to be consistent for comparison with past work.

Following this submittal, the NRC informally requested that pressure PSDs calculated based on 2014 data, recorded at 1775 MWt, be plotted against the new limit curves provided as part of Reference 2. On August 6, 2014, Xcel Energy recorded a MSL strain gauge dataset at the 1775 MWt thermal power level. Westinghouse has evaluated this dataset and plotted the MSL pressure PSDs against the limit curves derived based on corrected 2011 SG data. [ ]a,c Operability analyses existed and were enhanced to verify that the steam dryer was operable at 1775 MWt and at previous operation that included short periods at power levels up to 1864 MWt.

[ ]a,c A new set of limit curves, developed based on August 6, 2011 data, is also provided. A separate document will be provided to the NRC that describes the alternate power ascension process that NSPM/Westinghouse Electric Company will use to perform the remainder of EPU power ascension testing.

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

References

1. Email from T Beltz (NRC) to J Fields (NSPM), "Monticello Nuclear Generating Plant -Draft Request for Additional Information (EMCB) in Support of EPU Power Ascension(TAC No. MF3330)," dated May 15, 2014. (Attached in EDMS)

2. Letter from K Fili (NSPM), "Monticello Extended Power Uprate: Replacement SteamDryer - Response to NRC Requests for Additional Information, Revised Limit Curvesand Supporting Information (TAC No. MF3330)," July 22, 2014. (Attached in EDMS)

3. Westinghouse Letter LTR-BWR-ENG-14-010, Revision 1, "Responses to the US NRCRequest for Additional Information Relative to the Monticello Replacement Steam DryerAcoustic/Structural Analyses Set #7," July 18, 2014.

4. Xcel Energy Design Information Transmittal (DIT) 1353, "EPU Data Acquisition System(DAS) Main Steam Line (MSL) Data," August 6, 2014.

5. Xcel Energy Design Information Transmittal (DIT) EC-13638, "Transmittal of SIA LetterAMK-1 1-001, Revision 1 confirming that the pressure conversion factors remainunchanged and strain gage data taken during power ascension following the spring 2011refuel outage," June 2011.

6. Structural Integrity Associates Report 1301246.406.R2, "Investigation of SignalDiscrepancies in Extended Power Uprate Strain Gage Data," April 10, 2014.

7. Structural Integrity Associates Report 1301246.407.RO, "Review of Strain Gage SignalPerformance over Extended Time Periods," August 14, 2014.

8. Westinghouse Letter LTR-BSA-14-9, Revision 0, "Monticello Power AscensionAssessment of 105% of CLTP Power Level Data," May 17, 2014.

9. Westinghouse Letter LTR-BWR-ENG-14-031, Revision 0, "Monticello Steam DryerStructural Integrity," August 14, 2014.

10. Structural Integrity Associates Report 1301246.408.RO, "Summary of Onsite DASFunctionality Verification," August 26, 2014.

2

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-14-034-NP

Evaluation

Westinghouse has evaluated the 1775 MWt dataset, transmitted from Xcel Energy toWestinghouse on August 6, 2014 in Reference 4.

a,c

]a,c

The LI and L2 curves in Figures 1A through 8C are based on the MASR consistent with the2011 MSL SG data projected to 2004 MWt in Reference 3.

[

Table 2Recirculation Pump Speeds for 2011 and 2014

]a,c

a,b,c

3

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-14-034-NP

Ii

Ia,c

3.SvrlcanlIaecage

lgtyfo

01t 04

Ia,c

3. Several channels have changed slightly from 2011 to 2014. []a,c The changes include:

0 [

Ia,c

0 [

]a,c

I

Ia,c

From the SIA study, [

Ia,c

4

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

II

]a,c

a I

Ia,c

I

Ia,c

I

I a,c

The changes to the MASR for MSL SG datasets taken at different times are summarized inTable 2.

Table 2I I a,c

a,b,c

5

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

Conclusion

Ia,c

6

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-14-034-NP

a,b,c

Figure 1-A MSL A Upstream0-250 Hz

7

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-14-034-NP

a,b,c

Figure 1-B MSL A Upstream0-100 Hz

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a,b,c

Figure 1-C MSL A Upstream100-250 Hz

9

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 1 4-034-NP

a,b,c

Figure 2-A MSL A Downstream0-250 Hz

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

a,b,c

Figure 2-B MSL A Downstream0-100 Hz

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a,b,c

Figure 2-C MSL A Downstream100-250 Hz

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a,b,c

Figure 3-A MSL B Upstream0-250 Hz

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a,b,c

Figure 3-B MSL B Upstream0-100 Hz

14

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-14-034-NP

a,b,c

Figure 3-C MSL B Upstream100-250 Hz

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

a,b,c

Figure 4-A MSL B Downstream0-250 Hz

16

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a,b,c

Figure 4-B MSL B Downstream0-100 Hz

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a,b,c

Figure 4-C MSL B Downstream100-250 Hz

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a,b,c

Figure 5-A MSL C Upstream0-250 Hz

19

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

a,b,c

Figure 5-B MSL C Upstream0-100 Hz

20

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG-1 4-034-NP

a,b,c

Figure 5-C MSL C Upstream100-250 Hz

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 1 4-034-NP

7 a,b,c

Figure 6-A MSL C Downstream0-250 Hz

22

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a,b,c

Figure 6-B MSL C Downstream0-100 Hz

23

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

a,b,c

Figure 6-C MSL C Downstream100-250 Hz

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

a,b,c

Figure 7-A MSL D Upstream0-250 Hz

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a,b,c

Figure 7-B MSL D Upstream0-100 Hz

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

a,b,c

Figure 7-C MSL D Upstream100-250 Hz

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a,b,c

Figure 8-A MSL D Downstream0-250 Hz

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a,b,c

Figure 8-B MSL D Downstream0-100 Hz

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a,b,c

Figure 8-C MSL D Downstream100-250 Hz

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a,b,c

Figure 9 [Ia,c

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a,b,c

Figure 10 [Ia,c

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

a,b,c

Figure 11 [Ia,c

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

a,b,c

Figure 12 [Ia,c

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

I a,b,c

Figure 13 [Ia,c

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- 14-034-NP

7a,b,c

Figure 14 [Iaxc

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2 a,b,c

Figure 15 [I aC

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- a,b,c

Figure 16 [I a,c

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Westinghouse Non-Proprietary Class 3LTR-BWR-ENG- I 4-034-NP

Figure 17 Sample Plant 2, MSL A Upper

a,b,c

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Figure 18 Sample Plant 2, MSL A Lower

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a,b,c

Figure 19 Sample Plant 2, MSL D Upper

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a,b,c

Figure 20 Sample Plant 2, D Lower

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a,b,c

Figure 21 MSL A Upstream

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a,b,c

Figure 22 MSL A Downstream

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a,b,c

Figure 23 MSL B Upstream

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Figure 24 MSL B Downstream

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a,b,c

Figure 25 MSL C Upstream

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a,b,c

Figure 26 MSL C Downstream

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a,b,c

Figure 27 MSL D Upstream

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Westinghouse Non-Proprietary Class 3LTR-B WR-ENG- I 4-034-NP

a,b,c

Figure 28 MSL D Downstream

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